Showing 18,739 complaints for LINCOLN
Incident date: May 28, 2020
TL* THE CONTACT OWNS A 2016 LINCOLN MKZ. THE CONTACT STATED THAT FOR 5-10 MINUTES WHILE ATTEMPTING TO SECURE THE DRIVER'S SIDE FRONT SEAT BELT, SEVERAL ATTEMPTS WERE NEEDED TO SECURELY LATCH THE SEAT BELT. THE CONTACT STATED THAT THE FAILURE WAS EXPERIENCED DURING THE DAYTIME HOURS BUT NOT AT NIGHT. THE VEHICLE WAS TAKEN TO FUTURE FORD LINCOLN LOCATED AT 650 AUTOMALL DR, ROSEVILLE, CA 95661, (888)
... 656-7577, WHERE THE TECHNICIAN WAS MADE AWARE OF THE FAILURE. THE VEHICLE HAD NOT BEEN DIAGNOSED OR REPAIRED AS OF YET. THE MANUFACTURER HAD NOT BEEN INFORMED OF FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 283,000.Read more
Incident date: May 31, 2020
LOSS OF POWER ASSIST STEERING, COULD NOT CONTROL VEHICLE ON THE ROAD. STEERING WAS STICKY, NOT SMOOTH ROTATION OF STEERING WHEEL, HARD TO MAINTAIN A STRAIGHT LINE IT STARTED WHILE DRIVING ON THE HIGHWAY WITH A WARNING TO SERVICE STEERING NOW AND WHEN I TURNED OFF THE CAR TO LOOK AT IT, WHEN I STARTED IT BACK UP, I LOST ALL POWER STEERING ASSIST. CAR IS AT THE DEALER NOW FOR A $2000 REPAIR. I CAN P
... ROVIDE REPAIR BILL IN 2 OR 3 DAYS IF NEED. *TRRead more
Incident date: May 22, 2020
TL* THE CONTACT OWNS A 2012 LINCOLN MKT. THE CONTACT STATED WHILE HIS WIFE WAS STARTING THE VEHICLE, THE STEERING WHEEL BECAME DIFFICULT TO TURN. THE CONTACT STATED THE POWER STEERING ASSIST WARNING MESSAGE WAS DISPLAYED ON THE INSTRUMENT PANEL. THE VEHICLE WAS TOWED TO INDEPENDENT MECHANIC WHERE THE CONTACT WAS INFORMED THAT THE VIN WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V340000 (STEERING). THE
... CONTACT STATED HIS WIFE CONTACTED KRIEGERS FORD LOCATED AT 3205 NORTH HIGHWAY 61, MUSCATINE, IA 52761, (563) 263-5324, AND WAS INFORMED THAT THE MILEAGE EXCEEDED THE 150,000 MILES LIMIT. THE CONTACT WAS INFORMED THAT THE VEHICLE WAS NO LONGER ELIGIBLE FOR THE FREE REPAIR. THE VEHICLE WAS NOT DIAGNOSED NOR REPAIRED. THE MANUFACTURER WAS NOT INFORMED OF THE FAILURE. THE FAILURE MILEAGE WAS 181,000.Read more
Incident date: May 23, 2020
I'VE PURCHASED MY 2013 LINCOLN MKT AWD ECOBOOST ON 1-5-2020. TWO DAYS AFTER BUYING IT, I HAD TO REPLACE THE FUEL PUMP. MY CHECK ENGINE LIGHT CAME ON STATED PO420 CATALYST SYSTEM EFFICIENCY BELOW THRESHOLD BANK 1. THE SECOND ROW'S SEATBELT WON'T COME OUT PROPERLY. CAN'T HAVE ANYONE SIT AT THAT SEAT. FOR SOME REASON I AM UNABLE TO USE MY WINDSHIELD WATER NOZZLE (NOT SURE WHAT'S IT CALLED). I'VE BEEN
... GETTING A MESSAGE STATING POWER STEERING FAULT, I TURN OFF THE CAR THEN TURN IT BACK ON AND IT GOES AWAY. THANK GOD THE STEERING WHEEL FAULT NEVER GAVE ME ISSUES WHILE DRIVING. AS OF LAST WEEK, I HAVEN'T BEEN ABLE TO DRIVE MY CAR B/C OF THE POWER STEERING FAULT. NOT TOO HAPPY WITH THIS VEHICLE. I'VE HAD IT LESS THEN A YEAR AND ALREADY HAVING SO MANY PROBLEMS WITH IT. *TRRead more
Incident date: May 23, 2020
I'VE PURCHASED MY 2013 LINCOLN MKT AWD ECOBOOST ON 1-5-2020. TWO DAYS AFTER BUYING IT, I HAD TO REPLACE THE FUEL PUMP. MY CHECK ENGINE LIGHT CAME ON STATED PO420 CATALYST SYSTEM EFFICIENCY BELOW THRESHOLD BANK 1. THE SECOND ROW'S SEATBELT WON'T COME OUT PROPERLY. CAN'T HAVE ANYONE SIT AT THAT SEAT. FOR SOME REASON I AM UNABLE TO USE MY WINDSHIELD WATER NOZZLE (NOT SURE WHAT'S IT CALLED). I'VE BEEN
... GETTING A MESSAGE STATING POWER STEERING FAULT, I TURN OFF THE CAR THEN TURN IT BACK ON AND IT GOES AWAY. THANK GOD THE STEERING WHEEL FAULT NEVER GAVE ME ISSUES WHILE DRIVING. AS OF LAST WEEK, I HAVEN'T BEEN ABLE TO DRIVE MY CAR B/C OF THE POWER STEERING FAULT. NOT TOO HAPPY WITH THIS VEHICLE. I'VE HAD IT LESS THEN A YEAR AND ALREADY HAVING SO MANY PROBLEMS WITH IT. *TRRead more
