Showing 18,739 complaints for LINCOLN
Incident date: Jul 21, 2019
WHILE TRAVELING ON INTERSTATE 90 A APPROX 60 MPH. THE VEHICLE STARTED SLOWING DOWN. I LOOKED AT THE SPEEDOMETER AND IT READ 0. SECONDS LATER THE DASH POWER FLASHED AND WENT COMPLETELY DARK. I'M HAD ABSOLUTELY NO POWER AT 60MPH ON AN INTERSTATE. FORTUNATELY, I WAS ABLE TO CRUISE ALONG AT MAKE IT TO THE NEXT EXIT AND STOP ON THE SIDE OF THE ROAD. ONCE STOPPED, I TOOK GEAR OUT OF DRIVE AND PU
... T IT IN PARK. I PUSH THE START BUTTON AND IT STARTED UP. FORTUNATELY, I WAS ABLE TO MAKE IT HOME BUT I WAS COMPLETELY TERRIFIED THAT IT WOULD HAPPEN AGAIN. SOON AS I MADE IT HOME, I BEGAN RESEARCHING LINCOLN MKX TO SEE IF THIS HAS HAPPENED TO ANYONE ELSE. TO MY HORROR, MANY LINCOLN MKX OWNERS HAVE REPORTED THE SAME PROBLEM. THERE IS NO RECALLS LISTED ON MY VIN. THIS VEHICLE IS A DEATH TRAP AND LINCOLN NEED TO ADDRESS THIS ISSUE IMMEDIATELY. PEOPLE HAVE DIED FROM THIS CRITICAL MALFUNCTION AND IF NOT SOMEONE'S DEATH WILL BE CAUSED. THIS VEHICLE IS A DEATH TRAP.Read more
Incident date: Jul 21, 2019
WHILE TRAVELING ON INTERSTATE 90 A APPROX 60 MPH. THE VEHICLE STARTED SLOWING DOWN. I LOOKED AT THE SPEEDOMETER AND IT READ 0. SECONDS LATER THE DASH POWER FLASHED AND WENT COMPLETELY DARK. I'M HAD ABSOLUTELY NO POWER AT 60MPH ON AN INTERSTATE. FORTUNATELY, I WAS ABLE TO CRUISE ALONG AT MAKE IT TO THE NEXT EXIT AND STOP ON THE SIDE OF THE ROAD. ONCE STOPPED, I TOOK GEAR OUT OF DRIVE AND PU
... T IT IN PARK. I PUSH THE START BUTTON AND IT STARTED UP. FORTUNATELY, I WAS ABLE TO MAKE IT HOME BUT I WAS COMPLETELY TERRIFIED THAT IT WOULD HAPPEN AGAIN. SOON AS I MADE IT HOME, I BEGAN RESEARCHING LINCOLN MKX TO SEE IF THIS HAS HAPPENED TO ANYONE ELSE. TO MY HORROR, MANY LINCOLN MKX OWNERS HAVE REPORTED THE SAME PROBLEM. THERE IS NO RECALLS LISTED ON MY VIN. THIS VEHICLE IS A DEATH TRAP AND LINCOLN NEED TO ADDRESS THIS ISSUE IMMEDIATELY. PEOPLE HAVE DIED FROM THIS CRITICAL MALFUNCTION AND IF NOT SOMEONE'S DEATH WILL BE CAUSED. THIS VEHICLE IS A DEATH TRAP.Read more
Incident date: Jul 21, 2019
WHILE TRAVELING ON INTERSTATE 90 A APPROX 60 MPH. THE VEHICLE STARTED SLOWING DOWN. I LOOKED AT THE SPEEDOMETER AND IT READ 0. SECONDS LATER THE DASH POWER FLASHED AND WENT COMPLETELY DARK. I'M HAD ABSOLUTELY NO POWER AT 60MPH ON AN INTERSTATE. FORTUNATELY, I WAS ABLE TO CRUISE ALONG AT MAKE IT TO THE NEXT EXIT AND STOP ON THE SIDE OF THE ROAD. ONCE STOPPED, I TOOK GEAR OUT OF DRIVE AND PU
... T IT IN PARK. I PUSH THE START BUTTON AND IT STARTED UP. FORTUNATELY, I WAS ABLE TO MAKE IT HOME BUT I WAS COMPLETELY TERRIFIED THAT IT WOULD HAPPEN AGAIN. SOON AS I MADE IT HOME, I BEGAN RESEARCHING LINCOLN MKX TO SEE IF THIS HAS HAPPENED TO ANYONE ELSE. TO MY HORROR, MANY LINCOLN MKX OWNERS HAVE REPORTED THE SAME PROBLEM. THERE IS NO RECALLS LISTED ON MY VIN. THIS VEHICLE IS A DEATH TRAP AND LINCOLN NEED TO ADDRESS THIS ISSUE IMMEDIATELY. PEOPLE HAVE DIED FROM THIS CRITICAL MALFUNCTION AND IF NOT SOMEONE'S DEATH WILL BE CAUSED. THIS VEHICLE IS A DEATH TRAP.Read more
Incident date: Jul 18, 2019
STEERING WHEEL MAKES A LOUD NOISE (SQUEALING NOISE) WHILE DRIVING LEFT OR RIGHT VERY DIFFICULT TO MANEUVER STEERING WHEEL.
Incident date: Jul 7, 2019
THE INSTRUMENT CLUSTER FAILED 2 DAYS AFTER PURCHASE. NO INDICATION OF SPEED NOR FUEL LEVEL.
