Showing 18,739 complaints for LINCOLN
Incident date: Apr 25, 2010
I HAVE A 2004 LINCOLN LS THAT STARTED TO RUN ROUGH SO I REPLACED THE AIR FILTER. THIS DID NOT HELP SO NEXT I REPLACED THE SPARK PLUGS. THIS DID NOT HELP. THE THINGS THAT I HAVE DONE UP TO THIS POINT STARTED BECAUSE MY CAR STARTED MISSING AND RUNNING ROUGH HOWEVER I HAVE FOUND OUT THAT IT WAS JUST THE BEGINNING OF A BIGGER PROBLEM IN THAT THE CAR WAS AND IS PUMPING GAS INTO THE ENGINE AND AIR INTA
... KE TO THE POINT THAT IT IS COMING OUT OF THE EXHAUST SYSTEM IN AN AMOUNT THAT CAUSES A STEADY STREAM AND IT POOLS UNDER THE CAR. THE INTAKE FILLS WITH FUEL TO THE POINT THAT THE AIR FILTER GETS SOAKED IN GAS AND I HAVE TO TAKE IT OFF AND DUMP IT OUT. THIS HAS BEEN GOING ON FOR 3 WEEKS NOW AND I AM AFRAID TO DRIVE IT. THE CAR HAS FUEL INJECTORS??? THE COMPANY AND THE DEALER HAVE TOLD ME TO BRING IT TO THEM AND THEY WILL FIX IT HOWEVER I WILL HAVE TO PAY FOR IT. EVERYTHING ON THE CAR IS CONTROLLED MY COMPUTERS EVEN THE GAS FLOW AND PEDAL THAT CONTROLS HOW FAST I GO. TO ME THAT IS WRONG. *TRRead more
Incident date: May 1, 2010
2006 LINCOLN NAVIGATOR, 50,000 MILES ON CAR. CAR SHUT DOWN AFTER GIVING AN ENGINE SAFETY MODE ERROR ON DASH WHILE ON FOUR LANE BUSY HIGHWAY TRAVELING 40-45 MPH. COASTED TO SIDE OF ROAD (NO BERM AVAILABLE). CARS RACING BY. WAITED 5 MINUTES. RESTARTED CAR AND LIMPED INTO TEAM FORD OF MARIETTA GEORGIA DEALER. I WAS TOLD THE THROTTLE CONTROL BODY & MOTOR ASY #8L3Z*9E926*A WAS BAD AND WAS NOT COVE
... RED UNDER THE $1,000 EXTENDED WARRANTY I PURCHASED ON THE CAR IN 2006. REPAIR BILL WAS $800 OUT OF POCKET. CHECKED ONLINE AND THIS IS A KNOWN ISSUE FOR FORD EXPEDITIONS & LINCOLN NAVIGATOR ENGINES AND YET FORD DOES NOTHING TO FIX. DOES SOMEONE HAVE TO DIE TO GET FORD TO REPAIR THESE DEFECTIVE PARTS? NOTHING MORE DANGEROUS THAN A CAR THAT SHUTS DOWN IN HEAVY TRAFFIC TRAVELING AT HIGH SPEEDS. *TRRead more
Incident date: Feb 10, 2010
TL* THE CONTACT OWNS A 2000 LINCOLN LS. WHILE DRIVING AT SPEEDS OF 50 MPH, THERE WAS A LOUD, UNUSUAL RATTLING NOISE COMING FROM UNDER THE VEHICLE. THE DEALER ADVISED THE STEERING AND BALL JOINTS WERE DEFECTIVE AND WOULD NEED TO BE REPLACED. THE MANUFACTURER ADVISED THERE WERE NO RECALLS FOR THE VEHICLE AND WOULD NOT PROVIDE ANY ASSISTANCE. THE CONTACT WAS CONCERNED THAT IF THE BALL JOINTS WERE TO
