Showing 18,739 complaints for LINCOLN
Incident date: Feb 22, 2020
DOOR AJAR WARNING COMES ON DESPITE ALL DOORS BEING CLOSED SECURELY. THIS CAUSES ANY NUMBER OF ISSUES INCLUDING INTERIOR LIGHTS COMING ON WHICH IS NOT SAFE AT NIGHT, ENTRY ALARM GOING OFF AT ANY HOUR OF THE DAY OR NIGHT, AND EXCESSIVE DRAIN ON BATTERY. THE PROBLEM OCCURS BOTH WHILE IN MOTION AND WHILE STATIONARY.
Incident date: Jan 14, 2020
WHILE DRIVING THE 2019 LINCOLN NAUTILUS ON A 4 LANE HIGHWAY WITH ADAPTIVE CRUISE CONTROL AND LANE CENTERING ON, THE CAR ALL OF A SUDDEN TURNED INTO THE NEXT LANE. IT DOES THIS BOTH TO THE RIGHT AND THE LEFT. I WAS ON THE PHONE WITH BOTH MY MOTHER AND THE LINCOLN SERVICE MANAGER ON SEPARATE INCIDENTS WHEN IT OCCURRED. ALSO, I TOOK IT ON A TEST DRIVE WITH THE LEAD MECHANIC AND IT DID THE SAME
... THING TO HIM TO THE RIGHT, RIGHT WHERE OUR VETERINARIAN OFFICE IS LOCATED. CENTER LINE WAS STILL THERE. AFTER THEY HAD THE CAR FOR A FEW DAYS, AND A CONVERSATION WITH THE GENERAL MANAGER, THEY DETERMINED THAT IT WAS WORKING AS DESIGNED, THEY CHECKED OTHER NON-NAUTULIS VEHICLES AND FOUND THE SAME THING. THEY TOLD ME THAT IT WOULD NOT HAPPEN ON AN INTERSTATE. I WAS SHOCKED. THERE IS NO DIFFERENCE BETWEEN A 4 LANE HIGHWAY AND AN INTERSTATE. I AM A RETIRED NAVY OPERATIONAL TEST PILOT, AND WE WOULD NEVER ALLOW THIS TO BE GIVEN TO THE FLEET OPERATORS. I CHECKED THE OPERATORS MANUAL ON PAGE 239. HERE IS WHAT IT SAYS: THE SYSTEM MAY NOT CORRECTLY OPERATE IN ANY OF THE FOLLOWING CONDITIONS: ' YOUR VEHICLE IS NOT CENTERED IN THE LANE. ' THE LANE IS TOO NARROW OR WIDE. ' THE SYSTEM DOES NOT DETECT AT LEAST ONE LANE MARKING OR WHEN LANES MERGE OR SPLIT. ' YOU SWITCH THE DIRECTION INDICATOR ON. ' LIMITED STEERING TORQUE INPUT IS APPLIED. ' AREAS UNDER CONSTRUCTION OR NEW INFRASTRUCTURE. ' WHEN MODIFICATIONS TO THE STEERING SYSTEM HAVE BEEN MADE. ' WHEN USING A SPARE TIRE. NOTE CONDITION ABOVE: ' THE SYSTEM DOES NOT DETECT AT LEAST ONE LANE MARKING OR WHEN LANES MERGE OR SPLIT AT THE TIME OF THE INCIDENTS THERE WERE TURN LANES ON EACH SIDE OF THE CAR WITH SMALL OPENINGS TO MOVE INTO THE TURN LANE. THE CENTER LANE MARKINGS WERE ALWAYS THERE.Read more
Incident date: Jan 14, 2020
WHILE DRIVING THE 2019 LINCOLN NAUTILUS ON A 4 LANE HIGHWAY WITH ADAPTIVE CRUISE CONTROL AND LANE CENTERING ON, THE CAR ALL OF A SUDDEN TURNED INTO THE NEXT LANE. IT DOES THIS BOTH TO THE RIGHT AND THE LEFT. I WAS ON THE PHONE WITH BOTH MY MOTHER AND THE LINCOLN SERVICE MANAGER ON SEPARATE INCIDENTS WHEN IT OCCURRED. ALSO, I TOOK IT ON A TEST DRIVE WITH THE LEAD MECHANIC AND IT DID THE SAME
... THING TO HIM TO THE RIGHT, RIGHT WHERE OUR VETERINARIAN OFFICE IS LOCATED. CENTER LINE WAS STILL THERE. AFTER THEY HAD THE CAR FOR A FEW DAYS, AND A CONVERSATION WITH THE GENERAL MANAGER, THEY DETERMINED THAT IT WAS WORKING AS DESIGNED, THEY CHECKED OTHER NON-NAUTULIS VEHICLES AND FOUND THE SAME THING. THEY TOLD ME THAT IT WOULD NOT HAPPEN ON AN INTERSTATE. I WAS SHOCKED. THERE IS NO DIFFERENCE BETWEEN A 4 LANE HIGHWAY AND AN INTERSTATE. I AM A RETIRED NAVY OPERATIONAL TEST PILOT, AND WE WOULD NEVER ALLOW THIS TO BE GIVEN TO THE FLEET OPERATORS. I CHECKED THE OPERATORS MANUAL ON PAGE 239. HERE IS WHAT IT SAYS: THE SYSTEM MAY NOT CORRECTLY OPERATE IN ANY OF THE FOLLOWING CONDITIONS: ' YOUR VEHICLE IS NOT CENTERED IN THE LANE. ' THE LANE IS TOO NARROW OR WIDE. ' THE SYSTEM DOES NOT DETECT AT LEAST ONE LANE MARKING OR WHEN LANES MERGE OR SPLIT. ' YOU SWITCH THE DIRECTION INDICATOR ON. ' LIMITED STEERING TORQUE INPUT IS APPLIED. ' AREAS UNDER CONSTRUCTION OR NEW INFRASTRUCTURE. ' WHEN MODIFICATIONS TO THE STEERING SYSTEM HAVE BEEN MADE. ' WHEN USING A SPARE TIRE. NOTE CONDITION ABOVE: ' THE SYSTEM DOES NOT DETECT AT LEAST ONE LANE MARKING OR WHEN LANES MERGE OR SPLIT AT THE TIME OF THE INCIDENTS THERE WERE TURN LANES ON EACH SIDE OF THE CAR WITH SMALL OPENINGS TO MOVE INTO THE TURN LANE. THE CENTER LANE MARKINGS WERE ALWAYS THERE.Read more
Incident date: Jan 1, 2018