Incident date: Jul 13, 2019
WHILE DRIVING, SOMETIMES THE HORN COMPLETELY STOPS WORKING, AT THE SAME TIME THE HORN STOPS WORKING I CAN REMOVE MY SEATBELT OR HAVE A PASSENGER NOT WEARING A SEAT BELT AND THE SEAT BELT INDICATOR AND CHIME DOES NOT COME ON, I HAVE BUCKLED AND UNBUCKLED THE SEATBELT TO TRY TO GET THE INDICATOR TO COME ON AND NOTHING HAPPENS. I AM WORRIED THAT THE SEAT SENSORS OR SEAT BELT LATCH ARE DEFECTIVE ALS
... O THE HORN ISSUE MAY BE ANOTHER UNDERLYING PROBLEM.Read more
Incident date: Jul 13, 2019
WHILE DRIVING, SOMETIMES THE HORN COMPLETELY STOPS WORKING, AT THE SAME TIME THE HORN STOPS WORKING I CAN REMOVE MY SEATBELT OR HAVE A PASSENGER NOT WEARING A SEAT BELT AND THE SEAT BELT INDICATOR AND CHIME DOES NOT COME ON, I HAVE BUCKLED AND UNBUCKLED THE SEATBELT TO TRY TO GET THE INDICATOR TO COME ON AND NOTHING HAPPENS. I AM WORRIED THAT THE SEAT SENSORS OR SEAT BELT LATCH ARE DEFECTIVE ALS
... O THE HORN ISSUE MAY BE ANOTHER UNDERLYING PROBLEM.Read more
Incident date: Jul 13, 2019
WHILE DRIVING, SOMETIMES THE HORN COMPLETELY STOPS WORKING, AT THE SAME TIME THE HORN STOPS WORKING I CAN REMOVE MY SEATBELT OR HAVE A PASSENGER NOT WEARING A SEAT BELT AND THE SEAT BELT INDICATOR AND CHIME DOES NOT COME ON, I HAVE BUCKLED AND UNBUCKLED THE SEATBELT TO TRY TO GET THE INDICATOR TO COME ON AND NOTHING HAPPENS. I AM WORRIED THAT THE SEAT SENSORS OR SEAT BELT LATCH ARE DEFECTIVE ALS
... O THE HORN ISSUE MAY BE ANOTHER UNDERLYING PROBLEM.Read more
Incident date: Jul 9, 2019
MY BRAKE BOOSTER WENT OUT. I DID FIND THAT THERE WAS A EXTENDED WARRANTY FOR SOME BUT MY VIN NUMBER DID "NOT" QUALIFY. SOUNDS LIKE A LIE TO ME. THIS IS A LIFE THREATENING. I AM NOT THE ONLY ONE WITH THIS PROBLEM AS OTHERS HAVE BEEN GIVEN THE EXTENDED WARRANTY COVERAGE. THE FACT THAT THIS IS WAS DONE ON SOME BUT NOT ALL, DOES NOT MAKE SAFETY SENSE TO ME. MY CAR WAS ASSEMBLED AT THE DESIGNATED SITE
... THAT HAD THE PROBLEM. I AM HAVING MY CAR REPAIRED AT A "NON-FORD" MECHANIC, SINCE THE LAST TIME I WENT TO A FORD DEALER, THE DEALER TRIED "THEFT BY DECEPTION" ON ME.Read more
Incident date: Jul 12, 2019
BRAKE BOOSTER VACUUM LEAKS CAUSING BRAKES TO SQUEAL AND HISS THUS RENDERING VEHICLE UNSAFE STOP.. THE RECALL STARTS ON 2010 MODELS BUT THE RECALL SHOULD HAVE STARTED ON THE 2009S. I HAD TO REPLACE IT AND IT COST 700. NOW MY VEHICLE IS MECHANICALLY SOUND.
Incident date: Jul 12, 2019
TL* THE CONTACT OWNS A 2003 LINCOLN AVIATOR. THE CONTACT STATED THAT THE GEAR FAILED TO SHIFT FROM PARK INTO ANY OTHER GEAR BECAUSE THE GEAR SHIFTER WAS FRACTURED. THE VEHICLE WAS UNABLE TO BE DRIVEN. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 02V313000 (POWER TRAIN); HOWEVER, THE VEHICLE EXHIBITED THE SAME FAILURE AS LISTED IN THE RECALL CAMPAIGN. THE VEHICLE WAS NOT REPAIRED. THE DEA
... LER WAS NOT CONTACTED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS NOT AVAILABLE.Read more
Incident date: Dec 1, 2017
TL* THE CONTACT OWNS A 2014 LINCOLN MKZ. THE CONTACT STATED THAT THE DOOR LATCHES WERE INOPERABLE. THE FAILURE OCCURRED TWICE. THE FIRST FAILURE OCCURRED ON THE REAR DRIVER'S SIDE DOOR. FIESTA LINCOLN (1720 S MESA DR, MESA, AZ 85210, (480) 813-4900) WAS CONTACTED, BUT WOULD NOT REPAIR THE VEHICLE BECAUSE IT WAS NOT UNDER WARRANTY OR INCLUDED IN A RECALL. THE MANUFACTURER WAS NOTIFIED OF THE FAILUR
... E. THE FAILURE MILEAGE WAS 50,000.Read more
Incident date: Jul 10, 2019
WHILE MAKING A TURN ONTO HIGHWAY MY ELECTRIC POWER STEERING COMPLETELY WENT OUT WITH CARS TURNING NEXT TO ME. IT YANKED THE WHEEL OUT OF MY HAND ALMOST CAUSING A CRASH. THEN A WINDOW APPEARS IN LY CAR SAYING YOUR STEERING HAS FAILED PULL OVER SAFELY . LITTLE LATE FOR THAT. AFTER GETTING CAR TO DEALER AND WAITING I SEARCHED AND FOUND ELECTRIC STEERING RECALL FROM 2015 SOME 400K CARS. THE SAME YEAR
... MINE WAS BUILT. DEALER SAYS NO BUT ITS THE SAME EXACT PROBLEM.Read more
Incident date: Jan 1, 2019
SEAT BELT SENSOR DOES NOT COME ON ALL THE TIME WHEN SEAT IS OCCUPIED, HORN DOES NOT WORK ALL THE TIME. I WAS INFORMED THAT THIS COULD BE A MAJOR PROBLEM IF LEFT UNREPAIRED. I CANT SEEM TO GET MY LOCAL LINCOLN DEALERSHIP TO FIX THE PROBLEM WEITHER ITS A MODULE OR SOMETHING ELSE.
Incident date: Jan 1, 2019
SEAT BELT SENSOR DOES NOT COME ON ALL THE TIME WHEN SEAT IS OCCUPIED, HORN DOES NOT WORK ALL THE TIME. I WAS INFORMED THAT THIS COULD BE A MAJOR PROBLEM IF LEFT UNREPAIRED. I CANT SEEM TO GET MY LOCAL LINCOLN DEALERSHIP TO FIX THE PROBLEM WEITHER ITS A MODULE OR SOMETHING ELSE.
Incident date: Jan 1, 2019
SEAT BELT SENSOR DOES NOT COME ON ALL THE TIME WHEN SEAT IS OCCUPIED, HORN DOES NOT WORK ALL THE TIME. I WAS INFORMED THAT THIS COULD BE A MAJOR PROBLEM IF LEFT UNREPAIRED. I CANT SEEM TO GET MY LOCAL LINCOLN DEALERSHIP TO FIX THE PROBLEM WEITHER ITS A MODULE OR SOMETHING ELSE.