Incident date: May 23, 2020
I'VE PURCHASED MY 2013 LINCOLN MKT AWD ECOBOOST ON 1-5-2020. TWO DAYS AFTER BUYING IT, I HAD TO REPLACE THE FUEL PUMP. MY CHECK ENGINE LIGHT CAME ON STATED PO420 CATALYST SYSTEM EFFICIENCY BELOW THRESHOLD BANK 1. THE SECOND ROW'S SEATBELT WON'T COME OUT PROPERLY. CAN'T HAVE ANYONE SIT AT THAT SEAT. FOR SOME REASON I AM UNABLE TO USE MY WINDSHIELD WATER NOZZLE (NOT SURE WHAT'S IT CALLED). I'VE BEEN
... GETTING A MESSAGE STATING POWER STEERING FAULT, I TURN OFF THE CAR THEN TURN IT BACK ON AND IT GOES AWAY. THANK GOD THE STEERING WHEEL FAULT NEVER GAVE ME ISSUES WHILE DRIVING. AS OF LAST WEEK, I HAVEN'T BEEN ABLE TO DRIVE MY CAR B/C OF THE POWER STEERING FAULT. NOT TOO HAPPY WITH THIS VEHICLE. I'VE HAD IT LESS THEN A YEAR AND ALREADY HAVING SO MANY PROBLEMS WITH IT. *TRRead more
Incident date: Nov 12, 2019
TL* THE CONTACT OWNS A 2016 LINCOLN MKX. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 19V809000 (ELECTRICAL SYSTEM) HOWEVER, THE PART NEEDED FOR THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. BOWLING GREEN LINCOLN AUTO SALES (1079 N MAIN ST, BOWLING GREEN, OH 43402) WAS CONTACTED AND INFORMED THE CON
... TACT THAT THE PARTS WERE NOT AVAILABLE. THE MANUFACTURER WAS CONTACTED AND CONFIRMED PARTS NOT AVAILABLE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT. *BF CONSUMER STATES THAT REPAIRS FOR THE RECALL HAVE BEEN COMPLETED. *DLRead more
Incident date: May 27, 2020
TL* THE CONTACT OWNS A 2006 LINCOLN ZEPHYR. THE CONTACT STATED THAT THE AIR BAGS WARNING LIGHT WAS ILLUMINATED. THE VEHICLE WAS TAKEN TO JOE MACHENS FORD LOCATED AT 1911 W WORLEY ST, COLUMBIA, MO 65203, (573) 445-4411, WHERE THE DEALER WAS MADE AWARE OF THE FAILURE. THE CONTACT WAS INFORMED THAT THE VEHICLE WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 19V001000 (AIR BAGS). THE VEHICLE WAS NOT REPAIRED.
... THE MANUFACTURER WAS NOT INFORMED OF THE FAILURE. THE FAILURE MILEAGE WAS 162,426.Read more
Incident date: Oct 18, 2019
AROUND SEPTEMBER 2019, THE BRAKE BOOSTER ON MY LINCOLN MKX BEGAN FAILING, GETTING WORSE AND WORSE QUICKLY. IT GOT TO THE POINT THAT I HAD TO ALMOST STAND WITH TWO FEET ON THE BRAKE TO MAKE THE CAR STOP. (WHICH WAS FRIGHTENING WHEN I WAS TRYING TO STOP THE CAR BEFORE HITTING THE ONE IN FRONT OF ME, EVEN THOUGHT I WAS ONLY GOING ABOUT 30-40 MPH). WHEN I PRESSED THE BRAKE THE PEDAL WOULD SLIGHTLY
... DEPRESS, THEN HISS AND THEN WITH MY INCREASED PRESSURE ON THE BRAKE PEDAL IT WOULD DEPRESS FURTHER, SEEMINGLY CLOSE TO THE CAR FLOOR. THE CAR BECAME INCREASINGLY DIFFICULT TO STOP. MY MECHANIC SAID MY BRAKE BOOSTER NEEDED REPLACED AND THAT THERE WAS AN EXTENDED WARRANTY ON THE PART. I PURCHASED THE CAR USED. I CALLED FORD AND GAVE THEM MY VIN NUMBER AND THEY SAID THAT THE BAD PARTS STOPPED BEING USED IN MARCH OF 2013 AND THAT MY CAR WAS PRODUCED IN MAY OF 2013. WELL OBVIOUSLY SINCE I HAD THE EXACT SAME PROBLEM AS THAT WHICH WAS THE SUBJECT OF THE RECALL, THE BAD PART WAS USED IN MY CAR AS WELL. FORD OPENED A CASE (#24559511K4) BUT REFUSED TO COVER THE REPAIR. I HAD TO PAY OUT OF POCKET TO HAVE MY CAR REPAIRED SINCE IT WAS DANGEROUS TO CONTINUE TO DRIVE. THE MILEAGE ON THE CAR AT THE TIME OF REPAIR IN OCTOBER 2019 WAS 110,334. I BELIEVE THE FORD SHOULD REIMBURSE ME FOR THE COST OF THE REPAIR.Read more
Incident date: May 25, 2020
VEHICLE WAS PARKED OUTSIDE DURING RAIN SHOWERS AND WATER ACCUMULATED INSIDE THE REAR PASSENGER FOOT AREA 1ST AND OVERFLOWED INTO THE FRONT PASSENGER'S FOOT AREA.