TL* THE CONTACT OWNS A 2014 LINCOLN MKZ. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 16V875000 (SEAT BELTS) AND 15V246000 (LATCHES/LOCKS/LINKAGES) HOWEVER, THE PARTS TO DO THE RECALL REPAIRS WERE NOT YET AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER AND ROBINSON BROTHERS FORD (LOCATED AT 11455 AIRLINE HWY, BATON ROUGE, LA 70816) HAD EXCEEDED A REASONABLE AMOUNT OF TIME FOR TH
... E RECALL REPAIR. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT.Read more
Incident date: Jan 1, 2018
TL* THE CONTACT OWNS A 2014 LINCOLN MKZ. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 16V875000 (SEAT BELTS) AND 15V246000 (LATCHES/LOCKS/LINKAGES) HOWEVER, THE PARTS TO DO THE RECALL REPAIRS WERE NOT YET AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER AND ROBINSON BROTHERS FORD (LOCATED AT 11455 AIRLINE HWY, BATON ROUGE, LA 70816) HAD EXCEEDED A REASONABLE AMOUNT OF TIME FOR TH
... E RECALL REPAIR. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT.Read more
Incident date: Oct 3, 2019
WHILE WAITING AT A STOP SIGN, THE VEHICLE IN FRONT OF ME STARTED TO GO. SOMEONE GOING ACROSS TRAFFFIC RAN THE STOP SIGN. THE DRIVER IN FRONT OF ME HIT THE BRAKES TO AVOID COLLISION. WHEN I ATTEMPTED TO BRAKE MY BRAKES JUST KIND OF SPUTTERED FORWARD AND I WAS UNABLE TO STOP IN TIME TO AVOID HITTING THE BACK OF THE CAR IN FRONT OF ME. THERE WAS NO DAMAGE TO MY VEHICLE BUT THE OTHER PARTY DID REPORT
... MINOR DAMAGES TO THEIR VEHICLE WHICH I WAS FORCED TO PAY FOR.Read more
Crash
Incident date: Sep 21, 2019
ALTHOUGH THE WARNING WAS DISPLAYED, I WAS NOT AWARE THAT MY CAR ONLY HAD AN ELECTRONIC POWER STEERING. THIS TYPE OF ISSUE IS ONE THAT CAN TRULY CAUSE A SERIOUS ACCIDENT SHOULD ONE IS DRIVING WHEN THEIR POWER STEERING GO OUT. THE POWER STEERING ON THIS CAR STOPS MORE THAN JUST YOUR STEERING WHEEL AND I FOR ONE THINK THAT THERE NEEDS TO BE A RECALL. IT'S A GOOD THING THAT I WAS PARKED AND GLAD BE
... CAUSE MY DAUGHTER WAS WITH ME.Read more
Incident date: Sep 21, 2019
ALTHOUGH THE WARNING WAS DISPLAYED, I WAS NOT AWARE THAT MY CAR ONLY HAD AN ELECTRONIC POWER STEERING. THIS TYPE OF ISSUE IS ONE THAT CAN TRULY CAUSE A SERIOUS ACCIDENT SHOULD ONE IS DRIVING WHEN THEIR POWER STEERING GO OUT. THE POWER STEERING ON THIS CAR STOPS MORE THAN JUST YOUR STEERING WHEEL AND I FOR ONE THINK THAT THERE NEEDS TO BE A RECALL. IT'S A GOOD THING THAT I WAS PARKED AND GLAD BE
... CAUSE MY DAUGHTER WAS WITH ME.Read more
Incident date: Sep 21, 2019
ALTHOUGH THE WARNING WAS DISPLAYED, I WAS NOT AWARE THAT MY CAR ONLY HAD AN ELECTRONIC POWER STEERING. THIS TYPE OF ISSUE IS ONE THAT CAN TRULY CAUSE A SERIOUS ACCIDENT SHOULD ONE IS DRIVING WHEN THEIR POWER STEERING GO OUT. THE POWER STEERING ON THIS CAR STOPS MORE THAN JUST YOUR STEERING WHEEL AND I FOR ONE THINK THAT THERE NEEDS TO BE A RECALL. IT'S A GOOD THING THAT I WAS PARKED AND GLAD BE
... CAUSE MY DAUGHTER WAS WITH ME.Read more
Incident date: Feb 14, 2020
AS PER RECALL CRUISE CONTROL NEITHRT STARTS OR WORKS ON HIGHWAY
Incident date: Jan 10, 2020
TL* THE CONTACT OWNS A 2008 LINCOLN MKZ. THE CONTACT STATED THAT WHILE DRIVING AT 20 MPH, HE DROVE OVER A PATCH OF ICE, THE BRAKE PEDAL WAS DEPRESSED AND WENT TO THE FLOORBOARD WITH THE ABS WARNING LIGHT ILLUMINATED. THE CONTACT TOOK THE VEHICLE TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THE VEHICLE WITH A DEFECTIVE ANTI-LOCK BRAKE (ABS) UNIT. THE CONTACT THEN RECEIVED NOTIFICATION OF NHTSA CAMPAIGN
... NUMBER: 19V904000 (SERVICE BRAKES, HYDRAULIC) WHICH THE CONTACT LINKED TO THE FAILURE. THE CONTACT THEN TOOK THE VEHICLE TO SARATOGA FORD 3002 NY-50, SARATOGA SPRINGS, NY 12866 WHERE HE WAS INFORMED THAT THE ELECTRONIC CONTROL UNIT(ECU) WAS DEFECTIVE AND NEEDED TO BE REPLACED. THE CONTACT WAS GIVEN AN ESTIMATE FOR THE REPAIR. THE CONTACT WAS ALSO NOTIFIED BY THE DEALER THAT THE PARTS WERE UNAVAILABLE FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS APPROXIMATELY 133,000. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.Read more
Incident date: Feb 15, 2020
THE POWER STEERING CUTS OUT WHILE VEHICLE IS IN MOTION. ERROR MESSAGE STATES POWER STEERING ASSIST FAILURE, TYPICALLY DURING A HARD TURN AT LOW SPEED SUCH AS IN OR OUT OF A PARKING SPOT. 15V340000 RECALL IS FOR THE NEXT MODEL YEAR AND THE DEALER AND MANUFACTURER HAVE STATED THIS VEHICLE CANNOT BE FIXED UNDER THAT RECALL.
