Showing 39,107 complaints for PONTIAC
Incident date: Mar 10, 2015
GOT KEY FOB RECALL DONE, NOW THE IGNITION SWITCH IS NOT ACCEPTING THE KEY AT ALL MAKING IT VERY HARD TO TURN THE KEY TO ON AND START POSITION AS IF THE SWITCH IS IN LOCK POSITION BEFORE DRIVING. AFTER DRIVING DOWN THE ROAD A BIT THE IGNITION SWITCH SHUTS THE CAR OFF MAKING ME HAVE TO RESTART THE CAR WHILE IM DRIVING DOWN THE ROAD. THIS SHOULD BE A RECALL NOT ONLY FOR MY CAR BUT FOR ALL PONTIACS LI
... KE MINE THAT ARE 2004 AND UP. THIS COULD CAUSE SERIOUS INJURY OR AN ACCIDENT IF ITS NOT FIXED. I DRIVE SAFE AND HAVE KIDS IN THE CAR AT ALL TIMES. I SHOULDN'T HAVE TO FIGHT WITH THE IGNITION SWITCH TO TURN MY KEY TO START POSITION. ANOTHER THING TO GET FIXED, THE TRACTION LIGHT AND ABS LIGHT COMES ON AUTOMATICALLY IN REVERSE AND STAYS ON UNTIL THE CAR IS PARKED. *TRRead more
Incident date: Mar 10, 2015
GOT KEY FOB RECALL DONE, NOW THE IGNITION SWITCH IS NOT ACCEPTING THE KEY AT ALL MAKING IT VERY HARD TO TURN THE KEY TO ON AND START POSITION AS IF THE SWITCH IS IN LOCK POSITION BEFORE DRIVING. AFTER DRIVING DOWN THE ROAD A BIT THE IGNITION SWITCH SHUTS THE CAR OFF MAKING ME HAVE TO RESTART THE CAR WHILE IM DRIVING DOWN THE ROAD. THIS SHOULD BE A RECALL NOT ONLY FOR MY CAR BUT FOR ALL PONTIACS LI
... KE MINE THAT ARE 2004 AND UP. THIS COULD CAUSE SERIOUS INJURY OR AN ACCIDENT IF ITS NOT FIXED. I DRIVE SAFE AND HAVE KIDS IN THE CAR AT ALL TIMES. I SHOULDN'T HAVE TO FIGHT WITH THE IGNITION SWITCH TO TURN MY KEY TO START POSITION. ANOTHER THING TO GET FIXED, THE TRACTION LIGHT AND ABS LIGHT COMES ON AUTOMATICALLY IN REVERSE AND STAYS ON UNTIL THE CAR IS PARKED. *TRRead more
Incident date: Feb 4, 2015
TL* THE CONTACT OWNS A 2007 PONTIAC G6 . ON SEVERAL OCCASIONS, THE LOW BEAM HEADLIGHTS STOPPED ILLUMINATING. THE CONTACT REPLACED THE LIGHT BULBS MULTIPLE TIMES, BUT THE LIGHTS CONTINUED TO BURN OUT. WHILE REPLACING THE BULBS, IT WAS DISCOVERED THAT BOTH LIGHT BULB SOCKETS EXPERIENCED BURNING AND MELTING. THE CONTACT INDICATED THAT THE ODOR OF BURNING PLASTIC WAS PRESENT WHEN THE HEADLIGHTS WERE A
... CTIVATED FOR EXTENDED PERIODS OF TIME. THE CAUSE OF THE FAILURE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 68,000.Read more
Fire
Incident date: Apr 15, 2015
THE VAN WHEN IN PARK WILL REVIVE THE ENGINE AND JUMP, WHEN STOPPING WITH NEW BRAKES AND ALL THAT FUN STUFF WHEN THE VAN IS DOING THIS REVIVING STATE IT TAKES LONGER TO STOP AND LIKE THE VAN IS FIGHTING IT. IT SOMETIMES OVER SHIFTS WHEN IN THIS STATE WHEN TAKING OFF FROM A LIGHT (DOES THE REVIVING THING WHEN MOVING. I AM AFRAID ONE DAY IT IS GOING TO JUMP AND HIT SOMETHING OR SOME ONE OR NOT STOP.
... *TRRead more
Incident date: Apr 14, 2015
2007 PONTIAC SOLSTICE WITH JUST OVER 20,000 MILES ON IT, THIS SHOULD NOT HAPPEN. I AM MEMBER OF PONTIAC FORUM, I KNOW OTHERS HAVE SAME PROBLEM AND YOU HAVE THEIR INFO. THIS IS A HUGE SAFETY CONCERN. PASSENGER AIR BAG ON LIGHT DOES NOT COME ON, STAYS OFF WITH PASSENGER. , SERVICE AIR BAG MESSAGE ON DIC.. *TR
Incident date: Apr 14, 2015
TOOK MY CAR TO [XXX] BECAUSE POWER STEERING CONTROL MODULE WENT OUT THE SAME PART THAT THEY BEEN RECALLING ON THERE OTHER CARS. WHEN I CALLED CHEVROLET THEY SAID THAT THERE IS NO RECALL ON MY CAR AND THAT THERE WAS NOTHING THAT THEY CAN DO FOR ME BUT WORK WITH THE PRICING. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR
Incident date: Mar 25, 2015
I WAS DRIVING AT A RATE OF 45 MPH AND MY STEERING WHEEL LOCKED UP ON ME WHICH CAUSED ME TO GO TOWARDS IN COMING TRAFFIC LUCKILY THE CAR I WAS HEADED TOWARDS STOPPED. I TRIED TO TURN MY STEERING WHEEL BACK TO THE RIGHT BUT NOTHING HAPPENED. I HAD TO STOP MY CAR IN THE MIDDLE OF THE ROAD TO TURN MY STEERING WHEEL BECAUSE IT WAS SO HARD TO TURN. THE GENTLEMAN IN THE OTHER CAR GOT OUT TO HELP ME MOVE
... MY CAR OUT OF THE ROAD, AND HE WAS ABLE TO TURN THE STEERING WHEEL. HE TOLD ME TO TURN IT OFF AND TURN IT BACK ON AND THEN I WAS ABLE TO DRIVE IT WITHOUT IT LOCKING BACK UP ON ME THAT DAY. SINCE THEN I HAVE HAD IT LOCK UP ON ME WHILE BACKING OUT OR TURNING INTO THE PARKING GARAGE AT WORK ON MULTIPLE OCCASIONS. *TRRead more
Incident date: Apr 13, 2015
TL* THE CONTACT OWNS A 2006 PONTIAC SOLSTICE. THE CONTACT STATED THAT THE AIR BAG WARNING LAMP FLASHED INDICATING TO SERVICE THE AIR BAGS. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 14V047000 (AIR BAGS, ELECTRICAL SYSTEM). THE VEHICLE WAS TO BE TAKEN TO AN AUTHORIZED DEALER FOR FURTHER INSPECTION. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS NOT AVAILABLE.