Incident date: Jul 12, 2019
I WAS DRIVING ON INTERSTATE 69 IN HOUSTON, TEXAS WHEN I FEEL LT LIKE THE BRAKE PETAL WAS HARD TO PUSH AND ALSO HEARD A SOUND FROM THE DASH. THIS TERRIFIED ME SO I GOT OFF THE FREEWAY AND IMMEDIATELY LOOKED UP BRAKE CHECK LOCATION TO GO GET THE BRAKES CHECKED. I FOUND ONE 8 MILES AWAY AND DROVE THERE AND EXPLAINED TO A TECHNICIAN WHAT HAD HAPPEN. THE TECHNICIAN GOT INTO MY LINCOLN AND STEPPED ON TH
... E BRAKE PEDAL AND SAID IT'S GOING ALL THE WAY DOWN TO THE FLOORBOARD AND HARD TO PUSH. AND HE ASKED ME IF IT FELT HARDER TO PUSH. I TOLD HIM YES. HE CHECKED THE BRAKES OUT AND TOLD ME IT WAS THE BRAKE BOOSTER. HE SAID WITH ONLY 41,700 MILES HE HIMSELF WOULD TAKE IT BACK TO THE DEALERSHIP. WE DON'T LIVE IN HOUSTON, AND WE WERE ON THE WAY HOME FROM HOUSTON AFTER MY HUSBAND HAVING SURGERY AND I NEEDED TO GET HIM HOME. WE HAD NO CHOICE BUT TO DRIVE HOME. I DROVE IN THE MIDDLE LANE AT 55 MPH AND KEEPING A DISTANCE IN FRONT OF ME. WHEN I WOULD USE THE BRAKE I WOULD HAVE TO START BRAKING WAY AHEAD WHEN SOMEONE WOULD CUT I FRONT IF ME BECAUSE THE BRAKES WERE BARELY WORKING. I BABIED THE BRAKES ALL OUR 4 HOUR DRIVE HOME. PLEASE INFORM ME WHAT CAN BE DONE. THIS SHOULD NOT BE HAPPENING TO A VEHICLE WITH ONLY 41,700 MILES. WE BOUGHT IT USED IN 2017 AFTER HURRICANE HARVEY. I'M THINKING THERE WAS A RECALL ON THE BRAKING SYSTEM AND IT WAS NEVER DONE BY THE PRIOR OWNERS AND THEY DECIDED TO SELL IT. THIS SHOULD APPLY TO THE LEMON LAW. BECAUSE WE WERE SOLD A DEFECTIVE VEHICLE. WE COULD HAVE BEEN KILLED DRIVING ON A BUSY INTERSTATE IN HOUSTON TX. TERRIFYING DRIVING HOME. IRead more
Incident date: Jul 12, 2019
I WAS DRIVING ON INTERSTATE 69 IN HOUSTON, TEXAS WHEN I FEEL LT LIKE THE BRAKE PETAL WAS HARD TO PUSH AND ALSO HEARD A SOUND FROM THE DASH. THIS TERRIFIED ME SO I GOT OFF THE FREEWAY AND IMMEDIATELY LOOKED UP BRAKE CHECK LOCATION TO GO GET THE BRAKES CHECKED. I FOUND ONE 8 MILES AWAY AND DROVE THERE AND EXPLAINED TO A TECHNICIAN WHAT HAD HAPPEN. THE TECHNICIAN GOT INTO MY LINCOLN AND STEPPED ON TH
... E BRAKE PEDAL AND SAID IT'S GOING ALL THE WAY DOWN TO THE FLOORBOARD AND HARD TO PUSH. AND HE ASKED ME IF IT FELT HARDER TO PUSH. I TOLD HIM YES. HE CHECKED THE BRAKES OUT AND TOLD ME IT WAS THE BRAKE BOOSTER. HE SAID WITH ONLY 41,700 MILES HE HIMSELF WOULD TAKE IT BACK TO THE DEALERSHIP. WE DON'T LIVE IN HOUSTON, AND WE WERE ON THE WAY HOME FROM HOUSTON AFTER MY HUSBAND HAVING SURGERY AND I NEEDED TO GET HIM HOME. WE HAD NO CHOICE BUT TO DRIVE HOME. I DROVE IN THE MIDDLE LANE AT 55 MPH AND KEEPING A DISTANCE IN FRONT OF ME. WHEN I WOULD USE THE BRAKE I WOULD HAVE TO START BRAKING WAY AHEAD WHEN SOMEONE WOULD CUT I FRONT IF ME BECAUSE THE BRAKES WERE BARELY WORKING. I BABIED THE BRAKES ALL OUR 4 HOUR DRIVE HOME. PLEASE INFORM ME WHAT CAN BE DONE. THIS SHOULD NOT BE HAPPENING TO A VEHICLE WITH ONLY 41,700 MILES. WE BOUGHT IT USED IN 2017 AFTER HURRICANE HARVEY. I'M THINKING THERE WAS A RECALL ON THE BRAKING SYSTEM AND IT WAS NEVER DONE BY THE PRIOR OWNERS AND THEY DECIDED TO SELL IT. THIS SHOULD APPLY TO THE LEMON LAW. BECAUSE WE WERE SOLD A DEFECTIVE VEHICLE. WE COULD HAVE BEEN KILLED DRIVING ON A BUSY INTERSTATE IN HOUSTON TX. TERRIFYING DRIVING HOME. IRead more
Incident date: Apr 1, 2019
TL* THE CONTACT OWNS A 2010 LINCOLN MKT. THE CONTACT STATED THAT THE EPS WARNING INDICATOR FLASHED REGARDING A POWER STEERING ASSIST FAILURE. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V340000 (STEERING); HOWEVER, THE 2011 MODELS WERE INCLUDED. THE CONTACT STATED THAT THE VEHICLE EXHIBITED THE SAME FAILURE AS THE RECALL CAMPAIGN. THE VEHICLE WAS NOT DIAGNOSED BY A DEALER. CANNON FORD
... -LINCOLN OF STARKVILLE (12249 MS-182, STARKVILLE, MS 39759, (662) 323-1900) WAS CONTACTED AND A DIAGNOSTIC APPOINTMENT WAS SCHEDULED FOR JULY 16, 2019. AN INDEPENDENT MECHANIC DIAGNOSED THAT THERE WAS A POWER STEERING ELECTRICAL UNIT FAILURE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 184,000. *BF *TRRead more
Incident date: Jul 11, 2019
DOOR LATCH DEFECTIVE. I HAD A DEFECTIVE LATCH REPLACED BY LINCOLN DEALERSHIP ONE YEAR AGO. THIS WAS THE REAR DRIVERS SIDE DOOR. ON 7/11/19, MY PASSENGER SIDE DOOR LATCH IS NOW DEFECTIVE. I CONTACTED MY LINCOLN DEALERSHIP AND THEY EXPLAINED MY WARRANTY IS NOT VALID, THEREFORE, THEY WILL NOT COVER THE COST. I CONTACTED LINCOLN CUSTOMER SERVICE, RECALL DEPARTMENT AND THEY TOO SAID THEY WOULD NOT COVE