Incident date: Feb 13, 2020
I WAS DRIVING ON THE HIGHWAY AROUND 70MPH WHEN MY SUNROOF EXPLODED. THERE IS A LOT OF PEOPLE REPORTING THE SAME ISSUE, BUT UNFORTUNATELY FORD/LINCOLN DOESN'T TAKE ANY RESPONSIBILITY AND IT'S OBVIOUS THAT IS A DEFECT AND REALLY DANGEROUS FOR PEOPLE IN THE VEHICLE.
Incident date: Jan 14, 2020
TL* THE CONTACT OWNS A 2012 LINCOLN MKZ. THE CONTACT STATED WHILE DRIVING APPROXIMATELY 35- 40 MPH, LOST CONTROL OF THE VEHICLE AND CRASHED INTO A WOODED ELECTRIC POLE, HOWEVER THE AIR BAGS DID NOT DEPLOY. THE DRIVER SUSTAINED A BROKEN NOSE, CONTUSIONS ON THE KNEES, SPRAINED ANKLE AND WRIST AS WELL AS THE PASSENGER SUSTAINED CONTUSIONS ON THE KNEES AND HEAD INJURIES THAT REQUIRED MEDICAL ATTENTI
... ON. NO WARNING LIGHTS ILLUMINATED BEFORE THE CRASH. A POLICE REPORT WAS FILED. THE VEHICLE WAS TOWED TO ALEX KARRAS LINCOLN, INC. (6760 14TH ST W, BRADENTON, FL 34207) WHERE THE FAILURE WAS NOT DIAGNOSED AS THE VEHICLE WAS DEEMED A TOTAL LOSS. THE MANUFACTURER WAS CONTACTED HOWEVER NO ASSISTANCE WAS OFFERED. THE CONTACT MENTIONED THAT THE PASSENGER FRONT AIR BAG WAS SERVICED UNDER AN UNKNOWN AIR BAG RECALL IN 2016. THE APPROXIMATE FAILURE MILEAGE WAS 40,000.Read more
Crash
2 injured
Incident date: Feb 14, 2020
TL* THE CONTACT OWNS A 2009 LINCOLN MKS. THE CONTACT STATED HIS WIFE THE DRIVER WAS AT A STOPPED SIGN AND WHILE PRECEDING INTO THE INTERSECTION THE VEHICLE FRONT PASSENGER SIDE COLLIDED WITH ANOTHER VEHICLE. THE AIR BAGS DEPLOYED AND WITHIN A FEW SECONDS A FIRE WAS STARTED. HOWEVER, THE FLAMES EXTINGUISHED THEMSELVES AND THE VEHICLE CABIN WAS FILLED WITH SMOKE. THE CONTACT STATED THAT HIS WIFE'S R
... IGHT SIDE COAT SLEEVE WAS ON FIRE AND SHE WAS ABLE TO EXIT THE VEHICLE. THE CONTACT MENTIONED THAT HIS WIFE PATTED THE COAT SLEEVE TO EXTINGUISH THE COAT FLAMES. THE CONTACT MENTIONED THAT HE WAS CONCERNED THAT THE FIRE WAS STARTED DUE TO THE AIR BAGS GASES AS THE AIR BAGS EXPLODED. THE FIRE DEPARTMENT OR POLICE WAS NOT NOTIFIED. THE CONTACT'S WIFE WENT TO URGENT CARE FOR MEDICAL TREATMENT DUE TO SHOULDER PAIN AND THE INJURIES TO HER WRIST FROM THE FIRE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE THE FAILURE WAS NOT DIAGNOSED BUT THE CONTACT STATED THAT THE MECHANIC STATED THAT THE WAS SURPRISED THAT THE AIR BAGS HAD DEPLOYED. THE CONTACT ALSO STATED THAT THE AIRBAGS WERE CUT OUT OF THE VEHICLE AS HE HAD THE AIR BAGS. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND REFERRED THE CONTACT TO NHTSA. THE APPROXIMATE FAILURE MILEAGE WAS 124,000.Read more
Crash
Fire
1 injured
Incident date: Dec 30, 2019
THE PCM/ECM MODULE WENT OUT ON THIS VEHICLE WITHOUT ANY WARNING. THERE WERE SEVERAL TSB'S ISSUED BY FORD REGARDING THIS ISSUE DATING BACK TO AT LEAST 2013 WITH ABSOLUTELY NO NOTIFICATION TO OWNERS WHOSE LIVES ARE AT RISK (SEE LIST BELOW). THIS MODULE IS THE MAIN COMPUTER, SO ALL POWER WAS LOST AFTER THE CHECK ENGINE LIGHT BEGUN RAPIDLY FLASHING NON-STOP AND THE VEHICLE WAS SHAKING AGGRESSIVELY ON
... THE HIGHWAY WHILE DRIVING. TO ADD INSULT TO INJURY THE REPAIR IS ESTIMATED AT NEARLY $4000 BECAUSE ALL SPARKS PLUGS, ALL IGNITION COILS MUST BE REPLACED ALONG WITH THE THROTTLE BODY. (TSB NUMBERS RELATED TO THIS ISSUE ARE AS FOLLOWS: NHTSA ID #10052190, NHTSA ID #10109070, NHTSA ID #10048099)Read more
Incident date: Dec 30, 2019