Incident date: Apr 13, 2015
TL* THE CONTACT OWNS A 2006 PONTIAC SOLSTICE. THE CONTACT STATED THAT THE AIR BAG WARNING LAMP FLASHED INDICATING TO SERVICE THE AIR BAGS. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 14V047000 (AIR BAGS, ELECTRICAL SYSTEM). THE VEHICLE WAS TO BE TAKEN TO AN AUTHORIZED DEALER FOR FURTHER INSPECTION. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS NOT AVAILABLE.
Incident date: Apr 1, 2015
HEADLAMP WIRING IS DEFECTIVE FROM THE FACTORY. HEADLAMP WIRING AND CONNECTORS BURN OUT DUE TO INABILITY TO WITHSTAND HEAT GENERATED BY NORMAL FACTORY HEADLAMP BULBS. THIS IS A WIDELY KNOWN PROBLEM. NUMEROUS COMPLAINTS EXIST ON THIS SITE, IN ADDITION TO SERVICE BULLETINS. EVERY MECHANIC IN TOWN, DEALERSHIP, BODY SHOP, ETC. SAYS THE SAME THING. "UNTIL THEY ISSUE A RECALL, THERE IS NOTHING WE CA
... N DO BUT KEEP CHARGING YOU TO FIX THE CONNECTOR." I HAVE PAID THREE TIMES TO HAVE THIS ISSUE FIXED AND MY CAR HAS 62,000 MILES ON IT. WHEN WILL SOMEONE INVESTIGATE THIS AND ISSUE A PROPER RECALL? IT IS NOT SAFE TO HAVE YOUR HEADLIGHTS SUDDENLY GO OUT WHEN DRIVING 75 MPH ON THE INTERSTATE IN THE MIDDLE OF THE NIGHT. *TRRead more
Incident date: Apr 1, 2015
HEADLAMP WIRING IS DEFECTIVE FROM THE FACTORY. HEADLAMP WIRING AND CONNECTORS BURN OUT DUE TO INABILITY TO WITHSTAND HEAT GENERATED BY NORMAL FACTORY HEADLAMP BULBS. THIS IS A WIDELY KNOWN PROBLEM. NUMEROUS COMPLAINTS EXIST ON THIS SITE, IN ADDITION TO SERVICE BULLETINS. EVERY MECHANIC IN TOWN, DEALERSHIP, BODY SHOP, ETC. SAYS THE SAME THING. "UNTIL THEY ISSUE A RECALL, THERE IS NOTHING WE CA
... N DO BUT KEEP CHARGING YOU TO FIX THE CONNECTOR." I HAVE PAID THREE TIMES TO HAVE THIS ISSUE FIXED AND MY CAR HAS 62,000 MILES ON IT. WHEN WILL SOMEONE INVESTIGATE THIS AND ISSUE A PROPER RECALL? IT IS NOT SAFE TO HAVE YOUR HEADLIGHTS SUDDENLY GO OUT WHEN DRIVING 75 MPH ON THE INTERSTATE IN THE MIDDLE OF THE NIGHT. *TRRead more
Incident date: Apr 10, 2015
DRIVER SIDE HEADLIGHT WENT OUT , I REPLACED IT 3 TIMES IN ONE WEEK. I THEN GO ON THE INTERNET AND GOOGLE THE PROBLEM I WAS HAVING WITH MY G6. THERE WAS OVER 500 THOUSANDS RESULTS OF PEOPLE HAVING THE SAME PROBLEM AS ME . SO WENT TO REPLACE THE HEADLIGHT AGAIN AND LOOKED FOR ANY CORROSION, UNPLUGGED MY HEADLIGHT THAT WAS SUPPOSED TO BE BLOWN AND IT WASN'T , I PLUGGED THAT SAME HEADLIGHT BA
... CK IN AND IT CAME ON. I CALLED GM , AND COMPLAIN ABOUT THIS PROBLEM AND WAS TOLD I WOULD HAVE TO TAKE IT TO THE DEALERSHIP AND HAVE IT FIXED AT MY COST. VERY DISAPPOINTED IN GM! *TRRead more
Incident date: Apr 7, 2015
ON 4/7/15, WHILE DRIVING HEARD CHIMES. ALL ICONS ON INSTRUMENT PANEL TURNED ON. THE FUEL GAUGE NEEDLE MOVED TO EMPTY. THE LOW FUEL GAUGE TURNED ON. ALL THIS INDICATING MALFUNCTION. THE ODOMETER TURNED OFF AND THE CODE ERROR CAME ON AND TURNED OFF; THEN THE ODOMETER CAME BACK ON. ALL THE ICONS ON THE INSTRUMENT PANEL TURNED OFF EXCEPT FOR THE SECURITY LIGHT ICON WHICH STAYED ON. IT FELT AS
... IF SOMEONE WAS ATTEMPTING TO DISABLE MY VEHICLE. LATER THAT DAY TURNED THE VEHICLE ON AND EVERYTHING SEEMED NORMAL, LIKE IT RESET ITSELF. ON 4/8/15, AFTER DRIVING APPROXIMATELY 70 MILES ON THE HIGHWAY, THE SECURITY LIGHT ICON TURNED ON AND STAYED ON. I TOOK THE VEHICLE DIRECTLY TO THE DEALER AND THEY INFORMED ME THEY WOULD HAVE TO DIAGNOSE THE VEHICLE. THE RESULT WAS INCONCLUSIVE, THEY DID NOT FIND ANYTHING WRONG. SO NOT ONLY WAS I PUT IN AN UNSAFE CONDITION, THIS END UP COSTING ME $140.00 JUST TO TELL ME THEY COULD NOT FIND ANYTHING - NOT ONLY AM I IN THE HOLE FOR $140 BUT I AM BACK TO SQUARE ONE. I FEEL GM SHOULD FOOT THIS BILL AS A CUSTOMER COURTESY DUE TO THE PREDICAMENT THIS VEHICLE PUT ME IN. THIS SHOULD NEVER HAVE HAPPENED TO A VEHICLE THAT IS 6 YEARS OLD AND 80,000 MILES. *TRRead more
Incident date: Apr 7, 2015