Incident date: May 15, 2020
2007 LINCOLN MKZ V6. THE WHEEL/RIMS ARE GARBAGE. THEY ARE FALLING APART, CRACKS IN THE METAL, FINISH PEELING, AROUND THE TIRE PIECES OF THE RIM HAS FALLEN OFF. I CAN'T BELIEVE LINCOLN WOULD USE SUCH JUNK. I HAVE TO KEEP CHECKING THE AIR PRESSURE BECAUSE THE WHEELS/RIMS ARE SO TORN UP. I JUST BOUGHT THE CAR TWO WEEKS AGO. LINCOLN NEEDS TO HAVE A RECALL ON THESE WHEELS BEFORE SOMEONE GETS KILLED BEC
... AUSE OF THEM FALLING APART. THE WELDS ARE BREAKING APART. THESE WHEELS/RIMS ARE DANGEROUS. *TRRead more
Incident date: May 11, 2020
TL* THE CONTACT'S GRANDMOTHER OWNS A 2017 LINCOLN CONTINENTAL. THE CONTACT STATED THE REAR PASSENGER DOOR AJAR WARNING LIGHT WAS ILLUMINATED. THE VEHICLE WAS TAKEN TO MILLER FORD LOCATED AT 1596 NJ-38, LUMBERTON, NJ 08048, (609) 261-7836, TO BE DIAGNOSED. THE CONTACT WAS INFORMED THAT THE REAR PASSENGER DOOR LATCH NEEDED TO BE REPLACED. THE VEHICLE HAD NOT BEEN REPAIRED AS OF YET. UPON INVESTIGATI
... ON, THE CONTACT ASSOCIATED THE FAILURE WITH NHTSA CAMPAIGN NUMBER: 19V077000 (LATCHES/LOCKS/LINKAGES) HOWEVER, THE VIN WAS INCLUDED IN THE RECALL. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE CONTACT WAS INFORMED THAT NHTSA CAMPAIGN NUMBER: 19V077000 (LATCHES/LOCKS/LINKAGES) REPAIR WAS NOT COMPLETED IN NOVEMBER OF 2019. THE FAILURE MILEAGE WAS 158,780. *DT*JBRead more
Incident date: Feb 1, 2020
THIS LINCOLN MKT HAS GIVEN CONTINUAL PROBLEMS WITH FUEL ISSUES, ENGINE PROBLEMS, CHECK ENGINE LIGHT CONSTANTLY COMING ON AND TAKING IT BACK AND FORTH TO THE DEALER AND THEY CANT EVEN FIGURE OUT THE ISSUE AS TO WHY THE CHECK ENGINE LIGHT KEEPS COMING ON. THE VEHICLE HAS FUMES COMING FROM THE PIPES, IT JERKS AND THREATENS TO CUT OFF AND WITH ALL THE REPAIRS DONE AND COMPLAINTS SENT TO THE LINCOLN
... CORP, THERE IS STILL NO RESOLVE. THIS IS OUR FAMILY CAR, BUT WE NEVER KNOW WHEN IT IS GOING TO SHUT OFF OR START SMOKING OR WHEN THE CHECK ENGINE LIGHT WILL COME ON. THIS MAKES THE VEHICLE UNSAFE TO DRIVE AND IT SEEMS TO BE UNREPAIRABLE. ESPECIALLY SINCE EACH TIME WE GET IT BACK FROM THE DEALERSHIP, THE LIGHT COMES BACK ON. THESE PROBLEMS OCCUR WITH THE VEHICLE IN MOTION. I DON'T KNOW WHEN IT IS GOING TO FUNCTION PROPERLY OR NOT AND MOST TIMES, I HAVE MY CHILDREN WITH ME. IT IS REALLY SCARY. *TRRead more
Incident date: Feb 1, 2020
THIS LINCOLN MKT HAS GIVEN CONTINUAL PROBLEMS WITH FUEL ISSUES, ENGINE PROBLEMS, CHECK ENGINE LIGHT CONSTANTLY COMING ON AND TAKING IT BACK AND FORTH TO THE DEALER AND THEY CANT EVEN FIGURE OUT THE ISSUE AS TO WHY THE CHECK ENGINE LIGHT KEEPS COMING ON. THE VEHICLE HAS FUMES COMING FROM THE PIPES, IT JERKS AND THREATENS TO CUT OFF AND WITH ALL THE REPAIRS DONE AND COMPLAINTS SENT TO THE LINCOLN
... CORP, THERE IS STILL NO RESOLVE. THIS IS OUR FAMILY CAR, BUT WE NEVER KNOW WHEN IT IS GOING TO SHUT OFF OR START SMOKING OR WHEN THE CHECK ENGINE LIGHT WILL COME ON. THIS MAKES THE VEHICLE UNSAFE TO DRIVE AND IT SEEMS TO BE UNREPAIRABLE. ESPECIALLY SINCE EACH TIME WE GET IT BACK FROM THE DEALERSHIP, THE LIGHT COMES BACK ON. THESE PROBLEMS OCCUR WITH THE VEHICLE IN MOTION. I DON'T KNOW WHEN IT IS GOING TO FUNCTION PROPERLY OR NOT AND MOST TIMES, I HAVE MY CHILDREN WITH ME. IT IS REALLY SCARY. *TRRead more