THE PCM/ECM MODULE WENT OUT ON THIS VEHICLE WITHOUT ANY WARNING. THERE WERE SEVERAL TSB'S ISSUED BY FORD REGARDING THIS ISSUE DATING BACK TO AT LEAST 2013 WITH ABSOLUTELY NO NOTIFICATION TO OWNERS WHOSE LIVES ARE AT RISK (SEE LIST BELOW). THIS MODULE IS THE MAIN COMPUTER, SO ALL POWER WAS LOST AFTER THE CHECK ENGINE LIGHT BEGUN RAPIDLY FLASHING NON-STOP AND THE VEHICLE WAS SHAKING AGGRESSIVELY ON
... THE HIGHWAY WHILE DRIVING. TO ADD INSULT TO INJURY THE REPAIR IS ESTIMATED AT NEARLY $4000 BECAUSE ALL SPARKS PLUGS, ALL IGNITION COILS MUST BE REPLACED ALONG WITH THE THROTTLE BODY. (TSB NUMBERS RELATED TO THIS ISSUE ARE AS FOLLOWS: NHTSA ID #10052190, NHTSA ID #10109070, NHTSA ID #10048099)Read more
Incident date: Dec 30, 2019
THE PCM/ECM MODULE WENT OUT ON THIS VEHICLE WITHOUT ANY WARNING. THERE WERE SEVERAL TSB'S ISSUED BY FORD REGARDING THIS ISSUE DATING BACK TO AT LEAST 2013 WITH ABSOLUTELY NO NOTIFICATION TO OWNERS WHOSE LIVES ARE AT RISK (SEE LIST BELOW). THIS MODULE IS THE MAIN COMPUTER, SO ALL POWER WAS LOST AFTER THE CHECK ENGINE LIGHT BEGUN RAPIDLY FLASHING NON-STOP AND THE VEHICLE WAS SHAKING AGGRESSIVELY ON
... THE HIGHWAY WHILE DRIVING. TO ADD INSULT TO INJURY THE REPAIR IS ESTIMATED AT NEARLY $4000 BECAUSE ALL SPARKS PLUGS, ALL IGNITION COILS MUST BE REPLACED ALONG WITH THE THROTTLE BODY. (TSB NUMBERS RELATED TO THIS ISSUE ARE AS FOLLOWS: NHTSA ID #10052190, NHTSA ID #10109070, NHTSA ID #10048099)Read more
Incident date: Jan 29, 2020
DRIVING ON HIGHWAY AT POSTED SPEED LIMIT OF 65MPH AND BRAKES FAILED. BRAKE PEDAL WENT ALL THE WAY TO THE FLOOR. PEDAL TO THE FLOOR HAPPENED THREE SEPARATE TIMES DURING THE SAME TRIP. VEHICLE WAS EXTREMELY DIFFICULT TO STOP AND BRAKES LOCKED UP. VEHICLE BEGAN SLIDING. BRAKE FAILURE DUE TO ANTI-LOCK BRAKING SYSTEM FAILURE. THIS PERTAINS TO RECALL NHTSA 19V-904. I HAD THE CAR TOWED TO A LINCOLN DEAL
... ERSHIP AND SERVICE TECHNICIAN SAID THE PROBLEM HAS TO DO WITH THE RECALL. MY CAR IS EXTREMELY UNSAFE TO DRIVE AND THE RECALL PARTS ARE NOT AVAILABLE YET. LINCOLN IS NOT PAYING FOR AN INTERM REPAIR NOR OFFERING RENTAL CARS. I HAVE BEEN WITHOUT MY CAR FOR 13 DAYS. LINCOLN SHOULD BE MORE CONCERNED WITH THIS RECALL AND BE PAYING FOR INTERM REPAIRS.Read more
Incident date: Dec 31, 2019
I RECEIVED A RECALL NOTICE FROM LINCOLN DESCRIBING THE SAFET ISSUES IN DECEMBER OF 2019. SINCE THEN MY CAR WAS NEVER RECALLED FOR THE SAFETY RECALL REPAIR. SAFETY RECALL 19S/41 / NHTSA RECALL 19V-809
Incident date: Feb 13, 2020
I WAS DRIVING MY CAR AND ALL OF A SUDDEN MY POWER STEERING GOES OUT TRACTION CONTROL AND PARK HILL ASSIST ALL FLASH. THIS IS THE SECOND TIME IT HAS HAPPENED TRAVELING 70 MPH . I WAS ABLE TO GET OFF OF THE ROAD BUT HAD A DIFFICULT TIME TURNING THE WHEEL AS IT FELT LIKE IT WAS ALMOST LOCKED. PLEASE ADVISE. THANKS
Incident date: Feb 13, 2020
I WAS DRIVING MY CAR AND ALL OF A SUDDEN MY POWER STEERING GOES OUT TRACTION CONTROL AND PARK HILL ASSIST ALL FLASH. THIS IS THE SECOND TIME IT HAS HAPPENED TRAVELING 70 MPH . I WAS ABLE TO GET OFF OF THE ROAD BUT HAD A DIFFICULT TIME TURNING THE WHEEL AS IT FELT LIKE IT WAS ALMOST LOCKED. PLEASE ADVISE. THANKS
Incident date: Feb 13, 2020
GOT RECALL LETTER. AFFRAID TO DRIVE VEHICLE WITH AIRBAG THAT KILLS. DEALER DONT HAVE PART. NEED S LOANER TILL CAR IS FIXED BUT FORD POLICY IS LOANER ONLY DURING ACTUAL REPAIR IS DONE NOT WHILE WAITING FOR PARTS TO ARRIVE. WHAT IF ACCIDENT HAPPENS B4 PARTS GETS HERE.