ON 4/7/15, WHILE DRIVING HEARD CHIMES. ALL ICONS ON INSTRUMENT PANEL TURNED ON. THE FUEL GAUGE NEEDLE MOVED TO EMPTY. THE LOW FUEL GAUGE TURNED ON. ALL THIS INDICATING MALFUNCTION. THE ODOMETER TURNED OFF AND THE CODE ERROR CAME ON AND TURNED OFF; THEN THE ODOMETER CAME BACK ON. ALL THE ICONS ON THE INSTRUMENT PANEL TURNED OFF EXCEPT FOR THE SECURITY LIGHT ICON WHICH STAYED ON. IT FELT AS
... IF SOMEONE WAS ATTEMPTING TO DISABLE MY VEHICLE. LATER THAT DAY TURNED THE VEHICLE ON AND EVERYTHING SEEMED NORMAL, LIKE IT RESET ITSELF. ON 4/8/15, AFTER DRIVING APPROXIMATELY 70 MILES ON THE HIGHWAY, THE SECURITY LIGHT ICON TURNED ON AND STAYED ON. I TOOK THE VEHICLE DIRECTLY TO THE DEALER AND THEY INFORMED ME THEY WOULD HAVE TO DIAGNOSE THE VEHICLE. THE RESULT WAS INCONCLUSIVE, THEY DID NOT FIND ANYTHING WRONG. SO NOT ONLY WAS I PUT IN AN UNSAFE CONDITION, THIS END UP COSTING ME $140.00 JUST TO TELL ME THEY COULD NOT FIND ANYTHING - NOT ONLY AM I IN THE HOLE FOR $140 BUT I AM BACK TO SQUARE ONE. I FEEL GM SHOULD FOOT THIS BILL AS A CUSTOMER COURTESY DUE TO THE PREDICAMENT THIS VEHICLE PUT ME IN. THIS SHOULD NEVER HAVE HAPPENED TO A VEHICLE THAT IS 6 YEARS OLD AND 80,000 MILES. *TRRead more
Incident date: Apr 7, 2015
ON 4/7/15, WHILE DRIVING HEARD CHIMES. ALL ICONS ON INSTRUMENT PANEL TURNED ON. THE FUEL GAUGE NEEDLE MOVED TO EMPTY. THE LOW FUEL GAUGE TURNED ON. ALL THIS INDICATING MALFUNCTION. THE ODOMETER TURNED OFF AND THE CODE ERROR CAME ON AND TURNED OFF; THEN THE ODOMETER CAME BACK ON. ALL THE ICONS ON THE INSTRUMENT PANEL TURNED OFF EXCEPT FOR THE SECURITY LIGHT ICON WHICH STAYED ON. IT FELT AS
... IF SOMEONE WAS ATTEMPTING TO DISABLE MY VEHICLE. LATER THAT DAY TURNED THE VEHICLE ON AND EVERYTHING SEEMED NORMAL, LIKE IT RESET ITSELF. ON 4/8/15, AFTER DRIVING APPROXIMATELY 70 MILES ON THE HIGHWAY, THE SECURITY LIGHT ICON TURNED ON AND STAYED ON. I TOOK THE VEHICLE DIRECTLY TO THE DEALER AND THEY INFORMED ME THEY WOULD HAVE TO DIAGNOSE THE VEHICLE. THE RESULT WAS INCONCLUSIVE, THEY DID NOT FIND ANYTHING WRONG. SO NOT ONLY WAS I PUT IN AN UNSAFE CONDITION, THIS END UP COSTING ME $140.00 JUST TO TELL ME THEY COULD NOT FIND ANYTHING - NOT ONLY AM I IN THE HOLE FOR $140 BUT I AM BACK TO SQUARE ONE. I FEEL GM SHOULD FOOT THIS BILL AS A CUSTOMER COURTESY DUE TO THE PREDICAMENT THIS VEHICLE PUT ME IN. THIS SHOULD NEVER HAVE HAPPENED TO A VEHICLE THAT IS 6 YEARS OLD AND 80,000 MILES. *TRRead more
Incident date: Apr 6, 2015
TL* THE CONTACT OWNS A 2009 PONTIAC G6. WHILE DRIVING 40 MPH, THE STEERING WHEEL SEIZED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC, WHO DIAGNOSED THAT THE STEERING INPUT SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 46,000.
Incident date: Apr 13, 2015
WHILE DRIVING ON THE HIGHWAY AT 70 THE CAR SHIFTED TO PARK AND THEN SHIFTED BACK TO DRIVE ON IT'S OWN. *TR
Incident date: Apr 12, 2015
TL* THE CONTACT OWNS A 1999 PONTIAC GRAND AM. WHILE DRIVING AT APPROXIMATELY 55 MPH, THE VEHICLE SUDDENLY STALLED WITHOUT WARNING. THE FAILURE RECURRED TWICE. THE CONTACT WAS ABLE TO RESTART THE VEHICLE. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 111,000. UPDATED 6/30/15*CN UPDATED 07/02/15*JB
Incident date: Apr 12, 2015
TL* THE CONTACT OWNS A 1999 PONTIAC GRAND AM. WHILE DRIVING AT APPROXIMATELY 55 MPH, THE VEHICLE SUDDENLY STALLED WITHOUT WARNING. THE FAILURE RECURRED TWICE. THE CONTACT WAS ABLE TO RESTART THE VEHICLE. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 111,000. UPDATED 6/30/15*CN UPDATED 07/02/15*JB
Incident date: Nov 1, 2009
DAUGHTERS IN 2006 SOLSTICE. DRUNK DRIVER RAN RED LIGHT GOING 50 MPH AND HIT OUR DAUGHTERS MAKING A LEFT TURN. SEVERE IMPACT ON AN ANGLE (FRONT/LEFT SIDE) WITH 2 FOOT INTRUSION INTO OCCUPANT COMPARTMENT. AIRBAGS DID NOT DEPLOY. REQUIRED PROLONGED EXTRICATION; SERIOUS INJURY WITH BAYFLIGHT TO HOSPITAL. 2006 SOLSTICE IS A GM RECALL VEHICLE FOR DEFECTIVE IGNITION SWITCH. *TR
Crash
2 injured
Incident date: Nov 1, 2009
DAUGHTERS IN 2006 SOLSTICE. DRUNK DRIVER RAN RED LIGHT GOING 50 MPH AND HIT OUR DAUGHTERS MAKING A LEFT TURN. SEVERE IMPACT ON AN ANGLE (FRONT/LEFT SIDE) WITH 2 FOOT INTRUSION INTO OCCUPANT COMPARTMENT. AIRBAGS DID NOT DEPLOY. REQUIRED PROLONGED EXTRICATION; SERIOUS INJURY WITH BAYFLIGHT TO HOSPITAL. 2006 SOLSTICE IS A GM RECALL VEHICLE FOR DEFECTIVE IGNITION SWITCH. *TR