Incident date: Feb 1, 2020
THIS LINCOLN MKT HAS GIVEN CONTINUAL PROBLEMS WITH FUEL ISSUES, ENGINE PROBLEMS, CHECK ENGINE LIGHT CONSTANTLY COMING ON AND TAKING IT BACK AND FORTH TO THE DEALER AND THEY CANT EVEN FIGURE OUT THE ISSUE AS TO WHY THE CHECK ENGINE LIGHT KEEPS COMING ON. THE VEHICLE HAS FUMES COMING FROM THE PIPES, IT JERKS AND THREATENS TO CUT OFF AND WITH ALL THE REPAIRS DONE AND COMPLAINTS SENT TO THE LINCOLN
... CORP, THERE IS STILL NO RESOLVE. THIS IS OUR FAMILY CAR, BUT WE NEVER KNOW WHEN IT IS GOING TO SHUT OFF OR START SMOKING OR WHEN THE CHECK ENGINE LIGHT WILL COME ON. THIS MAKES THE VEHICLE UNSAFE TO DRIVE AND IT SEEMS TO BE UNREPAIRABLE. ESPECIALLY SINCE EACH TIME WE GET IT BACK FROM THE DEALERSHIP, THE LIGHT COMES BACK ON. THESE PROBLEMS OCCUR WITH THE VEHICLE IN MOTION. I DON'T KNOW WHEN IT IS GOING TO FUNCTION PROPERLY OR NOT AND MOST TIMES, I HAVE MY CHILDREN WITH ME. IT IS REALLY SCARY. *TRRead more
Incident date: May 14, 2020
THE WARNING LIGHTS FOR TRACTION CONTROL MALFUNCTION, ABS MALFUNCTION AND BRAKE MALFUNCTION SIMULTANEOUSLY ILLUMINATED ON THE DASH, ALONG WITH WARNING CHIMES, AND THE BRAKES STOPPED FUNCTIONING AS DESIGNED. THE VEHICLE WOULD NOT STOP WITH BRAKE PEDAL APPLICATION (PEDAL WAS SOFT, FAR TOO EASY TO DEPRESS, BUT INEFFECTIVE). CAR WAS STEERED INTO A RESIDENTIAL LAWN AND EMERGENCY HAND BRAKE APPLIED TO AV
... OID A COLLISION. *TRRead more
Incident date: May 15, 2020
PASSENGER SEAT AIRBAG DEPLOYED OVERNIGHT. CAR WAS TURNED OFF AND PARKED IN DRIVEWAY, 50' FROM STREET. *TR
Incident date: Dec 11, 2019
TL* THE CONTACT OWNS A 2007 LINCOLN MKZ. THE CONTACT STATED THAT WHILE DRIVING AT VARIOUS SPEEDS, AN ABNORMAL SQUEAKING SOUND WAS HEARD WHILE DEPRESSING THE BRAKE PEDAL. THE CONTACT THEN RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 19V904000 (SERVICE BRAKES, HYDRAULIC) HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TI
... ME FOR THE RECALL REPAIR. THE MANUFACTURER NOR THE DEALER HAD BEEN NOTIFIED OF THE ISSUE. THE FAILURE MILEAGE WAS 85,000. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.Read more
Incident date: Mar 1, 2020
STARTED HAVE PROBLEMS WITH THE HEAT ON THE CAR, TOOK IT TO THE FORD DEALERSHIP AND WAS TOLD THE ENGINE NEEDED TO BE REPLACED. ACCORDING TO TSB 19-2346 IT IS A KNOWN DEFECT WITH THIS MODEL OF VEHICLE AND THEY REFUSE TO PAY FOR REPAIR DUE IT BEING OUT OF WARRANTY. *TR
Incident date: May 14, 2020
I TURNED ON MY CAR AND RECEIVED A MESSAGE FROM IN THE INFORMATION PANEL STATING, " POWER STEERING ASSIST FAULT". ITS EXTREMELY HARD TO TURN MY STEERING WHEEL. I DRIVE EASY ON MY CAR AND THE ROADS ARE SMOOTH IN MY COMMUTES. *TR
Incident date: Dec 11, 2018