Incident date: Jan 24, 2020
PASSENGER'S SIDE HEADLAMP BECAME INOPERATIVE (BURNED OUT). UPON INVESTIGATION AT THE LINCOLN DEALERSHIP THEY NOTICED THE BULB WAS NOT FULLY SEATED. CLOSER INSPECTION REVEALED THAT ONE OF THE EARS THAT SPRING CLIP LOCKS TO WAS MISSING FROM THE ASSEMBLY. THERE WAS NO EXPLANATION OF HOW THE SPRING CLIP LOCKS WERE MISSING. CONCERN IS IN ASSEMBLY OF THIS VEHICLES THIS PIECE WAS NEVER ADDED. ONE COU
... LD LOOSE A HEADLIGHT OR BOTH AT ANY TIME AND IN DARK CIRCUMSTANCES COULD BE A SAFETY CONCERN TO THOSE ON THE ROAD POTENTIALLY CAUSING AN ACCIDENT.Read more
Incident date: Feb 7, 2020
2013 LINCOLN MKZ, 3.7L WITH 32516 MILES 2/7/20 AT 9:30 AM TRAVELING AT 60 MPH ON A 4 LANE HIGHWAY THE MOTOR CUT OUT. DROVE IT TO THE FORD DEALER WHO RAIN DIAGNOSTICS AND FOUND NOTHING.
Incident date: Jan 28, 2020
TL* THE CONTACT OWNS A 2008 LINCOLN MKX. THE CONTACT STATED THAT THERE WAS A STRONG FUEL ODOR IN THE CABIN OF THE VEHICLE. THE CONTACT LOOKED UNDERNEATH THE VEHICLE AND BECAME AWARE OF FUEL LEAKING FROM THE FUEL TANK. DANA FORD LINCOLN LOCATED AT 266 WEST SERVICE ROAD, STATEN ISLAND, NY 10314 (718) 983-8700, WAS CONTACTED BY PHONE AND INFORMED OF THE FAILURE. THE MANUFACTURER WAS NOT CONTACTED NOR
... INFORMED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 139,000.Read more
Incident date: Dec 1, 2019
ON SEVERAL OCCASIONS WHILE OWNING THIS CAR, THE BRAKE PEDAL HAS GONE ALMOST TO THE FLOOR AFTER ACTIVATION OF THE ANTI-LOCK BRAKES. THE BRAKING DISTANCE INCREASES DRAMATICALLY WHILE THE PEDAL REMAINS VERY SOFT. IT EVENTUALLY (A FEW HOURS MAYBE) RETURNS TO NORMAL FUNCTION. WHILE DRIVING IN THIS CONDITION, IT FEELS AS IF THE CAR WILL NOT STOP BUT IT EVENTUALLY DOES, BUT THE BRAKE PEDAL MUST BE PUS
... HED ALMOST ALL THE WAY TO THE FLOOR.Read more
Incident date: Jan 8, 2019
TL* THE CONTACT OWNS A 2010 LINCOLN MKZ. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 25 MPH, THE VEHICLE WENT OVER A BUMP IN THE ROADWAY AND LOST THE BRAKING ABILITY. NO WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS DRIVEN TO THE DEALER DOWNS FORD INC, 360 NEW JERSEY AVE 37, TOMS RIVER, NJ 08753, WHERE IT WAS DETERMINED THAT HYDRAULIC CONTROL UNIT NEEDED TO BE REPLACED. THE CONTACT STATE
... D THAT THE FAILURE RECURRED FOUR TIMES. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 89,400. *BF CONSUMER STATED HER FAMILY REMEMBER HAS THE SAME MODEL, HAS RECEIVED A RECALL BUT SHE DIDN'T.*JBRead more
Incident date: Feb 2, 2020
WHILE STATIONARY AFTER TURNING ON THE VEHICLE THERE IS A HARD SHIFT IN GEARS FROM PARK TO DRIVE. WHILE VEHICLE IS IN MOTION ON THE CITY STREET THERE IS A HARD SHIFT AROUND 35 MPH TO 55 MPH. WHILE DRIVING ON THE CITY STREET AFTER 5 MILES THE VEHICLE START SPUTTERING AND NOT SHIFTING GEARS PROPERLY THEN THERE ISN'T ANY ACCELERATION FROM A TRAFFIC LIGHT STOP AND GO. AND THEN IT PICKS BACK UP AND DRI
... VE HIGH RPM SOUND. OR HIGH REV SOUNDS. IN ADDITION THE GAS CAP UNIT IS FAULTY I REPLACED IT BEFORE AND NOW IT APPEARS IT HAS TO BE REPLACED AGAIN BECAUSE IT WON'T CLOSE PROPERLY. A P0171 CODE MAF SENSOR CAME UP ALONG WITH TRANSMISSION CODES FOR THE 5TH AND 4TH GEAR RATIO ACCORDING TO THE DIAGNOSTICS REPORTED FROM THE OB READING AND SOME ADDITIONAL CODES THAT I CAN'T EVEN DESCRIBE. FOR THE MOST PART THE VEHICLE STALLS WHILE DRIVING CITY AND HIGHWAY WHICH MAKES IT VERY DANGEROUS TO DRIVERead more