... R THE 2ND DEFECTIVE DOOR LATCH, DUE TO NO WARRANTY. THEY EXPLAINED THEY UNDERSTOOD THIS IS THE 2ND DEFECTIVE DOOR LATCH AND THIS DOOR LATCH ISSUE IS PART OF RECALL. HOWEVER, MY VIN# IS NOT PART OF RECALL, BUT MY MAKE, MODEL AND YEAR ARE INCLUDED IN RECALL.Read more
Incident date: May 1, 2019
CHECK ENGINE LIGHT WENT ON .. TOOK TO TECH .. TIMING ISSUES .. FURTHER EXAMINATION REVELED WATER PUMP LEAKING, TIMING CHAIN STRETCHED ON ONE SIDE .. RESULT REQUIRED WATER PUMP REPLACEMENT, TIMING CHAIN REPLACEMENT, REPLACEMENT OF RIGHT BANK PHASER AND SECONDARY CHAIN AND TENTIONER, REPLACED UPPER CHAIN GUIDES, REPLACED CRANK/SPROCKET. TOTAL COST OF REPAIRS $2775.23 .. MILEAGE 88245 .. DETAILED INV
... OICE FROM REPAIR SHOP IS AVAILABLE.Read more
Incident date: Jun 5, 2019
WE HAD TAKEN OUR LINCOLN FOR WARRANTY WORK ON THE NAVIGATION/STEREO AND IT WAS DETERMINED A PART NEEDED TO BE ORDERED. WE WERE TOLD WE COULD DRIVE THE CAR WHILE WAITING ON THE PART TO ARRIVE BUT WHEN WE WENT TO PICK IT UP OUR CAR WOULD NOT START. THE DEALERSHIP CHARGED THE BATTERY AND RAN IT THROUGH SOME TESTS AND EVERYTHING CHECKED OUT SO WE PICKED IT UP THE NEXT DAY. ONE DAY LATER THE VEHICLE ON
... CE AGAIN WOULD NOT START. DEALERSHIP ONCE AGAIN CHARGED BATTERY AND RAN IT THROUGH TESTS AND ONCE AGAIN EVERYTHING CHECKED OUT. WE DECIDED TO LEAVE THE VEHICLE AT THE DEALERSHIP UNTIL THE PART FOR THE NAVIGATION/STEREO WAS REPLACED AND THEN PICKED IT UP. WE DROVE IT ABOUT A WEEK WITH ABSOLUTELY NO PROBLEMS UNTIL I WAS PULLING OUT OF A PARKING LOT INTO A STREET AND MY CAR LOST ALL POWER INCLUDING STEERING WITHOUT ANY WARNING. I MANAGED TO COAST INTO A SINGLE LANE SO I WASNT BLOCKING THE ENTIRE STREET. MY CAR WOULD NOT RESTART GIVING A MESSAGE ABOUT POWER FAILURE OR POWER OFF ON THE DISPLAY. I TRIED RESTARTING SEVERAL TIMES WHILE SITTING BLOCKING TRAFFIC INCLUDING TAKING THE KEY FOB OUT OF THE CAR COMPLETELY FOR A FEW MINUTES THEN PLACING IT BACK IN THE CAR HOPING SOMETHING WOULD RESET AND STILL HAD NO LUCK. A TOW TRUCK ARRIVED AND TOWED MY LINCOLN INTO THE DEALERSHIP WHERE IT STARTED RIGHT UP SO NO CODE COULD BE FOUND. THE DEALERSHIP HAS NO WAY TO FIX THE ISSUE WITHOUT CODES. I FEEL LUCKY THIS PROBLEM HAS ONLY OCCURED IN RELATIVELY CALM TRAFFIC AND NOT WHILE I WAS ON THE INTERSTATE WHERE THIS ISSUE COULD BE DEADLY.Read more
Incident date: Jul 8, 2019
VEHICLE STALLS/LOSES POWER ONCE FUEL REACHES BELOW HALF TANK OF GAS. FORD HAS ISSUED TSB'S ON THIS VERY ISSUE ON MANY OF THEIR OTHER ENGINES, BUT I'VE BEEN UNABLE TO FIND A TSB FOR THIS ISSUE FOR MY VEHICLE SPECIFICALLY. HERE IS THE TSB FOR FORD FOCUS'S WITH THIS ISSUE: FORD MOTOR COMPANY (FORD) IS RECALLING CERTAIN 2012-2018 FORD FOCUS VEHICLES WITH A 2.0L GDI OR 2.0L GTDI ENGINE. THE CANISTER
... PURGE VALVE (CPV) MAY MALFUNCTION, POSSIBLY CAUSING EXCESSIVE VACUUM IN FUEL VAPOR MANAGEMENT SYSTEM. TSB # 18S32. WHEN PRESSURE IS BEING RELEASED FROM THE GAS TANK VIA THE FUEL DOOR OPENING, GAS SPRAYS OUT OF THE OPENING AND GOERS STUCK/HARDENED TO EXTERIOR OF CAR.Read more
Incident date: Jul 8, 2019
VEHICLE STALLS/LOSES POWER ONCE FUEL REACHES BELOW HALF TANK OF GAS. FORD HAS ISSUED TSB'S ON THIS VERY ISSUE ON MANY OF THEIR OTHER ENGINES, BUT I'VE BEEN UNABLE TO FIND A TSB FOR THIS ISSUE FOR MY VEHICLE SPECIFICALLY. HERE IS THE TSB FOR FORD FOCUS'S WITH THIS ISSUE: FORD MOTOR COMPANY (FORD) IS RECALLING CERTAIN 2012-2018 FORD FOCUS VEHICLES WITH A 2.0L GDI OR 2.0L GTDI ENGINE. THE CANISTER
... PURGE VALVE (CPV) MAY MALFUNCTION, POSSIBLY CAUSING EXCESSIVE VACUUM IN FUEL VAPOR MANAGEMENT SYSTEM. TSB # 18S32. WHEN PRESSURE IS BEING RELEASED FROM THE GAS TANK VIA THE FUEL DOOR OPENING, GAS SPRAYS OUT OF THE OPENING AND GOERS STUCK/HARDENED TO EXTERIOR OF CAR.Read more
Incident date: Jul 10, 2019
STARTED HAPPENING IN 2015, "DOOR AJAR" INDICATOR STAYS ON WHEN DOOR IS CLOSED, CAUSES INDICATOR LIGHT TO FLASH BACK AND FORTH BETWEEN THAT AND "SHIFT TO PARK" NON-STOP WHEN IN MOTION. IT PREVENTS THE CAR FROM BEING LOCKED WHILE STATIONARY AND IN MOTION, DANGEROUS WITH KIDS IN CAR. AT TIMES DOME LIGHTS WILL NOT GO OUT WHEN VEHICLE IS TURNED OFF. THE ALARM GOES AT RANDOM TIMES WHILE PARKED AND OFF,