INSTRUMENT CLUSTER DEPROGRAMS ITSELF, INTERIOR LIGHTING STOPPED WORKING, FOLDING EXTERIOR MIRRORS FOLD THEMSELVES WITHOUT COMMAND TO DO SO,REAR VIEW MIRROR CHANGES IT SETTING WITHOUT COMMAND, HUD FLASHES MULTICOLOR LIGHTS ONTO WINDSHIELD VIEWING AREA, APPROACH LIGHTING STOPPED WORKING. SYNC3 WAS PROGRAMMED TO DISPLAY MAP ON STARTUP BUT RECENTLY CAME UP WITH DIFFERENT SETUP. ALL OCCURRED WHILE VEHI
... CLE WAS STATIONARY. BEGAN 12/11/2018 UNTIL PRESENT. *TRRead more
Incident date: Dec 11, 2018
INSTRUMENT CLUSTER DEPROGRAMS ITSELF, INTERIOR LIGHTING STOPPED WORKING, FOLDING EXTERIOR MIRRORS FOLD THEMSELVES WITHOUT COMMAND TO DO SO,REAR VIEW MIRROR CHANGES IT SETTING WITHOUT COMMAND, HUD FLASHES MULTICOLOR LIGHTS ONTO WINDSHIELD VIEWING AREA, APPROACH LIGHTING STOPPED WORKING. SYNC3 WAS PROGRAMMED TO DISPLAY MAP ON STARTUP BUT RECENTLY CAME UP WITH DIFFERENT SETUP. ALL OCCURRED WHILE VEHI
... CLE WAS STATIONARY. BEGAN 12/11/2018 UNTIL PRESENT. *TRRead more
Incident date: Dec 11, 2018
INSTRUMENT CLUSTER DEPROGRAMS ITSELF, INTERIOR LIGHTING STOPPED WORKING, FOLDING EXTERIOR MIRRORS FOLD THEMSELVES WITHOUT COMMAND TO DO SO,REAR VIEW MIRROR CHANGES IT SETTING WITHOUT COMMAND, HUD FLASHES MULTICOLOR LIGHTS ONTO WINDSHIELD VIEWING AREA, APPROACH LIGHTING STOPPED WORKING. SYNC3 WAS PROGRAMMED TO DISPLAY MAP ON STARTUP BUT RECENTLY CAME UP WITH DIFFERENT SETUP. ALL OCCURRED WHILE VEHI
... CLE WAS STATIONARY. BEGAN 12/11/2018 UNTIL PRESENT. *TRRead more
Incident date: May 3, 2020
TL* THE CONTACT LEASED A 2020 LINCOLN CONTINENTAL. THE CONTACT STATED THAT WHILE OPENING THE TRUNK FROM THE DASHBOARD AND UNLOADING GROCERIES FROM THE TRUNK, THE TRUNK LID INDEPENDENTLY CLOSED STICKING HIS HEAD. THE CONTACT MENTIONED THAT THERE WAS NO CHIME AND THAT THE TRUNK WAS HEAVY. THE CONTACT SUSTAINED HEAD AND SHOULDER INJURIES THAT REQUIRED MEDICAL ATTENTION. THE CONTACT CALLED PALM SPRING
... S MOTORS LOCATED AT 69-200 CA-111, CATHEDRAL CITY, CA 92234, AND INFORMED THEM OF THE FAILURE. THE DEALER INFORMED THE CONTACT THAT DUE TO HIM HAVING THE KEY FOB IN HIS POCKET, THE COMPUTER UNDERNEATH THE BUMPER WAS ACTIVATED CAUSING THE TRUNK TO CLOSE OR THAT THE KEY FOB MIGHT BE DEFECTIVE. THE DEALER REFUSED TO BUY BACK THE VEHICLE. THE VEHICLE WAS NOT TAKEN TO A DEALER FOR A DIAGNOSTIC TESTING. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 160.Read more
1 injured
Incident date: Oct 8, 2019
BALL JOINTS, OUTER TIE ROD ENDS AND STEERING SECTION GOES BAD, DOING A LOT OF POPPING AND CREAKING. *TR
Incident date: Oct 8, 2019
BALL JOINTS, OUTER TIE ROD ENDS AND STEERING SECTION GOES BAD, DOING A LOT OF POPPING AND CREAKING. *TR
Incident date: Oct 8, 2019
BALL JOINTS, OUTER TIE ROD ENDS AND STEERING SECTION GOES BAD, DOING A LOT OF POPPING AND CREAKING. *TR
Incident date: Apr 6, 2020
THE VEHICLE WILL INITIALLY HAVE THE SPEED ODOMETER DROP TO 0 MPH WHILE STILL MOVING. A "WRENCH" LIGHT WILL ILLUMINATE ALONG WITH THE AIRBAG LIGHT. THE VEHICLE WILL LOSE POWER AND NOT SHIFT PROPERLY. ONCE THE VEHICLE COMES TO A STOP, THE DRIVER MUST PUSH THE ACCELERATOR DOWN UNTIL THE TACH READS APPROX. 3000 RPMS BEFORE THE VEHICLE WILL START MOVING AGAIN. WHEN IT IS MOVING IT SHIFTS ERRATICALLY AN