Incident date: Feb 2, 2020
WHILE STATIONARY AFTER TURNING ON THE VEHICLE THERE IS A HARD SHIFT IN GEARS FROM PARK TO DRIVE. WHILE VEHICLE IS IN MOTION ON THE CITY STREET THERE IS A HARD SHIFT AROUND 35 MPH TO 55 MPH. WHILE DRIVING ON THE CITY STREET AFTER 5 MILES THE VEHICLE START SPUTTERING AND NOT SHIFTING GEARS PROPERLY THEN THERE ISN'T ANY ACCELERATION FROM A TRAFFIC LIGHT STOP AND GO. AND THEN IT PICKS BACK UP AND DRI
... VE HIGH RPM SOUND. OR HIGH REV SOUNDS. IN ADDITION THE GAS CAP UNIT IS FAULTY I REPLACED IT BEFORE AND NOW IT APPEARS IT HAS TO BE REPLACED AGAIN BECAUSE IT WON'T CLOSE PROPERLY. A P0171 CODE MAF SENSOR CAME UP ALONG WITH TRANSMISSION CODES FOR THE 5TH AND 4TH GEAR RATIO ACCORDING TO THE DIAGNOSTICS REPORTED FROM THE OB READING AND SOME ADDITIONAL CODES THAT I CAN'T EVEN DESCRIBE. FOR THE MOST PART THE VEHICLE STALLS WHILE DRIVING CITY AND HIGHWAY WHICH MAKES IT VERY DANGEROUS TO DRIVERead more
Incident date: Feb 2, 2020
WHILE STATIONARY AFTER TURNING ON THE VEHICLE THERE IS A HARD SHIFT IN GEARS FROM PARK TO DRIVE. WHILE VEHICLE IS IN MOTION ON THE CITY STREET THERE IS A HARD SHIFT AROUND 35 MPH TO 55 MPH. WHILE DRIVING ON THE CITY STREET AFTER 5 MILES THE VEHICLE START SPUTTERING AND NOT SHIFTING GEARS PROPERLY THEN THERE ISN'T ANY ACCELERATION FROM A TRAFFIC LIGHT STOP AND GO. AND THEN IT PICKS BACK UP AND DRI
... VE HIGH RPM SOUND. OR HIGH REV SOUNDS. IN ADDITION THE GAS CAP UNIT IS FAULTY I REPLACED IT BEFORE AND NOW IT APPEARS IT HAS TO BE REPLACED AGAIN BECAUSE IT WON'T CLOSE PROPERLY. A P0171 CODE MAF SENSOR CAME UP ALONG WITH TRANSMISSION CODES FOR THE 5TH AND 4TH GEAR RATIO ACCORDING TO THE DIAGNOSTICS REPORTED FROM THE OB READING AND SOME ADDITIONAL CODES THAT I CAN'T EVEN DESCRIBE. FOR THE MOST PART THE VEHICLE STALLS WHILE DRIVING CITY AND HIGHWAY WHICH MAKES IT VERY DANGEROUS TO DRIVERead more
Incident date: Feb 4, 2020
TL* THE CONTACT OWNS A 2013 LINCOLN MKS. THE CONTACT STATED THAT WHILE ATTEMPTING TO COLD START THE VEHICLE, THE VEHICLE FAILED TO START. THE VEHICLE WAS TOWED TO SENTRY LINCOLN 940 BOSTON TURNPIKE SHREWSBURY, MA 01545 (508) 281-8171, TO BE DIAGNOSED. THE PROGNOSIS WAS THAT THE FUEL CONTROL MODULE NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBE
... R: 16V621000 (FUEL SYSTEM, GASOLINE). THE MANUFACTURER WAS CONTACTED AND INFORMED OF THE FAILURE. THE FAILURE MILEAGE WAS 65,000.*BF*JBRead more
Incident date: Feb 4, 2020
TL* THE CONTACT OWNS A 2013 LINCOLN MKS. THE CONTACT STATED THAT WHILE ATTEMPTING TO COLD START THE VEHICLE, THE VEHICLE FAILED TO START. THE VEHICLE WAS TOWED TO SENTRY LINCOLN 940 BOSTON TURNPIKE SHREWSBURY, MA 01545 (508) 281-8171, TO BE DIAGNOSED. THE PROGNOSIS WAS THAT THE FUEL CONTROL MODULE NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBE
... R: 16V621000 (FUEL SYSTEM, GASOLINE). THE MANUFACTURER WAS CONTACTED AND INFORMED OF THE FAILURE. THE FAILURE MILEAGE WAS 65,000.*BF*JBRead more
Incident date: Feb 6, 2020
WAS DRIVING 2008 LINCOLN MKX PASSENGER SEAT CAUGHT ON FIRE, HEATED SEAT WAS NOT ON
Fire
Incident date: Jan 13, 2020
BRAKES INTERMITTENTLY DON'T GRAB SOMETIMES AND SOMETIME THEY GRIND WHEN APPLIED. I HAVE HAD THEM WORKED ON MULTIPLE TIMES AND I'VE HAD MECHANICS TO TELL ME THAT THERE'S SOME PROBLEM IN THE CONTROL UNIT THAT'S CAUSING THIS. I'VE HAD EVERYTHING REPLACED AND IT STILL HAPPENS.