... LAST NIGHT EVERY 2 HRS STARTING AT 12 AM. HAVE COME OUT OF WORK TO FIND LIGHTS FLASHING FROM ALARM HAVING GONE OFF. AFRAID TO PARK IN GARAGE NOW BECAUSE OF FIRE HAZARD. KEY FOB MUST BE PUSHED TO UNLOCK DRIVERS DOOR BUT NOT PASSENGER SIDE. STARTING IN 4-19 THE NAVIGATION SCREEN WHEN IN REVERSE AND BACKING UP RANDOMLY GOES BLACK.Read more
Incident date: Feb 1, 2019
TL* THE CONTACT OWNS A 2006 LINCOLN TOWN CAR. THE CONTACT STATED THAT THE STEERING COLUMN WAS COMING APART AND THE POWER STEERING MALFUNCTIONED WHILE DRIVING AND PARKING. THE CONTACT STATED THAT A PREVIOUS RECALL REPAIR FOR NHTSA CAMPAIGN NUMBER: 13V385000 (STEERING) WAS PERFORMED INCORRECTLY. THE CONTACT STATED THAT THE VIN WAS EXCLUDED FROM NHTSA CAMPAIGN NUMBER: 14V704000 (STEERING). RILEY FORD
... INC (9693 U.S. 9, CHAZY, NY 12921, (518) 846-7131) WANTED TO CHARGE THE CONTACT $2,600 TO CORRECT THE INITIAL RECALL REPAIR. THE MANUFACTURER ADMITTED THAT THE CONTACT HAD A VALID POINT, BUT THEY WERE NOT AUTHORIZED TO MAKE A DECISION. THE CONTACT WAS REFERRED TO NHTSA. THE FAILURE MILEAGE WAS 186,000.Read more
Incident date: Jun 1, 2019
TAKATA RECALL. MY AIRBAG INDICATOR LIGHT REMAINS ON. BASED ON RESEARCH IT INDICATES THAT MY FRONT AIRBAGS MAY NOT ACTIVATE DURING AN ACCIDENT. THIS LIGHT APPEARED A FEW WEEKS AGO. THIS IS CONCERNING AS I OFTEN TRAVEL WITH SMALL CHILDREN AND MAKES ME WONDER ABOUT THE SAFETY OF EVERYONE IN THE CAR. UNABLE TO SALE CAR DUE TO THIS ISSUE. I DO NOT WANT TO PAY FOR A REPAIR IN WHICH THE MAKERS OF T
... AKATA INFLATORS ARE RESPONSIBLE FOR REPAIRING.Read more
Incident date: Jul 5, 2019
THE INNER DOOR HANDLE ASY DOESN'T OPEN FROM THE INSIDE.
Incident date: Mar 1, 2017
I HAVE A 2015 LINCOLN MKS PURCHASED IN MAY 2016. IT HAS A MALFUNCTIONING FCIM PANEL . WHEREBY THE HEATER WILL TURN ON ALL BY ITSELF AND GOES UP TO ITS HIGHEST TEMPS TIRE AND THEN STOP. IT HAS A TOUCH SCREEN TO TURN DOWN OR OFF TO ALLOW YOU TO RESET THE TEMPS. BUT IS NOW NOT WORKING AND TEMP STUCK ON HEAT AND VEHICLE IS NOW UNDRIVABLE. AND FORD/LINCOLN REFUSES TO ACKNOWLEDGE PROBLEM, LET ALONE FIX
... IT DESPITE NUMEROUS COMPLAINTS. THIS PROBLEM HAS BEEN ONGOING FOR 1 1/2 YEARS.Read more
Incident date: Jul 4, 2019
HTTPS://YOUTU.BE/CU8J1MSZ8OE CAM PHASER WITH DOCUMENTATION
Crash
Fire
38 injured
40 deaths
Incident date: Jul 27, 2017
DURING HARD ACCELERATION, THE SMELL OF ROTTEN EGGS ENTERS THE CABIN REGARDLESS OF WHAT TYPE OF FAN IS BLOWING (AIR CONDITIONING - FRESH AIR OR RECIRCULATE). LINCOLN UNDER A TSB CLAIMED THAT THEY FIXED THE PROBLEM BY RESEALING THE REAR SEALS TO THE REAR HATCH. THE SMELL CONTINUES AND IF YOU DO RESEARCH, THIS IS A WIDESPREAD PROBLEM IN FORD EDGE'S, EXPLORER'S AND LINCOLN MKX'S. FORD DOESN'T SEEM TO
... THINK THAT EXHAUST ENTERING THE CABIN FOR WHICH THEY DO NOT HAVE FIX FOR IS WORTHY OF A SYSTEM WIDE RECALL. I SUSPECT THAT CARBON MONOXIDE AND OTHER POISONOUS GASES ARE ENTERING THE CABIN AND CANNOT BE GOOD FOR THE OCCUPANTS... THIS ISSUE WAS PRESENT FROM THE FIRST DAY I LEASED THE VEHICLE.Read more
Incident date: Jul 3, 2019
I AM HAVING A REALLY HARD TIME GETTING THIS AIR BAG REPLACED WITH A LOCAL DEALERSHIP THE ONLY DEALERSHIP IN RADIUS. MTN VIEW LINCOLN FORD CHATTANOOGA, TN. THIS IS THE ONLY VEHICLE I DRIVE AND I ADVISED THEM I WOULD NEED A LOANER WHILE THIS REPAIR IS BEING DONE. THE FIRST TIME I CALLED WITH A CS REPRESENTATIVE ON THE PHONE THEY ADVISED ME THEY DIDN'T HAVE A PART BUT COULD ORDER IT. I ASKED ABOUT A
... LOANER THE REP TOLD ME ONLY THE SERVICE MANAGER CAN APPROVE THAT AND I WAS SENT TO HIS DESK WHERE I LEFT A MESSAGE. I DIDN'T RECEIVE A CALL BACK. (THERE IS A GOOGLE REVIEW REGARDING MY EXPERIENCE). AFTER RECEIVING YET ANOTHER RECALL NOTICE LAST WEEK I DREADFULLY ATTEMPTED TO SCHEDULE AN APPOINTMENT TO GET THIS FIXED. WHICH WAS TODAY AT 7:45, LAST WEEK I EXPRESSED AGAIN THE NEED FOR A LOANER THE GUY WHO ANSWERED THE PHONE ADVISED ME THEY HAD 40 LOANERS OUT BUT HE CAN SEE WHAT HE CAN DO. TODAY I ARRIVED WAITED 20 MINS AND TODD COMES TO MY VEHICLE I ADVISED THEM WHAT I WAS THERE FOR AND HE STATED THERE ARE NO LOANERS BUT HE WILL GIVE ME A CALL AND UPDATE ME. NO ONE HAS CALLED ME.Read more