Crash
2 injured
Incident date: May 28, 2010
2005 PONTIAC GRAND AM. CONSUMER WRITES IN REGARDS TO IGNITION SWITCH RECALL REPAIR WORK AND CONSUMER SEEKS REIMBURSEMENT. *SMD
Incident date: Apr 12, 2015
I RECENTLY PURCHASED A USED 2007 PONTIAC GRAND PRIX GT SEDAN. SHORTLY AFTER DRIVING THE VEHICLE OFF OF THE LOT, I WENT TO TURN ONTO A STREET TRAVELING ROUGHLY FIVE TO SEVEN MILES PER HOUR, AND THE TRACTION CONTROL AND ABS SENSOR LIGHT BOTH REGISTERED ACROSS THE SYSTEM INFORMATION SCREEN AND NOTED THAT I NEEDED TO SERVICE THE ABS SYSTEM AND TRACTION CONTROL SYSTEM. I IMMEDIATELY TOOK THE VEHICLE TO
... MY MECHANIC WHO SUGGESTED THAT WE START LOOKING ONLINE TO SEE IF THERE WERE A RECALL FOR THIS ISSUE. AFTERLOOKING ONLINE, WE NOTED THAT MULTIPLE OTHERS HAVE EXPERIENCED THE EXACT SAME ISSUE. MOST OF THE FIXES THAT WE HAVE SEEN THAT OTHERS HAVE TRIED WE HAVE ALSO TRIED, BUT NOTHING SEEMS TO FIX THE ISSUE. NOW THE TRACTION CONTROL AND ABS SYSTEM LIGHT ARE ON 90 PERCENT OF THE TIME AND IT HAS BECOME AN ISSUE WITH THE BRAKES. AT APPROXIMATELY 12 A.M. THIS MORNING, I TRIED TO STOP THE VEHICLE AND IT WOULD NOT RESPOND TO THE BRAKES. THERE WAS A GRINDING SOUND COMING FROM THE RIGHT SIDE OF THE CAR, ESPECIALLY WHEN I TRIED TO TURN THE WHEEL TO THE LEFT VERY HARD TO AVOID AN ACCIDENT. I WAS ABLE TO GET THE CAR TO STOP BY HITTING THE EMERGENCY BRAKE. AT THE TIME OF THE INCIDENT BOTH THE TRACTION CONTROL AND ABS LIGHTS WERE NOT REGISTERING ON THE SCREEN. NOW THE SERVICE ENGINE SOON LIGHT HAS STARTED TO APPEAR EVERY TIME I START THE CAR. THIS IS THE FIFTH OR SIXTH TIME IN THE LAST MONTH THAT THE BRAKES HAVE NOT RESPONDED. MY MECHANIC AND I ARE BOTH AT OUR WITS END TRYING TO FIGURE THIS ISSUE OUT. IT IS UNSAFE FOR ME TO DRIVE THE VEHICLE AS I NEVER KNOW WHEN THE BRAKES WILL NOT RESPOND. WE ARE LOOKING INTO REPLACING THE ABS MODULE AT THIS POINT AS A VERY LAST RESORT, BUT IT IS EXTREMELY EXPENSIVE. *TRRead more
Incident date: Apr 1, 2015
THE CAR DROVE FINE DURING THE DAY WITHOUT ANY PROBLEMS. THE DAY WAS A WARM SUNNY DAY. I PARKED THE CAR AT CHURCH AND WENT INSIDE. 45 MIN. - 1 HOUR AFTER PARKING THE CARE I WAS ASKED TO GO OUTSIDE. WHEN I GOT OUTSIDE I WAS TOLD MY CAR WAS SMOKING WITH THE LIGHTS FLASHING AND WIPERS RUNNING. UPON OPENING THE HOOD I FOUND THE FUSE BOX WAS COMPLETELY MELTED THROUGH WITH THE WIREHARNESS MELTED THROUGH
... WHERE IT PLUGS INTO THE FUSE BOX. THE WIREHARNESS ACROSS THE ENGINE WAS ALSO MELTED ACROSS THE TOP OF THE ENGINE. *TRRead more
Fire
Incident date: May 15, 2014
WHEN I GOT OFF WORK I TRIED TO START MY CAR BUT THE BATTERY WAS DEAD. THE CAR WAS JUMPED OFF. THE CAR OPERATED FINE BUT THE HEADLIGHTS WOULD NOT SHUT OFF TO DAYTIME RUNNING LIGHTS. AFTER DRIVING THE CAR FOR 10 MINUTES, YOU COULD SMELL BURNING ELECTRICAL COMPONENT'S. AFTER INSPECTING THE RELAYS WE FOUND THE HEADLIGHT RELAY WAS ALMOST COMPLETELY MELTED DOWN. THE RELAY WAS CHANGED AND THE CAR SEEMED
... TO BE WORKING OKAY. *TRRead more
Incident date: Mar 16, 2015
AFTER TRAVELING ABOUT 150 MILES FROM MACON, GA, IN THE MORNING OF THE 16TH, THE CAR SHUT DOWN ON I-75 IN HEAVY TRAFFIC GOING 75 MPH IN THE PASSING LANE. WE HAD NO ENGINE POWER, POWER STEERING OR BRAKES, BUT MANAGED TO COAST TO THE SHOULDER. I WAS ABLE TO RESTART THE CAR AFTER A FEW MINUTES ONLY TO HAVE IT STALL OUT AFTER 10 OR 15 MILES. THE ONLY WARNING WAS 2 CHIMES FROM THE CAR BEFORE TOTAL SHUT