... D "BANG" THE GEARS. IF THE DRIVER, AFTER STOPPING, TAKES THE VEHICLE OUT OF DRIVE AND PUTS IN REVERSE, IT BANGS THE TRANSMISSION SO HARD IT FEELS IT GOING TO DROP OUT OF THE VEHICLE. THIS HAPPENED TO ME A NUMBER OF TIMES. THE IMAGE I ATTACHED I WAS GOING 55 MPH. *TRRead more
Incident date: Apr 6, 2020
THE VEHICLE WILL INITIALLY HAVE THE SPEED ODOMETER DROP TO 0 MPH WHILE STILL MOVING. A "WRENCH" LIGHT WILL ILLUMINATE ALONG WITH THE AIRBAG LIGHT. THE VEHICLE WILL LOSE POWER AND NOT SHIFT PROPERLY. ONCE THE VEHICLE COMES TO A STOP, THE DRIVER MUST PUSH THE ACCELERATOR DOWN UNTIL THE TACH READS APPROX. 3000 RPMS BEFORE THE VEHICLE WILL START MOVING AGAIN. WHEN IT IS MOVING IT SHIFTS ERRATICALLY AN
... D "BANG" THE GEARS. IF THE DRIVER, AFTER STOPPING, TAKES THE VEHICLE OUT OF DRIVE AND PUTS IN REVERSE, IT BANGS THE TRANSMISSION SO HARD IT FEELS IT GOING TO DROP OUT OF THE VEHICLE. THIS HAPPENED TO ME A NUMBER OF TIMES. THE IMAGE I ATTACHED I WAS GOING 55 MPH. *TRRead more
Incident date: Apr 6, 2020
THE VEHICLE WILL INITIALLY HAVE THE SPEED ODOMETER DROP TO 0 MPH WHILE STILL MOVING. A "WRENCH" LIGHT WILL ILLUMINATE ALONG WITH THE AIRBAG LIGHT. THE VEHICLE WILL LOSE POWER AND NOT SHIFT PROPERLY. ONCE THE VEHICLE COMES TO A STOP, THE DRIVER MUST PUSH THE ACCELERATOR DOWN UNTIL THE TACH READS APPROX. 3000 RPMS BEFORE THE VEHICLE WILL START MOVING AGAIN. WHEN IT IS MOVING IT SHIFTS ERRATICALLY AN
... D "BANG" THE GEARS. IF THE DRIVER, AFTER STOPPING, TAKES THE VEHICLE OUT OF DRIVE AND PUTS IN REVERSE, IT BANGS THE TRANSMISSION SO HARD IT FEELS IT GOING TO DROP OUT OF THE VEHICLE. THIS HAPPENED TO ME A NUMBER OF TIMES. THE IMAGE I ATTACHED I WAS GOING 55 MPH. *TRRead more
Incident date: Jan 1, 2020
THERE'S BEEN A RECALL ON THE VALVE THAT OPERATES THE BREAKS FORD SAYS IT'S UNSAFE TO DRIVE AND CAN'T GIVE ME AN ANSWER WHEN THESE PARTS WILL BE IN. NOW I SIT HERE WITH A CAR I CANNOT DRIVE.
Incident date: Jan 10, 2019
NAVIGATOR SYSTEM, BLUETOOTH SYSTEM, ARE DISCONNECTED ALL THE TIME, IN THE MIDDLE OF ANY TRIP.
Incident date: Jan 10, 2019
NAVIGATOR SYSTEM, BLUETOOTH SYSTEM, ARE DISCONNECTED ALL THE TIME, IN THE MIDDLE OF ANY TRIP.
Incident date: Jan 10, 2019
NAVIGATOR SYSTEM, BLUETOOTH SYSTEM, ARE DISCONNECTED ALL THE TIME, IN THE MIDDLE OF ANY TRIP.
Incident date: Apr 14, 2020
WITH MY CAR IN PARK, I HAVE SHIFTED TO DRIVE AND REVERSE, AND WHILE MAINTAINING MY FOOT ON THE BRAKE AFTER TRANSFERRING TO DRIVE OR REVERSE THE CAR HAS MOVED BY ITSELF BY APPROXIMATELY 3 FEET BEFORE COMING TO A STOP. EACH TIME THIS HAS HAPPENED I WAS ON A LEVEL SURFACE. THE DEALERSHIP INSPECTED MY CAR BUT COULD NOT FIND ANYTHING THAT WOULD CAUSE THIS TO HAPPEN.
Incident date: Apr 14, 2020
WITH MY CAR IN PARK, I HAVE SHIFTED TO DRIVE AND REVERSE, AND WHILE MAINTAINING MY FOOT ON THE BRAKE AFTER TRANSFERRING TO DRIVE OR REVERSE THE CAR HAS MOVED BY ITSELF BY APPROXIMATELY 3 FEET BEFORE COMING TO A STOP. EACH TIME THIS HAS HAPPENED I WAS ON A LEVEL SURFACE. THE DEALERSHIP INSPECTED MY CAR BUT COULD NOT FIND ANYTHING THAT WOULD CAUSE THIS TO HAPPEN.