Incident date: Jun 7, 2019
THE CAR ACCELERATED WHILE GOING UP A RAMP THAT WENT TO AN AXIS ROAD TO THE INTERSTATE. WE HIT A RETAINING WALL HEAD ON, SPUN AROUND AND THEN THE BACK OF THE CAR ALSO HIT THE WALL. MY SEAT BELT DID NOT HOLD ME BACK. I ENDED WEDGED BETWEEN THE CONSOLE AND DASHBOARD. I HAVE A BROKEN RIB AND CHIPPED TOOTH AND BUMPS AND BRUISES. MY WIFE WAS A PASSENGER AND HER SEAT BELT HELD HER. THE AIR BAGS
... DID NOT DEPLOY. OUR CAR WAS TOTALEDRead more
Crash
1 injured
Incident date: Jun 7, 2019
THE CAR ACCELERATED WHILE GOING UP A RAMP THAT WENT TO AN AXIS ROAD TO THE INTERSTATE. WE HIT A RETAINING WALL HEAD ON, SPUN AROUND AND THEN THE BACK OF THE CAR ALSO HIT THE WALL. MY SEAT BELT DID NOT HOLD ME BACK. I ENDED WEDGED BETWEEN THE CONSOLE AND DASHBOARD. I HAVE A BROKEN RIB AND CHIPPED TOOTH AND BUMPS AND BRUISES. MY WIFE WAS A PASSENGER AND HER SEAT BELT HELD HER. THE AIR BAGS
... DID NOT DEPLOY. OUR CAR WAS TOTALEDRead more
Crash
1 injured
Incident date: Jun 7, 2019
THE CAR ACCELERATED WHILE GOING UP A RAMP THAT WENT TO AN AXIS ROAD TO THE INTERSTATE. WE HIT A RETAINING WALL HEAD ON, SPUN AROUND AND THEN THE BACK OF THE CAR ALSO HIT THE WALL. MY SEAT BELT DID NOT HOLD ME BACK. I ENDED WEDGED BETWEEN THE CONSOLE AND DASHBOARD. I HAVE A BROKEN RIB AND CHIPPED TOOTH AND BUMPS AND BRUISES. MY WIFE WAS A PASSENGER AND HER SEAT BELT HELD HER. THE AIR BAGS
... DID NOT DEPLOY. OUR CAR WAS TOTALEDRead more
Crash
1 injured
Incident date: Apr 20, 2018
WAS DRIVING HEARD ODD NOISES AND BURNT FLUID TRANSFER CASE WAS DEFECTIVE BOTH OF MY FORD AWD DID ECACT SAME THING.
Incident date: Jun 24, 2019
RIGHT REAR WHEEL BEARING WENT OUT. MILEAGE OF CAR IS 92,643. THERE WAS A RECALL OF THIS YEAR OF CAR MANUFACTURED FROM THE SAME PLANT, WIXOM, MI, BUT THE PRODUCTION LINE OF RECALL ENDED IN DECEMBER 2002. THIS CAR ROLLED OFF IN FEBRUARY2003. HOWEVER, IT WAS EXACTLY AS THE RECALL STATED AND THERE IS NO WAY THAT THE BAD PARTS WAS NOT PUT ON OTHER VEHICLES OF THE 2003 PRODUCTION VEHICLES. WHEN THE BEAR
... ING WENT, IT CHEWED THE AXLE SO IT TOO HAD TO BE REPLACED. IT WENT OUT WHILE ACCELERATING FROM A STOPPED POSITION. WAS IMMEDIATELY PARKED AND NOT DRIVEN TIL FIXED. MACHANIC AGREES THAT IT WAS BAD PARTS AND KNOWS OF SEVERAL 2003 MODELS WITH THE SAME PROBLEM.Read more
Incident date: Apr 15, 2019
STARTED VEHICLE IN PARKING LOT. BRAKE LIGHT, ABS, TRACTION CONTROL LIGHTS ALL ON. BACKED OUT OF PARKING SPOT. THOUGHT I COULD GET IT HOME. PULLED OUT ONTO CITY STREET. TOTAL BRAKE FAILURE; PEDAL WENT ALL THE WAY DOWN. DID NOT REMEMBER TO USE EMERGENCY BRAKE TO STOP, BUT PUT INTO PARK TO GET VEHICLE TO STOP. MANAGED TO PULL INTO ANOTHER PARKING LOT, CONTINUING TO PUT INTO PARK TO STOP. CALLE
... D AAA AND HAD TOWED. DEALER INVOICE STATES, "VERIFIED CUST CONCERN. EXPERIENCED NO POWER BRAKE ASSIST ON VEHICLE. R&I THE ABS CONTROL MODULE FOR INTERNAL FAULT...."Read more
Incident date: Jun 14, 2019
THE RADIO BLEW OUT, AFTER LINCOLN INSTALLED THE AN AIRBAG THAT WAS RECALLED. IT'S SOUNDED LIKE A BODY DROP ON THE VEHICLE ALSO THE AIRBAG LIGHT CAME BACK ON.
Incident date: Jun 14, 2019
THE RADIO BLEW OUT, AFTER LINCOLN INSTALLED THE AN AIRBAG THAT WAS RECALLED. IT'S SOUNDED LIKE A BODY DROP ON THE VEHICLE ALSO THE AIRBAG LIGHT CAME BACK ON.
Incident date: Jun 14, 2019
THE RADIO BLEW OUT, AFTER LINCOLN INSTALLED THE AN AIRBAG THAT WAS RECALLED. IT'S SOUNDED LIKE A BODY DROP ON THE VEHICLE ALSO THE AIRBAG LIGHT CAME BACK ON.
Incident date: Jun 20, 2019
THERE IS A LEAK COMING FROM THE WATER PUMP WHICH IS IN THE ENGINE. IT'S ON AVERAGE A $1700 FIX WHICH IS EXTREMELY EXPENSIVE. FROM WHAT I'VE BEEN TOLD BY MULTIPLE MECHANICS IS THAT IT IS A DESIGN DEFECT THE FORD DID FOR THAT YEAR. MY MECHANIC SAID HE'S BEEN FIXING THE SAME ISSUE ON FORD ESCAPE, LINCOLN MKZ, LINCOLN MKS, AND SOME FORD TRUCKS THAT ARE 2013. MY CAR IS BELOW 75,000 MILES AND THIS IS TY
... PICALLY A FIX THAT DOESN'T OCCUR UNTIL 120,000 MILES. IF THIS IS A DESIGN DEFECT THAN FORD SHOULD BE PAYING FOR IT NOT ME. THE CAR IS NOT OLD NOR DOES IT HAVE A HIGH MILES. THIS OUTRAGEOUSRead more
Incident date: Jun 3, 2019
THE REAR CAMERA WORKS INTERMITTENTLY. AT TIMES THE VIEW IS UPSIDE DOWN OR RIGHT SIDE UP OR BLACK.