... DOWN. WE DID HAVE FLASHER LIGHTS AND WERE ABLE TO RESTART THE CAR EACH TIME. THIS HAPPENED ABOUT 6 OR 8 TIMES. WE STOPPED AT SEVERAL AUTO PARTS PLACES TO SEE IF WE COULD FIND OUT WHAT THE PROBLEM WAS, BUT NO LUCK. WE WERE ABLE TO GET TO A CHEVROLET DEALER IN ASHBURN, GA (PARKER CHEVROLET). THEY WERE NOT ABLE TO DIAGNOSE THE PROBLEM, OR DIDN'T WANT TO DEAL WITH IT. POOR SERVICE! THEY SAID EVERYTHING WAS OKAY! JUST 2 MILES FROM THE DEALERSHIP, IT STALLED AGAIN. WE MANAGED TO GET TO GAINESVILLE, FL WHERE THE CLOSEST CHEVROLET DEALER WAS LOCATED. WE TALKED TO [XXX] FROM GAINESVILLE AUTOMOTIVE CHEVROLET WHO WAS A CALMING VOICE AFTER OUR EXPERIENCE. SHE GAVE US A HOTEL RECOMMENDATION FOR THE NIGHT AND SAID TO BRING THE CAR IN AT 7 AM THE FOLLOWING MORNING. SHE WAS GREAT, AND SO WAS THE ENTIRE STAFF! THEY GOT RIGHT TO WORK ON THE CAR THE NEXT DAY AT 7 AM. AFTER ABOUT AT HOUR, THE SERVICE MANAGER INFORMED US THEY FOUND THE PROBLEM, BUT IT WOULD REQUIRE A NEW COMPUTER AT A COST OF $940 AND COULD BE BACK ON THE ROAD BY NOON. WE WERE BACK ON THE ROAD BY 12:30. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Apr 2, 2015
BOUGHT CAR ON APRIL 1, 2015, WHEN WE DID TEST DRIVE, STEERING MADE WEIRD NOISE AND STEERING WAS REAL HARD TO TURN WHEEL. TOLD DEALERSHIP WOULDN'T BUY CAR UNLESS THEY HAD IT LOOKED AND FIXED. DEALER LOOKED AND SAID THEY HAD TO REPLACE SOMETHING IN THE STEERING SHAFT AND THEY WOULD HAVE TO ORDER PART AND WHEN IT CAME WE BRING CAR IN, BUT CAR WAS OK TO DRIVE UNTIL THEN. GOT A WORK ORDER FROM DEALER
... SHOWING THEY WOULD COVER COST TO FIX THE PROBLEM. THE NEXT MORNING WHILE MY BOYFRIEND WAS DRIVING CAR STEERING GOT REAL HARD TO TURN WHEEL AND HE CRASHED INTO TWO PARKED CARS AND OUR CAR FLIPPED AND AIR BAGS WENT OFF. HE HIT HEAD AND WAS KNOCKED OUT, CHEST PAIN AND BACK AND SHOULDER PAIN FROM THIS. CAR IS A COMPLETE LOSS TO US. *TRRead more
Crash
1 injured
Incident date: Apr 12, 2015
LEAKING ANTIFREEZE OVERHEATING PRESSURE BUILDING UP IN RADIATOR. *TR
Incident date: Apr 12, 2015
LEAKING ANTIFREEZE OVERHEATING PRESSURE BUILDING UP IN RADIATOR. *TR
Incident date: Apr 12, 2015
BATTERY DIED, AND AFTER GETTING A BOOST THE STABILITRACK LIGHT TRACK CAME ON. MY STEERING WHEEL BECAME VERY HARD TO STEER. TURNING WAS ALMOST IMPOSSIBLE. I RAN INTO A CURB WHILE TRYING TO TURN. *TR
Incident date: Apr 12, 2015
BATTERY DIED, AND AFTER GETTING A BOOST THE STABILITRACK LIGHT TRACK CAME ON. MY STEERING WHEEL BECAME VERY HARD TO STEER. TURNING WAS ALMOST IMPOSSIBLE. I RAN INTO A CURB WHILE TRYING TO TURN. *TR
Incident date: Apr 9, 2015
MY IGNITION CYLINDER SWITCH IS MAKING MY CAR TO STALL AND SHUT OFF WHILE I AM DRIVING AND I HAD IT REPLACE ON 4/8/15 AND WAS DRIVING AND IT NOT FIX, MY CAR HAS CUT OFF ON ME WHILE DRIVER 3 TIME SINCE I GOT IT FROM THE DEALERSHIP I AM NOT DRIVING IT AND WHAT THE DEALERSHIP TO SEND A TOW TO PICK THE CAR UP. I AM NOT SAFE IN THE CAR AND SPENT $377.00 FOR LABOR AND THE PART FOR IT NOT TO FUNCTION CORR
... ECTLY. I HAD MY KEY REPLACED ON A RECALL AND WHEN I GOT THAT SERVICE MY IGNITION LOCKED AND THE KEY WOULD NOT TURN THE CAR ON. *TRRead more
Incident date: Nov 1, 2013
WE PURCHASED THIS VEHICLE IN 2010 USED WITH APPROXIMATELY 45,000 MILES ON IT. AFTER ABOUT 4-5 MONTHS, WE RECEIVED THE FIRST "SERVICE TRACTION CONTROL" AND "STABILITRAK OFF" CAME UP IN THE INFORMATION CENTER. I CONTINUED TO DRIVE IT, WHICH THE MANUAL SAYS YOU CAN DO, AND AFTER AWHILE IT WENT OFF. THE "SERVICE ENGINE" LIGHT HOWEVER HAS STAYED ON EVER SINCE. ROLL FORWARD TO NOVEMBER, 2014. I WAS
... DRIVING FINE AT ABOUT 60 MILES AN HOUR, WHEN ALL OF SUDDEN THE VEHICLE KICKS MY CRUISE CONTROL OFF AND SLOWS ME DOWN TO ABOUT 20MPH IN JUST A FEW SECONDS! I WAS UNABLE TO GO ANY FASTER AND VEHICLE RAN VERY SLUGGISH AND JUMPING, ETC. FINALLY, AFTER DRIVING AT ABOUT 10 MPH FOR 15 MILES, I MADE IT HOME AND PARKED THE VEHICLE. HAD THE VEHICLE TOWED IN AND THERE WERE LOTS OF CODES ON THE SYSTEM AND THE MAIN THING WAS THAT THE ALTERNATOR WAS SHOT. THEY ALSO REPLACED FUEL SENSOR. AFTER $450, THE VEHICLE SEEMED OKAY. UNFORTUNATELY A WEEK AGO, THE STABILITRAK AND SERVICE TRACTION CONTROL LIGHT CAME ON AGAIN AND THE VEHICLE HAS BEEN HAVING GLITCHES IN POWER EVER SINCE, BUT STILL NOTHING WHERE I CAN'T DRIVE IT. HOWEVER, COMING OUT OF MY DRIVEWAY A COUPLE OF DAYS AGO, AND SPEEDING UP TO 55, THE "REDUCED ENGINE POWER" LIGHT CAME ON AND I LOST POWER IMMEDIATELY WITH BASICALLY NO WARNING. I COULDN'T GO ANY FASTER THAN 5-10MPH. AFTER GETTING BACK HOME AND LETTING IT SIT ALL DAY AND STARTING IT AGAIN, NO LIGHTS ARE ON EXCEPT "CHECK ENGINE" WHICH WILL ALWAYS STAY ON, AND IT IS RUNNING FINE AGAIN. THIS IS DEFINITELY A SAFETY HAZARD, SINCE THIS COULD HAPPEN IN HEAVY TRAFFIC AND CAUSE AN ACCIDENT! I HATE TO TAKE IT BACK IN FOR REPAIR SINCE IT SEEMS LIKE THEY JUST FIX WHATEVER THEY WANT, BUT THAT IT WOULD PROBABLY RUN FINE ANYWAY, UNTIL THE NEXT TIME THIS HAPPENS OUT OF THE BLUE! NOT GOOD, NOT GOOD AT ALL. WHAT IS IT GOING TO TAKE FOR THIS TO BE LOOKED INTO MORE? *TRRead more