Incident date: Apr 26, 2020
DRIVING CAR AND STOPPED TO GET GAS, BLANK INSTRUMENTAL PANEL WHEN I RESTARTED THE CAR. THE PROBLEM WILL NOT RESOLVE UNLESS CAR IS TURNED OFF FOR A PERIOD OF TIME, HOUR OR LONGER.AFTER IT OCCURRED 5 TIMES MARCH - AUGUST 2019 AND HAS SINCE OCCURRED AGAIN DECEMBER 24 2019 AND APRIL 26 2020. "AIR BAG RESTRAINT FAULT" ALERT GOES OFF EVERY TIME. EACH TIME I HAVE HAD IT IN THE DEALERSHIP WITH NOTHING RE
... SOLVED. IMPLEMENTED AND UPDATE IN AUGUST BUT ONLY AFTER I GOT FORD CORPORATE INVOLVED. I AM SO TIRED OF DEALING WITH THIS ISSUE AND IT'S NOT SAFE!Read more
Incident date: Apr 10, 2018
AFTER REPAIRING BRAKES AT MY COST MANY TIMES NOW THEY ARE RECALLED. I HAD TO REPLACE THE LINCOLN WHEELS AT MY COST AFTER RESEARCHING THAT MANY PROBLEMS WERE REPORTED. ALSO WITH ONLY 65,000 MILES ON MY CAR MY TRANSMISSION IS OUT. I HAVE HAD MANY ELECTRICAL ISSUES. IT IS CLEAR THAT MAJOR ISSUES IS ON THE THIS MODEL YEAR. WHILE DRIVING MY TRANSMISSION FAILED. I TOWED THE CAR TO DEALERSHIP AND THEY WA
... NT TO NOW CHARGE 4400.00 FOR THE TRANSMISSION. I AM OUT OF MONEY WITH THIS VEHICLE AND IT WAS CLEARLY POORLY MANUFACTURED. *TRRead more
Incident date: Apr 10, 2018
AFTER REPAIRING BRAKES AT MY COST MANY TIMES NOW THEY ARE RECALLED. I HAD TO REPLACE THE LINCOLN WHEELS AT MY COST AFTER RESEARCHING THAT MANY PROBLEMS WERE REPORTED. ALSO WITH ONLY 65,000 MILES ON MY CAR MY TRANSMISSION IS OUT. I HAVE HAD MANY ELECTRICAL ISSUES. IT IS CLEAR THAT MAJOR ISSUES IS ON THE THIS MODEL YEAR. WHILE DRIVING MY TRANSMISSION FAILED. I TOWED THE CAR TO DEALERSHIP AND THEY WA
... NT TO NOW CHARGE 4400.00 FOR THE TRANSMISSION. I AM OUT OF MONEY WITH THIS VEHICLE AND IT WAS CLEARLY POORLY MANUFACTURED. *TRRead more
Incident date: Apr 10, 2018
AFTER REPAIRING BRAKES AT MY COST MANY TIMES NOW THEY ARE RECALLED. I HAD TO REPLACE THE LINCOLN WHEELS AT MY COST AFTER RESEARCHING THAT MANY PROBLEMS WERE REPORTED. ALSO WITH ONLY 65,000 MILES ON MY CAR MY TRANSMISSION IS OUT. I HAVE HAD MANY ELECTRICAL ISSUES. IT IS CLEAR THAT MAJOR ISSUES IS ON THE THIS MODEL YEAR. WHILE DRIVING MY TRANSMISSION FAILED. I TOWED THE CAR TO DEALERSHIP AND THEY WA
... NT TO NOW CHARGE 4400.00 FOR THE TRANSMISSION. I AM OUT OF MONEY WITH THIS VEHICLE AND IT WAS CLEARLY POORLY MANUFACTURED. *TRRead more
Incident date: Apr 15, 2006
TL* THE CONTACT OWNS A 2006 LINCOLN ZEPHYR. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 19V904000 (SERVICE BRAKES, HYDRAULIC). THE CONTACT STATED THAT WHILE DRIVING 20 MPH IN THE SNOW THE BRAKE PEDAL WAS APPLIED BUT WAS SLOW TO RESPOND. THERE WERE NO WARNING LIGHTS ILLUMINATED. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE
... CONTACT CALLED THE LANDMARK LINCOLN LOCATED AT (5000 S BROADWAY, ENGLEWOOD, CO 80113, (303)761-1560, WHO CONFIRMED THAT THE PART WAS NOT YET AVAILABLE. THE VEHICLE WAS NOT DIAGNOSED NOR REPAIRED. THE CONTACT EXPERIENCED A FAILURE. THE MANUFACTURER WAS NOT CONTACTED. THE FAILURE MILEAGE WAS 93,000. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.Read more
Incident date: Feb 6, 2020
TL* THE CONTACT OWNED A 2007 LINCOLN MKZ. THE CONTACT STATED THAT WHILE GOING AROUND A CURVE AT 15 MPH, THE VEHICLE SLED ON SOME BLACK ICE AND LANDED IN A DITCH. THE FRONTAL DRIVER'S AND PASSENGER AIR BAGS DID NOT DEPLOY. THERE WERE NO INJURIES AND A POLICE REPORT WAS FILED. THE HOOD, BUMPER, FENDER, MIRROR AND THE UNDERCARRIAGE WERE DAMAGED. THE VEHICLE WAS TOTALED BY THE INSURANCE COMPANY AND T
... OWED AWAY FROM THE SCENE. THE DEALER AND MANUFACTURER WERE NOT CONTACTED YET. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 170,000.Read more
Crash
Incident date: Apr 11, 2020
WHILE DRIVING ON CITY STREETS, THE ENGINE UNEXPECTEDLY QUIT AND THE GEARS SWITCHED FROM DRIVE TO NEUTRAL ON ITS OWN. THIS HAS HAPPENED 5 TIMES SO FAR. IT IS DANGEROUS AND COULD BE LIFE THREATENING.
Incident date: Apr 11, 2020
WHILE DRIVING ON CITY STREETS, THE ENGINE UNEXPECTEDLY QUIT AND THE GEARS SWITCHED FROM DRIVE TO NEUTRAL ON ITS OWN. THIS HAS HAPPENED 5 TIMES SO FAR. IT IS DANGEROUS AND COULD BE LIFE THREATENING.