Incident date: May 25, 2019
IN MAY AND JUNE OF 2019 ON 2 DIFFERENT OCCASIONS, OUR 2016 LINCOLN MKX IGNITION 'TURNED OFF' ON ITS OWN WITHOUT ANY INPUT BY THE DRIVER WHILE USING CRUISE-CONTROL ON A CROWDED HIGHWAY GOING 75 MPH! WHEN IT OCCURRED, A TEXT MESSAGE WAS DISPLAYED SUPERIMPOSED OVER THE TACHOMETER THAT READ: 'CAUTION: IGNITION TURNED OFF'. FORTUNATELY, WHEN IT TURNED OFF, THE CAR AUTOMATICALLY SHIFTED INTO 'NEUTRAL'
... INSTEAD OF 'PARK', WHICH IT DOES AUTOMATICALLY WHEN THE IGNITION SWITCH IS USED TO TURN THE CAR 'OFF'! AFTER IT SHUT OFF, WE COASTED IN 'NEUTRAL' WITHOUT POWER BRAKES OR POWER STEERING WHILE SURROUNDED BY MACK TRUCKS AND OTHER CARS. THANK GOD THERE WAS A SHOULDER ON THE ROADWAY WHERE WE COULD SAFELY PULL OVER. BEFORE WE COULD ATTEMPT TO RESTART THE CAR, WE HAD TO COAST TO A COMPLETE STOP, PUT THE CAR IN 'PARK', DEPRESS THE BRAKE PEDAL, AND PRESS THE IGNITION BUTTON. HAD WE BEEN IN A WORK-ZONE W/CONCRETE BARRICADES AND NO SHOULDER, WE COULD HAVE BEEN RUN OVER/KILLED BY A MACK TRUCK AND/OR OTHER CAR(S) APPROACHING FROM BEHIND AT HIGH SPEEDS. THE SERVICE MANAGER AT OUR LINCOLN DEALERSHIP SAID THEY HAVE NEVER HEARD OF THIS OCCURRENCE, BUT WE EASILY FOUND TWO (2) WEBSITES DISCUSSING THIS ISSUE REGARDING THE MKX. WE CAN ONLY WONDER HOW MANY PEOPLE MAY HAVE ALREADY DIED WITH NO EXPLANATION ABOUT WHY THEY WERE AT A FULL STOP ON A BUSY HIGHWAY. BECAUSE WE RESTARTED THE CAR, THE SERVICE MANAGER SAID THE "ERROR" HISTORY IN THE COMPUTER WAS ERASED - BAD PROGRAMING! BOTH TIMES OUR INCIDENTS HAPPENED, WE HAD BEEN DRIVING ABOUT AN HOUR ON THE HIGHWAY. THE CAR HAS BEEN 'IN THE SHOP' AT THE DEALERSHIP FOR 2 WEEKS, AND WE ARE STILL AWAITING AN EXPLANATION AND FIX. I'M NOT SURE I'LL EVER FEEL CONFIDENT/SAFE ENOUGH TO DRIVE IT AGAIN!Read more
Incident date: May 25, 2019
IN MAY AND JUNE OF 2019 ON 2 DIFFERENT OCCASIONS, OUR 2016 LINCOLN MKX IGNITION 'TURNED OFF' ON ITS OWN WITHOUT ANY INPUT BY THE DRIVER WHILE USING CRUISE-CONTROL ON A CROWDED HIGHWAY GOING 75 MPH! WHEN IT OCCURRED, A TEXT MESSAGE WAS DISPLAYED SUPERIMPOSED OVER THE TACHOMETER THAT READ: 'CAUTION: IGNITION TURNED OFF'. FORTUNATELY, WHEN IT TURNED OFF, THE CAR AUTOMATICALLY SHIFTED INTO 'NEUTRAL'
... INSTEAD OF 'PARK', WHICH IT DOES AUTOMATICALLY WHEN THE IGNITION SWITCH IS USED TO TURN THE CAR 'OFF'! AFTER IT SHUT OFF, WE COASTED IN 'NEUTRAL' WITHOUT POWER BRAKES OR POWER STEERING WHILE SURROUNDED BY MACK TRUCKS AND OTHER CARS. THANK GOD THERE WAS A SHOULDER ON THE ROADWAY WHERE WE COULD SAFELY PULL OVER. BEFORE WE COULD ATTEMPT TO RESTART THE CAR, WE HAD TO COAST TO A COMPLETE STOP, PUT THE CAR IN 'PARK', DEPRESS THE BRAKE PEDAL, AND PRESS THE IGNITION BUTTON. HAD WE BEEN IN A WORK-ZONE W/CONCRETE BARRICADES AND NO SHOULDER, WE COULD HAVE BEEN RUN OVER/KILLED BY A MACK TRUCK AND/OR OTHER CAR(S) APPROACHING FROM BEHIND AT HIGH SPEEDS. THE SERVICE MANAGER AT OUR LINCOLN DEALERSHIP SAID THEY HAVE NEVER HEARD OF THIS OCCURRENCE, BUT WE EASILY FOUND TWO (2) WEBSITES DISCUSSING THIS ISSUE REGARDING THE MKX. WE CAN ONLY WONDER HOW MANY PEOPLE MAY HAVE ALREADY DIED WITH NO EXPLANATION ABOUT WHY THEY WERE AT A FULL STOP ON A BUSY HIGHWAY. BECAUSE WE RESTARTED THE CAR, THE SERVICE MANAGER SAID THE "ERROR" HISTORY IN THE COMPUTER WAS ERASED - BAD PROGRAMING! BOTH TIMES OUR INCIDENTS HAPPENED, WE HAD BEEN DRIVING ABOUT AN HOUR ON THE HIGHWAY. THE CAR HAS BEEN 'IN THE SHOP' AT THE DEALERSHIP FOR 2 WEEKS, AND WE ARE STILL AWAITING AN EXPLANATION AND FIX. I'M NOT SURE I'LL EVER FEEL CONFIDENT/SAFE ENOUGH TO DRIVE IT AGAIN!Read more
Incident date: May 25, 2019
IN MAY AND JUNE OF 2019 ON 2 DIFFERENT OCCASIONS, OUR 2016 LINCOLN MKX IGNITION 'TURNED OFF' ON ITS OWN WITHOUT ANY INPUT BY THE DRIVER WHILE USING CRUISE-CONTROL ON A CROWDED HIGHWAY GOING 75 MPH! WHEN IT OCCURRED, A TEXT MESSAGE WAS DISPLAYED SUPERIMPOSED OVER THE TACHOMETER THAT READ: 'CAUTION: IGNITION TURNED OFF'. FORTUNATELY, WHEN IT TURNED OFF, THE CAR AUTOMATICALLY SHIFTED INTO 'NEUTRAL'