Incident date: Feb 3, 2020
MY DAUGHTER WAS A RESTRAINED DRIVER ON A HIGHWAY ---IN RUSH HOUR TRAFFIC, MOVING ABOUT 55MPH. THE CAR IN FRONT OF HER BRAKED SUDDENLY AND WHEN MY DAUGHTER PUSHED ON THE BRAKE IT WENT TO THE FLOOR AND SHE HAD NO BRAKES. SHE CLIPPED THAT CAR REAR END AND SWERVED RIGHT'HITTING A SECOND CAR AS SHE GOT TO THE SHOULDER. SHE SCRAPPED ALONG THE METAL RAIL FOR A DISTANCE AND THEN WENT OFF THE
... ROAD IN TO A GULLY AND HIT A POLE AND AN DIRT EMBANKMENT. BOTH AIR BAGS DEPLOYED. THE LIGHT POLE DID NOT LOOK DAMAGED, I THINK THE POLE MUST HAVE HAD A LARGE CEMENT BASE, BASED ON THE EXTENT AND SHAPE OF THE FRONT END DAMAGE. THE CAR IS TOTALED. THE AIR BAGS DID A GREAT JOB. SHE HAS A BAD SPRAIN ON HER ANKLE THAT SHE WAS TRYING TO BRAKE WITH AND SORE EVERYWHERE. A FAMILY MEMBER WORKS AT FORD . HE ASKED ME TO CHECK THE BRAKE FLUID SINCE BOTH FRONT AND REAR BRAKES FAILED. I CHECKED THE BRAKE PEDDLE AND IT WENT TO THE FLOOR WITHOUT ANY RESISTANCE. I CHECKED THE BRAKE RESERVOIR AND IT WAS FULL. MY FAMILY MEMBER TOLD ME TO SUBMIT THIS REPORT.Read more
Crash
2 injured
Incident date: Mar 7, 2019
TL* THE CONTACT OWNS A 2008 LINCOLN MKZ. WHILE DRIVING 33 MPH THE BRAKE PEDAL WAS DEPRESSED HOWEVER, THE BRAKE FAILED TO ENGAGE QUICKLY CAUSING THE CONTACT TO REAR END ANOTHER VEHICLE. NO WARNING LIGHTS WERE ILLUMINATED. THE CONTACT STATED THAT THE BRAKE FAILURE WAS AN ON GOING ISSUE. NO INJURIES WERE SUSTAINED AND A POLICE REPORT WAS FILED. THE VEHICLE WAS TAKEN TO THE AN INDEPENDENT MECHANIC WH
... OM DIAGNOSED THE FAILURE AS THE MASTER CYLINDER HOWEVER, THE VEHICLE WAS NOT REPAIRED. THE VEHICLE WAS THEN TAKEN TO A DEALER WHOM STATED THAT THE FAILURE WAS NOT RELATED TO THE MASTER CYLINDER HOWEVER, A FAILURE CAUSE WAS NOT DIAGNOSED. THE CONTACT STATED RECENTLY RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 19V904000 (SERVICE BRAKES, HYDRAULIC) AND THE VEHICLE WAS TAKEN TO A DEALER WHERE THE FAILURE WAS DIAGNOSED AS BEING RELATED TO THE RECALL. HOWEVER, THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE BUT NO ASSISTANCE WAS OFFERED. THE CONTACT WAS UPSET THAT THE PARTS WERE NOT AVAILABLE FOR THE RECALL REMEDY IN A TIMELY MANNER. THE FAILURE MILEAGE WAS UNKNOWN. VIN TOOL CONFIRMS PARTS WERE NOT AVAILABLE.Read more
Crash
Incident date: Feb 14, 2016
TL* THE CONTACT OWNS A 2009 FORD MKZ. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 40 MPH THE BRAKING SYSTEM FAILED WHEN PRESSING THE BRAKE PEDAL CAUSING THE VEHICLE TO CRASH INTO THE REAR OF A COMMERCIAL TRUCK. DURING THE CRASH NO INJURIES WERE REPORTED. A POLICE REPORT( [XXX]) WAS TAKEN AT THE SCENE AND THE VEHICLE WAS TOWED AWAY. THE VEHICLE DAMAGE WAS REPAIRED BUT BRAKE FAILURES CONTINU
... ED. AFTER RETRIEVING THE VEHICLE THE BRAKE FAILURE CONTINUE AND THE BRAKE WAS SPONGY CAUSING THE BRAKING DISTANCE TO BE EXTENDED. THE VEHICLE WAS TAKEN TO THE LOCAL DEALER COLMINGER FORD(5011 JAKE ALEXANDER BLVD S. SALSBURY NC) ON SEVERAL OCCASIONS FOR THE BRAKE FAILURE. THE ABS MODULE AND BRAKING ASSEMBLY AND CONTROL (Y) WERE ALL REPLACED BUT THE FAILURES CONTINUED TO OCCUR. THE CONTACT RECENTLY RECEIVED A RECALL NOTICE FOR THE NHTSA RECALL CAMPAIGN NUMBER 19V904000(BRAKING SYSTEM). THE MANUFACTURER([XXX]) WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 88,096. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Crash
Incident date: Mar 22, 2013
CAR SPEEDS AND SLOWS DOWN ON ITS OWN ON HIGHWAYS AND SIDE STREETS IT IS VERY DANGEROUS
Incident date: Mar 22, 2013
CAR SPEEDS AND SLOWS DOWN ON ITS OWN ON HIGHWAYS AND SIDE STREETS IT IS VERY DANGEROUS
Incident date: Jul 1, 2019
WHEN WHEN I PUT MY CAR INTO PARK IT DOESN'T ALWAYS REGISTER THAT THE CAR IS IN PARK AND THE P DOESN'T LIGHT UP. A NOTICE POPS UP ON MY DASH AND TELLS MEN TO PUT MY CAR INTO PARK.