Incident date: Jan 12, 2020
THE TREAD SEPARATED FROM THE TIRE BODY ON A REPLACEMENT FIRESTONE TIRE. THE REPLACEMENT WAS MADE BY FIRESTONE BECAUSE OF A RECALL FOR THE SAME PROBLEM. THE TIRE HAD SEVERAL THOUSAND MILES ON IT SINCE IT WAS REPLACED. THE TREAD STARTED SEPARATING SEVERAL WEEKS BEFORE WE HAD IT REPLACED WITH A GOODYEAR TIRE.
Incident date: Mar 31, 2020
WHEN PULLING OUT OF DRIVEWAY THE FRONT PASSENGER DOOR OPENED. WASN'T ABLE TO LATCH THE DOOR. I HAD TO PUT A BUNGEE CORD TO KEEP DOOR FROM OPENING. THE CAR ISN'T SAFE TO DRIVE. THE VEHICLE WILL BE TOWED TO GET REPAIRED.
Incident date: Apr 4, 2020
ON APRIL 4TH, 2020. AFTER LEAVING THE FREEWAY AND MAKING A BRIEF STOPPED, A PASSENGER EXITED THE FRONT LEFT PASSENGER SIDES DOOR, AND ONCE THE PASSENGER REENTERED THE VEHICLE, THE DOOR WOULDN'T CLOSE, LATCH, OR LOCK. THE PASSENGER DOOR WILL BOUNCE BACK OPEN AFTER ATTEMPTING TO SHUT THE DOOR, THE DOOR REMAINED UNLOCKED AND THE LATCH WOULDN'T SWITCH TO THE LOCKED POSITION WHICH WOULD LOCK THE DOOR I
... N PLACE. THIS IS A HUGE SAFETY AND PRIVACY RISK, AS WE WOULD HAVE TO DRIVE HOLDING MANUALLY HOLDING THE DOOR SHUT, INCLUDING WHILE MAKING TURNS, DRIVING ON THE EXPRESSWAY, AND WHILE DRIVING IN VARIOUS DRIVING CONDITIONS. THIS IS INCREDIBLY DANGEROUS, ESPECIALLY IN LIMITED VISIBILITY, OR DURING DANGEROUS CONDITIONS SUCH AS SNOW, STORMS, AND ETC... THIS ALSO POSED A HUGE PRIVACY RISK, SINCE THE DOOR REMAINS OPEN AND UNLOCKED WITHOUT ANY WAY TO SECURELY CLOSE AND LOCK THE DOOR, ANY INDIVIDUAL CAN EASILY STEAL YOUR VEHICLE BY ENTERING THE UNLOCKED AND OPEN PASSENGER DOOR SIDE AND HOTWIRE THE CAR. THIS ALSO DRAINS THE BATTERY SINCE THE CAR IS TRYING TO ALERT THE OWNER THAT THE PASSENGER DOOR REMAINS OPEN. TO MY DISMAY, THIS VEHICLE AND YEAR (2013 LINCOLN MKZ) WAS INVOLVED IN A RECALL IN 2015 FOR THE SAME EXACT REASON, THE DEALERSHIP SEARCHED MY VIN, AND DIDN'T FIND A RECALL ON THE VEHICLE. FORD AND LINCOLN REFUSED TO WORK WITH ME ON THE PRICE OR ANYTHING, DESPITE LITERALLY THIS SAME MODEL HAVING A RECALL FOR THE SAME EXACT ISSUE THAT THE RECALLED 2013 LINCOLN MKZ MODELS HAD. THE ISSUE FOR THE FIRST RECALL WAS CAUSED BY A BROKEN SPRAWL TAB, WHICH A LOCAL MECHANIC LITERALLY DIAGNOSED. THE ISSUE LITERALLY HAPPENS WHILE STATIONARY, IN MOTION, ON A CITY STREET, AND HIGHWAY. THIS IS INCREDIBLY INFURIATING AND HAS CAUSED A $460 PRICE TAG ATTACHED TO THE REPAIRS FOR ONLY ONE DOOR, WHILE THE RECALL REPLACED ALL FOUR FOR FREE!Read more
Incident date: Apr 1, 2020
HOOD DOES NOT CLOSE PROPERLY AFTER OPENING. IT SEEMS THAT THE LATCH IS MISALIGNED. *TR
Incident date: Jun 24, 2019
TL* THE CONTACT OWNS A 2007 LINCOLN MKX. THE CONTACT STATED THAT THERE WAS AN ABNORMAL FUEL ODOR PRESENT OUTSIDE OF THE VEHICLE. THE CONTACT STATED THAT THERE WAS EVIDENCE OF A FUEL LEAK COMING FROM THE FUEL TANK. THE VEHICLE WAS PREVIOUSLY TAKEN TO BEAMAN FORD INC (1717 TENNESSEE 46, DICKSON, TN 37055), WHERE IT WAS DETERMINED THAT THE FUEL TANK NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED
... . THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 140,000.Read more
Incident date: Jun 24, 2019
TL* THE CONTACT OWNS A 2007 LINCOLN MKX. THE CONTACT STATED THAT THERE WAS AN ABNORMAL FUEL ODOR PRESENT OUTSIDE OF THE VEHICLE. THE CONTACT STATED THAT THERE WAS EVIDENCE OF A FUEL LEAK COMING FROM THE FUEL TANK. THE VEHICLE WAS PREVIOUSLY TAKEN TO BEAMAN FORD INC (1717 TENNESSEE 46, DICKSON, TN 37055), WHERE IT WAS DETERMINED THAT THE FUEL TANK NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED
... . THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 140,000.Read more