Incident date: Nov 1, 2013
WE PURCHASED THIS VEHICLE IN 2010 USED WITH APPROXIMATELY 45,000 MILES ON IT. AFTER ABOUT 4-5 MONTHS, WE RECEIVED THE FIRST "SERVICE TRACTION CONTROL" AND "STABILITRAK OFF" CAME UP IN THE INFORMATION CENTER. I CONTINUED TO DRIVE IT, WHICH THE MANUAL SAYS YOU CAN DO, AND AFTER AWHILE IT WENT OFF. THE "SERVICE ENGINE" LIGHT HOWEVER HAS STAYED ON EVER SINCE. ROLL FORWARD TO NOVEMBER, 2014. I WAS
... DRIVING FINE AT ABOUT 60 MILES AN HOUR, WHEN ALL OF SUDDEN THE VEHICLE KICKS MY CRUISE CONTROL OFF AND SLOWS ME DOWN TO ABOUT 20MPH IN JUST A FEW SECONDS! I WAS UNABLE TO GO ANY FASTER AND VEHICLE RAN VERY SLUGGISH AND JUMPING, ETC. FINALLY, AFTER DRIVING AT ABOUT 10 MPH FOR 15 MILES, I MADE IT HOME AND PARKED THE VEHICLE. HAD THE VEHICLE TOWED IN AND THERE WERE LOTS OF CODES ON THE SYSTEM AND THE MAIN THING WAS THAT THE ALTERNATOR WAS SHOT. THEY ALSO REPLACED FUEL SENSOR. AFTER $450, THE VEHICLE SEEMED OKAY. UNFORTUNATELY A WEEK AGO, THE STABILITRAK AND SERVICE TRACTION CONTROL LIGHT CAME ON AGAIN AND THE VEHICLE HAS BEEN HAVING GLITCHES IN POWER EVER SINCE, BUT STILL NOTHING WHERE I CAN'T DRIVE IT. HOWEVER, COMING OUT OF MY DRIVEWAY A COUPLE OF DAYS AGO, AND SPEEDING UP TO 55, THE "REDUCED ENGINE POWER" LIGHT CAME ON AND I LOST POWER IMMEDIATELY WITH BASICALLY NO WARNING. I COULDN'T GO ANY FASTER THAN 5-10MPH. AFTER GETTING BACK HOME AND LETTING IT SIT ALL DAY AND STARTING IT AGAIN, NO LIGHTS ARE ON EXCEPT "CHECK ENGINE" WHICH WILL ALWAYS STAY ON, AND IT IS RUNNING FINE AGAIN. THIS IS DEFINITELY A SAFETY HAZARD, SINCE THIS COULD HAPPEN IN HEAVY TRAFFIC AND CAUSE AN ACCIDENT! I HATE TO TAKE IT BACK IN FOR REPAIR SINCE IT SEEMS LIKE THEY JUST FIX WHATEVER THEY WANT, BUT THAT IT WOULD PROBABLY RUN FINE ANYWAY, UNTIL THE NEXT TIME THIS HAPPENS OUT OF THE BLUE! NOT GOOD, NOT GOOD AT ALL. WHAT IS IT GOING TO TAKE FOR THIS TO BE LOOKED INTO MORE? *TRRead more
Incident date: Apr 9, 2015
TL* THE CONTACT OWNS A 2007 PONTIAC G6. WHILE DRIVING AT AN UNKNOWN SPEED, THE POWER STEERING FAILED AND NO WARNING LAMP ILLUMINATED. THE VEHICLE WAS MERGED TO THE SIDE OF THE ROAD SINCE THE CONTACT WAS UNABLE TO TURN THE THE TORQUE SENSOR ASSEMBLY FAILED AND NEEDED TO BE REPLACED. THE DEALER INFORMED THE CONTACT OF NHTSA CAMPAIGN NUMBER: 15V064000 (STEERING); HOWEVER, THE VIN WAS NOT INCLUDED IN
... THE RECALL. THE FAILURE MILEAGE WAS 177,525.Read more
Incident date: Apr 9, 2015
TL* THE CONTACT OWNS A 2007 PONTIAC G6. THE CONTACT STATED THAT THE STEERING FAILED AND THE VEHICLE BECAME VERY DIFFICULT TO TURN. THE VEHICLE WAS TAKEN TO THE DEALER. THE TECHNICIAN DIAGNOSED THAT THE ELECTRONIC POWER STEERING UNIT NEEDED TO BE REPLACED. THE DEALER INFORMED THE CONTACT OF NHTSA CAMPAIGN NUMBER: 15V064000 (STEERING) BUT THE VEHICLE WAS NOT INCLUDED IN THE RECALL. THE VEHICLE WAS N
... OT REPAIRED. THE FAILURE MILEAGE WAS UNKNOWN.... UPDATED 06-02-15 *BF ...UPDATED 06/09/15 *BF UPDATED 10/05/2017*CNRead more
Incident date: Apr 3, 2015
ELECTRICAL POWER STEERING GOING OUT ON 2007 G6. GM SAYS THERE IS NO RECALL FOR HIS VIN BUT IT IS LISTED ON YOUR WEBSITE. THEY ARE REFUSING TO FIX IT. *TR
Incident date: Dec 23, 2014
STEERING MAKES A VIBRATING NOISE, INSTRUMENTS GAUGE SAYS POWERING STEERING, THE STEERING WHEEL GOES LEFT TO RIGHT AND RIGHT TO LEFT BY ITSELF WHILE DRIVING. THE DRIVER HAS LITTLE CONTROL WHILE THIS IS HAPPENING. RECALL FOR STEERING FOR THESE CARS ANNOUNCED 2/4/15 BUT MY VIN NO WAS NOT INCLUDED BUT I AM EXPERIENCING THESE SAME ISSUES. PLEASE ADVISE HOW I CAN BE INCLUDED IN THE RECALL. MY CAR'S ST