... INSTEAD OF 'PARK', WHICH IT DOES AUTOMATICALLY WHEN THE IGNITION SWITCH IS USED TO TURN THE CAR 'OFF'! AFTER IT SHUT OFF, WE COASTED IN 'NEUTRAL' WITHOUT POWER BRAKES OR POWER STEERING WHILE SURROUNDED BY MACK TRUCKS AND OTHER CARS. THANK GOD THERE WAS A SHOULDER ON THE ROADWAY WHERE WE COULD SAFELY PULL OVER. BEFORE WE COULD ATTEMPT TO RESTART THE CAR, WE HAD TO COAST TO A COMPLETE STOP, PUT THE CAR IN 'PARK', DEPRESS THE BRAKE PEDAL, AND PRESS THE IGNITION BUTTON. HAD WE BEEN IN A WORK-ZONE W/CONCRETE BARRICADES AND NO SHOULDER, WE COULD HAVE BEEN RUN OVER/KILLED BY A MACK TRUCK AND/OR OTHER CAR(S) APPROACHING FROM BEHIND AT HIGH SPEEDS. THE SERVICE MANAGER AT OUR LINCOLN DEALERSHIP SAID THEY HAVE NEVER HEARD OF THIS OCCURRENCE, BUT WE EASILY FOUND TWO (2) WEBSITES DISCUSSING THIS ISSUE REGARDING THE MKX. WE CAN ONLY WONDER HOW MANY PEOPLE MAY HAVE ALREADY DIED WITH NO EXPLANATION ABOUT WHY THEY WERE AT A FULL STOP ON A BUSY HIGHWAY. BECAUSE WE RESTARTED THE CAR, THE SERVICE MANAGER SAID THE "ERROR" HISTORY IN THE COMPUTER WAS ERASED - BAD PROGRAMING! BOTH TIMES OUR INCIDENTS HAPPENED, WE HAD BEEN DRIVING ABOUT AN HOUR ON THE HIGHWAY. THE CAR HAS BEEN 'IN THE SHOP' AT THE DEALERSHIP FOR 2 WEEKS, AND WE ARE STILL AWAITING AN EXPLANATION AND FIX. I'M NOT SURE I'LL EVER FEEL CONFIDENT/SAFE ENOUGH TO DRIVE IT AGAIN!Read more
Incident date: Oct 1, 2018
TL* THE CONTACT OWNS A 2011 LINCOLN MKZ. WHILE DRIVING VARIOUS SPEEDS, THE BRAKE PEDAL WAS APPLIED AND TRAVELED TO THE FLOORBOARD WITHOUT WARNING. THE VEHICLE WAS TOWED TO CRAFT HYUNDAI (2625 LAKESIDE DR, LYNCHBURG, VA 24501, (434) 455-7060) WHERE IT WAS DIAGNOSED THAT THE CALIPERS, FRONT BRAKE PADS, MASTER CYLINDER, AND BRAKE HYDRAULIC CONTROL NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED, BUT
... THE FAILURE RECURRED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO STATED THAT THE PARTS NEEDED TO BE REPLACED AGAIN. THE MANUFACTURER WAS CONTACTED AND REFERRED THE CONTACT TO NHTSA. THE FAILURE MILEAGE WAS APPROXIMATELY 92,000.Read more
Incident date: Jun 26, 2019
TAKATA RECALL: I GOT INTO MY MKX AND CLOSED THE DOOR AND THE REAR WINDSHIELD EXPLODED, THERE WERE NO DINGS OR CHIPS AND NOTHING HIT INTO IT. I'VE BEEN READING ONLINE AND IT LOOKS LIKE ITS A PROBLEM I CAN'T AFFORD TO HAVE IT FIXED AND I AM HOPING FORD WILL DO THE RIGHT THING. THANK YOU
Incident date: Jun 19, 2019
TL* THE CONTACT OWNS A 2003 LINCOLN TOWN CAR. THE CONTACT STATED THAT THE FRONT END OF THE VEHICLE WAS SCRAPED. THE VEHICLE WAS TAKEN TO POMPANO FORD (2741 N FEDERAL HWY, POMPANO BEACH, FL 33064, (954) 773-9486) FOR REPAIRS. WHEN THE CONTACT RETRIEVED THE VEHICLE, HE NOTICED THAT THE ENTIRE FLOORBOARD WAS FLOODED WITH WATER. THE DEALER BELIEVED THE WATER WAS DUE TO THE AIR CONDITIONING UNIT FLOODI
... NG OR THE WIPERS PUSHING WATER INSIDE THE VEHICLE. THE DEALER THEN STATED THAT THERE WAS A PAN IN THE ENGINE COMPARTMENT THAT WAS SUPPOSED TO DRAIN WATER OUT INTO THE STREET. THE DEALER TRIED TO BLAME THE INSURANCE COMPANY THAT DIRECTED THE CONTACT TO THE DEALER TO HAVE THE SCRAPE REPAIRED. THE DEALER GAVE THE CONTACT A BILL FOR $880 AND DID NOT CLEAR OUT THE WATER. THE DEALER INFORMED THE CONTACT THAT THE INSURANCE COMPANY WOULD PAY FOR THE REPAIRS. THE DEALER RETURNED THE VEHICLE TO THE CONTACT STILL FULL OF WATER AND GAVE HIM A STATEMENT LISTING THE CHARGES FOR WHICH THEY EXPECTED THE INSURANCE COMPANY TO PAY. THE MANUFACTURER WAS NOT CONTACTED. THE FAILURE MILEAGE WAS 81,000.Read more
Incident date: Jun 19, 2019
TL* THE CONTACT OWNS A 2003 LINCOLN TOWN CAR. THE CONTACT STATED THAT THE FRONT END OF THE VEHICLE WAS SCRAPED. THE VEHICLE WAS TAKEN TO POMPANO FORD (2741 N FEDERAL HWY, POMPANO BEACH, FL 33064, (954) 773-9486) FOR REPAIRS. WHEN THE CONTACT RETRIEVED THE VEHICLE, HE NOTICED THAT THE ENTIRE FLOORBOARD WAS FLOODED WITH WATER. THE DEALER BELIEVED THE WATER WAS DUE TO THE AIR CONDITIONING UNIT FLOODI
... NG OR THE WIPERS PUSHING WATER INSIDE THE VEHICLE. THE DEALER THEN STATED THAT THERE WAS A PAN IN THE ENGINE COMPARTMENT THAT WAS SUPPOSED TO DRAIN WATER OUT INTO THE STREET. THE DEALER TRIED TO BLAME THE INSURANCE COMPANY THAT DIRECTED THE CONTACT TO THE DEALER TO HAVE THE SCRAPE REPAIRED. THE DEALER GAVE THE CONTACT A BILL FOR $880 AND DID NOT CLEAR OUT THE WATER. THE DEALER INFORMED THE CONTACT THAT THE INSURANCE COMPANY WOULD PAY FOR THE REPAIRS. THE DEALER RETURNED THE VEHICLE TO THE CONTACT STILL FULL OF WATER AND GAVE HIM A STATEMENT LISTING THE CHARGES FOR WHICH THEY EXPECTED THE INSURANCE COMPANY TO PAY. THE MANUFACTURER WAS NOT CONTACTED. THE FAILURE MILEAGE WAS 81,000.Read more