Incident date: Feb 2, 2020
LIKE 2,000,000 OTHER FORD AND LINCOLN VEHICLES ALREADY UNDER RECALL, MY DRIVER'S SIDE DOOR LATCH IS DEFECTIVE. YESTERDAY, WHEN I WENT TO OPEN THE DOOR, THE HANDLE SWUNG OPEN WITHOUT OPENING THE DOOR. AFTER DOING SOME ONLINE RESEARCH, I FOUND THIS IS AN EXTENSIVE PROBLEM AFFECTING FORD AND LINCOLN VEHICLES MANUFACTURED BETWEEN 2010 THROUGH 2015. PLEASE EXPAND YOUR RECALL TO INCLUDE THE 2011 TO 2
... 012 LINCOLN MKZ'S IN ADDITION TO TO 2013 THROUGH 2015 MKZ'S ALREADY UNDER RECALL.Read more
Incident date: Jan 1, 2020
FORD IS RECALLING MY VEHICLE UNDER 19S54. FORD KNOWS OF 15 CRASHES RELATED TO THIS PROBLEM BUT THE RECALL NOTICE SAYS THE VEHICLE IS SAFE TO DRIVE UNTIL THE PARTS ARE AVAILABLE. HOW CAN THE VEHICLE BE SAFE TO DRIVE IF FORD KNOWS OF 15 CRASHES RELATED TO THE ISSUE? FORD SHOULD SUPPLY A RENTAL CAR UNTIL THEY ARE ABLE TO FIX THE PROBLEM.
Incident date: Feb 3, 2020
PASSENGER DOOR AJAR ALERT COMES ON RANDOMLY, EVEN WHEN THE PASSENGER DOOR HASN'T BEEN OPENED OR SHUT IN DAYS. IT HAS HAPPENED WHEN THE VEHICLE IS STATIONARY AND WHEN IT IS IN MOTION.
Incident date: Jan 8, 2020
TL* THE CONTACT OWNS A 1999 LINCOLN TOWN CAR. THE CONTACT STATED WHILE DRIVING AT AN UNDISCLOSED SPEED, THE CONTACT BECAME AWARE OF NOTICED LIQUID DRIPPING FROM THE AIR VENTS. THE VEHICLE WAS TAKEN TO A LOCAL MECHANIC FOR DIAGNOSIS AND REPAIR. THE DIAGNOSIS WAS A FAILURE WITH THE INTAKE MANIFOLD. THE DEALER WAS NOT CONTACTED AND THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE APPROXIMATE
... FAILURE MILEAGE WAS 150,000.Read more
Incident date: Feb 1, 2020
TL* THE CONTACT OWNS A 2004 LINCOLN NAVIGATOR. THE CONTACT STATED THAT THE REAR AIR SUSPENSION HAD FAILED CAUSING THE REAR END TO BOUNCE UP AND DOWN AND WHILE DRIVING A CLANKING NOISE WAS PRESENT COMING FROM THE FRONT DRIVER SIDE WHEEL. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE FRONT SUSPENSION ARM WAS NEEDED TO BE REPLACED AND THE REAR SUSPENSION AIR BAGS NEEDED TO B
... E REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE BUT NO ASSISTANCE WAS OFFERED. THE LOCAL DEALER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 150,000.Read more
Incident date: Jan 31, 2020
STARTED MY CAR TO LET IT WARM UP, WHEN I RETURNED AND WENT TO LEAVE THE DRIVEWAY IT FLASHED SERVICE STABILITRAC AND SERVICE POWER STEERING. TRIED TO DRIVE IT AND HAD NO POWER STEERING. THERE IS A RECALL ON MANY OF THIS SAME CAR FOR THE SAME REASON BUT NONE FOR MY VIN #.
Incident date: Jan 31, 2020
STARTED MY CAR TO LET IT WARM UP, WHEN I RETURNED AND WENT TO LEAVE THE DRIVEWAY IT FLASHED SERVICE STABILITRAC AND SERVICE POWER STEERING. TRIED TO DRIVE IT AND HAD NO POWER STEERING. THERE IS A RECALL ON MANY OF THIS SAME CAR FOR THE SAME REASON BUT NONE FOR MY VIN #.
Incident date: Oct 1, 2019
SINCE 2017, TOUCH SCREEN WENT TO BLACK SEVERAL TIMES WHEN I STARTED THE CAR ON A CITY STREET, AND WOULD NOT TURN ON WITHIN 24 HOURS. GOT MORE SERIOUS IN 2019, THE SCREEN DIDN'T TURN ON AFTER 3 DAYS. I TOOK THE CAR TO A LOCAL DEALER. WAS DIAGNOSED AND REPLACED DEFECTIVE APIM AND UPDATED TO LATEST LEVEL FOR PMI ON OCT 1, 2019, MILEAGE: 60759. PAID FOR $965.64.
Incident date: Jan 25, 2020
DRIVING AT HIGHWAY SPEED IN THE MIDDLE LANE DURING HEAVY RAIN. SUDDENLY THE STEERING BECAME ALMOST RIGID. FORTUNATELY WE WERE ABLE TO GET TO THE SIDE OF THE ROAD WITHOUT INCIDENT. THE CAR HAD RECENTLY BEEN RECALLED AND REPAIRED REGARDING THE BOLTS ON THE POWER STEERING ASSIST MODULE. OBVIOUSLY THERE REMAINS AN INHERENT DESIGN FLAW IN THE STEERING ASSIST FUNCTION, DISABLING STEERING CAPABILITY THA
... T COULD HAVE PROVEN FATAL. THE STEERING MODULE HAS BEEN REPLACED BUT WE HAVE LOST CONFIDENCE IN THE VEHICLE.Read more