... EERING IS DEFECTIVE. PLEASE BE RESPONSIBLE FOR REDUCING DEATHS AND INJURIES DUE TO MOTOR VEHICLE CRASHES. MY LIFE AND MY FAMILY'S LIFE MATTERS. *TRRead more
Incident date: Mar 3, 2014
VEHICLE HAS AN EXTREMELY STRONG FUEL SMELL AROUND THE VEHICLE AT ALL TIMES. THIS SMELL STARTED ABOUT A YEAR AGO AND HAS GOTTEN PROGRESSIVELY WORSE. THE VEHICLE CAN'T EVEN BE PARKED IN THE GARAGE FOR FEAR OF THE GAS WATER HEATER NEARBY CAUSING THE FUMES TO IGNITE. THE GAS SMELL ESPECIALLY FILLS THE TRUNK COMPARTMENT AND EVEN SOMETIMES SMELLS INSIDE THE VEHICLE ITSELF CAUSING US TO ROLL THE WINDO
... WS DOWN. I HAVE BEEN RESEARCHING THIS FOR SEVERAL MONTHS AND FOUND MANY 2007/2008 G6 OWNERS HAVE THE SAME ISSUE WHICH IS A CRACKED PLASTIC SUPPLY OR RETURN PORT ON THE FUEL PUMP MODULE. THERE IS A RECALL FOR THE G5 FUEL PUMP ISSUES OF THE SAME YEARS...I EVEN LIVE IN ONE OF THE STATES MENTIONED IN THE G5 RECALL WHERE THIS ISSUE IS SEEN. THE G5 RECALL EVEN STATES "CONSEQUENCE:FUEL LEAKAGE IN THE PRESENCE OF AN IGNITION SOURCE MAY RESULT IN A FIRE". *TRRead more
Incident date: Apr 1, 2015
PASSENGER OCCUPANT SENSOR, MALFUNCTION, I HAVE NO AIR BAGS ENABLED OR SEATBELT LOCKS DUE TO THIS FAILING IT'S 800 FOR THE WHOLE PART, PLUS LABOR OF 400. I HAVE EXTENDED WARRANT WHICH DON'T COVER THIS ISSUE. STATES SERVICE AIRBAG. WITHOUT THIS PROPERLY FIXED, THE CAR HAS NO SAFETY EQUIPMENT, AS IN AIRBAGS OR YOUR SEATBELTS LOCKING IN CASE OF A ACCIDENT. *TR
Incident date: Apr 1, 2015
PASSENGER OCCUPANT SENSOR, MALFUNCTION, I HAVE NO AIR BAGS ENABLED OR SEATBELT LOCKS DUE TO THIS FAILING IT'S 800 FOR THE WHOLE PART, PLUS LABOR OF 400. I HAVE EXTENDED WARRANT WHICH DON'T COVER THIS ISSUE. STATES SERVICE AIRBAG. WITHOUT THIS PROPERLY FIXED, THE CAR HAS NO SAFETY EQUIPMENT, AS IN AIRBAGS OR YOUR SEATBELTS LOCKING IN CASE OF A ACCIDENT. *TR
Incident date: Mar 1, 2015
RECEIVED RECALL NOTICE FOR GM#14350 ON MARCH 1, 2015. PLACED CALL TO THE SERVICE DEPARTMENT AT FOLSOM GMC TO SCHEDULE AN APPT. NO LIVE PERSON ANSWERED. WAS FORCED TO LEAVE MY INFORMATION ON VOICE MAIL. NO RETURNED CALL RECEIVED. MADE SECOND ATTEMPT WITH ANOTHER MESSAGE. NO RESULT. WROTE LETTER TO OWNER OF DEALERSHIP WITH AN EXPLANATION OF EXPERIENCE. NO RESPONSE OR CALL FROM HIM. CONTACTED PONTIAC
... NATIONAL CUSTOMER ASSISTANCE CENTER. FILED A COMPLAINT, CASE #[XXX] ON APRIL 1, 2015. THEY SAID THEY WOULD CONTACT THE AFOREMENTIONED DEALERSHIP ON MY BEHALF TO GET SERVICE. HAVE NOT RECEIVED CONTACT FROM DEALERSHIP OR PONTIAC CAC. CONTACTED NHTSA RECALL PARTS INVESTIGATION CENTER TO FILE ANOTHER COMPLAINT AND RECEIVE ASSISTANCE. WAS TOLD THAT THIS ONLINE CASE REGISTRATION WOULD PROVIDE AN ID NUMBER FOR FUTURE RECORD AND DOCUMENTATION. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Mar 2, 2012
LOST POWER STEERING WHEN ENTERING A ROUND-A-BOUT. PULLED OVER AND SHUT DOWN THE ENGINE. POWER STEERING WORKED AFTER RESTART. IN THE FOLLOWING WEEKS POWER STEERING WAS LOST SEVERAL TIMES. GM DEALER REPLACED THE TORQUE SENSOR ASSEMBLY AT A COST OF $551. INFORMED ME THAT THE DATE OF VEHICLE MANUFACTURE IS NOT PART OF THE CURRENT RECALL. *TR
Incident date: Apr 7, 2015
TL*THE CONTACT OWNS A 2007 PONTIAC G6. THE CONTACT STATED THAT THE POWER STEERING FAILED WITHOUT WARNING. THE VEHICLE WAS TAKEN TO THE DEALER AND IT WAS DETERMINED THAT THE TORQUE SENSOR ASSEMBLY NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V064000 (STEERING). THE FAILURE
... MILEAGE WAS UNKNOWN. ..UPDATED 05/20/15 *BF UPDATED 7/6/2015 *JSRead more
Incident date: Apr 8, 2014
TL*THE CONTACT OWNS A 2007 PONTIAC G6. THE CONTACT STATED THAT WHILE DRIVING AT 15 MPH, THE STEERING WHEEL SEIZED AND VIBRATED AS AN ABNORMAL NOISE EMITTED FROM THE STEERING WHEEL WITHOUT WARNING. THE FAILURE RECURRED NUMEROUS TIMES. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC, WHERE IT WAS DIAGNOSED THAT THE FRONT TIRES NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED BUT THE FAILURE RECURRED
... . THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND STATED THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V064000 (STEERING). THE FAILURE MILEAGE WAS APPROXIMATELY 70,000.Read more
Incident date: Mar 28, 2015
I STARTED THE CAR AND THERE WAS A MESSAGE ON RADIO DISPLAY THAT SAID POWER STEERING. WHEN I TRIED TO TURN THE WHEEL IT WAS VERY DIFFICULT TO TURN. I TOOK MY CAR TO THE CHEVY DEALERSHIP AND THEY SAID THERE WAS A RECALL BUT MY VEHICLE WAS NOT A PART OF THE RECALL. PLEASE ADD MY VEHICLE TO THE RECALL. *TR
Incident date: Mar 1, 2015
THE STEERING MAKES A CLUNKIN NOISE. IT TURNS BACK AND FOURTH BY ITSELF WHEN DRIVING AND WHILE PARKED.SOME TIMES WHEN I START THE CAR THE RADIO SAYS POWER STEERING WHEN I START THE CAR.WHEN THESE PROBLEMS HAPPEN I TURN THE CAR OFF OPEN DOOR SO THE RADIO GOES OFF THAN START IT AND THAN IT WORKS FINE UNTIL IT SITS TURNED OFF FOR A LITTLE WHILE.SOMETIMES I'LL HAVE TO TURN CAR OFF AND ON ABOUT FIVE TIM
... ES BEFORE IT WORKS.I HAVE READ THAT PONTIAC G6 S FROM 2006 THROUGH 2007 HAVE A STEERING RECALL FOR THE STEERING TORQUE SENSOR BUT I GAVE GM MY VIN AND THEY SAID MY CAR DOESN'T HAVE THAT RECALL.SO I TOOK MY CAR TO THE DEALERSHIP TO HAVE THE OTHER RECALLS TAKEN CARE OF AND TO CHECK MY STEERING AND THEY SAID IT IS THE TORQUE SENSOR.WHY IS IT THE SAME SENSOR AS THE OTHER G6S WITH THE SAME PROBLEMS THEY HAVE RECALLS AND MINE IS NOT UNDER RECALL.IT COST ME 600$.I MUST PAY BECAUSE IT'S VERY DANGEROUS TO DRIVE. *TRRead more
Incident date: Apr 1, 2015
TL*THE CONTACT OWNS A 2009 PONTIAC G6. THE CONTACT STATED THAT AFTER THE VEHICLE WAS STARTED, THE STEERING WHEEL SEIZED WITHOUT WARNING. THE VEHICLE WAS TAKEN TO A DEALER WHERE IT WAS DIAGNOSED THAT THE TORQUE SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND STATED THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 14V153000 (STEERI
... NG). THE FAILURE MILEAGE WAS 90,000.Read more
Incident date: Mar 16, 2015
VEHICLE PURCHASED NEW FROM QUEBEDEAUX BUICK IN TUCSON ARIZONA. SERVICED FOR DEFECTIVE PARTS TWICE: VISOR ACCESSORY, STRUTS ALL MAINTENANCE UP TO DATE, OIL, FILTERS, BREAKS, ETC. A COUPLE OF WEEKS AGO THE CAR WAS EMITTING GAS VAPOR SMELLS. WITHIN THE WEEK IT BECAME PROGRESSIVELY WORSE. TOOK VEHICLE TO CERTIFIED MECHANIC FOR CHECK UP. AFTER DIAGNOSTICS, SEVERAL OTHER EXHAUST TESTING, HE PULLED
... THE GAS TANK TO SEE WHERE THE LEAK WAS COMING FROM. THE FUEL MODULE WAS CRACKED. REPLACEMENT GM PART WAS ORDERED AND INSTALLED. ($673.16) PART ONLY. UPON INSPECTING THE ORIGINAL PART, I INQUIRED ON THE PART NUMBER ETCHED ON THE OEM PART. GM P/N 15804318 THIS PART NUMBER CAN?T BE FOUND ON THE GM PARTS LISTS. IT WILL NOT CROSS REFERENCE TO ANY CASTING PART NUMBER EITHER.A SECOND PART NUMBER WAS ETCHED BELOW THE GM PART NUMBER: F00HK00203 (BOSCH MFG) RESEARCHING THE PART IT IS CHINESE AND THERE IS NO DIRECT REFERENCE TO THE REQUIRED GM PARTS LIST OR SUITABLE SUBSTITUTE. COULD NOT FIND DIRECT REFERENCE ON THE NIPARTS.COM WEBSITE. THE ONLY PLACE I COULD CROSS REFERENCE THE BOSCH PART NUMBER WAS NIPARTS.COM IS THIS A SUBSTANDARD DEFECTIVE PART? THE EXACT ISSUES ON FUEL MODULE RECALLS AFFECTED THE PONTIAC TORRENT 2007 ? 2009. I BELIEVE THAT THE SAME ISSUE AFFECTS THE 2006 PONTIAC TORRENT. IT APPEARS TO BE A SERIOUS SAFETY HAZARD. EASILY CONFUSED WITH REPLACING THE GAS TANK CAP INSTEAD OF LOOKING INTO THE POSSIBILITY THAT IT IS A MORE SERIOUS ISSUE.I THINK FURTHER INVESTIGATION SHOULD BE MADE. *TRRead more
Incident date: Jan 18, 2013
2001 PONTIAC GRAND AM. CONSUMER WRITES IN REGARDS TO IGNITION SWITCH RECALL ISSUES. *SMD THE CONSUMER STATED ON TWO OCCASIONS, THE KEY FELL OUT OF THE IGNITION SWITCH, WHILE BACKING OUT OF THE DRIVEWAY. AFTER HITTING A POLE, THE CONSUMER WENT TO ANOTHER DEALER, WHERE IT WAS DETERMINED THE IGNITION SWITCH WAS DEFECTIVE. THE PREVIOUS DEALER STATED THE KEY WAS WORN OUT. *JB