... SEPARATE, THE WHEEL WOULD FRACTURE FROM THE VEHICLE AND COULD POTENTIALLY CAUSE A CRASH. THE FAILURE AND CURRENT MILEAGES WERE 120,000.Read more
Incident date: Feb 10, 2010
TL* THE CONTACT OWNS A 2000 LINCOLN LS. WHILE DRIVING AT SPEEDS OF 50 MPH, THERE WAS A LOUD, UNUSUAL RATTLING NOISE COMING FROM UNDER THE VEHICLE. THE DEALER ADVISED THE STEERING AND BALL JOINTS WERE DEFECTIVE AND WOULD NEED TO BE REPLACED. THE MANUFACTURER ADVISED THERE WERE NO RECALLS FOR THE VEHICLE AND WOULD NOT PROVIDE ANY ASSISTANCE. THE CONTACT WAS CONCERNED THAT IF THE BALL JOINTS WERE TO
... SEPARATE, THE WHEEL WOULD FRACTURE FROM THE VEHICLE AND COULD POTENTIALLY CAUSE A CRASH. THE FAILURE AND CURRENT MILEAGES WERE 120,000.Read more
Incident date: Mar 6, 2010
FORD'S PLASTIC INTAKE MANIFOLD IS CRACKED. IS THERE ANY RECOURSE STILL AVAILABLE FOR THIS PROBLEM? THE MANIFOLD IS STILL ON THE CAR AND NOW LEAKING. *TR
Incident date: Jun 29, 2009
WE HAD A SUDDEN UNINTENDED ACCELERATION OF OUR CAR. WE WERE TRAVELING WEST ON THE NEW YORK STATE THRUWAY (I-90) TOWARDS NIAGARA FALLS. AS WE EXITED INTO A REST AREA, SUDDENLY THE ENGINE RACED AS IF THE GAS PEDAL WERE FLOORED. THE DRIVER PRESSED ON THE BRAKE VERY VERY HARD, AND THE CAR ALMOST STOPPED, MOVING FORWARD SLOWLY. THE DRIVER THEN SHIFTED INTO NEUTRAL, AND THE ENGINE SLOWEDAND WE STOPP
... ED--ABOUT 50 FEET BEYOND WHERE THE SUDDEN UNINTENDED ACCELERATION STARTED. WE TURNED THE ENGINE OFF, AND EXAMINED THE FLOORMAT--IT WAS NOT IN A POSITION TO PRESS THE GAS PEDAL. WE CHECKED UNDER THE HOOD, AND DID NOT FIND ANYTHING THAT SEEMED RELATED TO CAUSING THE SUDDEN UNINTENDED ACCELERATION. WE LATER CHECKED IF THE DRIVER COULD PRESS THE GAS AND BRAKE PEDALS AT THE SAME TIME, BUT ON OUR CAR THEY ARE SO FAR APART THAT THIS IS NOT POSSIBLE. WE THINK IT IS POSSIBLE THAT THIS OCCURRENCE WAS DUE TO INADEQUATE SHIELDING, AND INADEQUATE PROGRAMMING, OF THE GAS PEDAL COMPUTER WHICH SENDS SIGNALS TO THE ACCELERATION SYSTEM. AT THE TIME OF THE INCIDENT, WE HAD A GPS, CELL PHONES, AND GAME MACHINES IN OPERATION, AND THE REST AREA WE WERE PULLING INTO HAD WIFI. THUS, THE ACCELERATION SYSTEM COMPUTER WAS RECEIVING MANY SIGNALS FROM "NOISE." IF THEY CAME IN A CERTAIN SEQUENCE, IT WOULD CAUSE AN SUA, UNLESS THE CAR HAD ADEQUATE CODING TO PREVENT THAT OCCURRENCE. THE FIX FOR THIS WOULD BE TO EITHER HARD WIRE THE GAS PEDAL, OR TO PUT ADEQUATE PROGRAMMING TO PREVENT STRAY SIGNALS FROM BEING ACCEPTED. WE WOULD LIKE TO SEE ONE OF THESE FIXES IMPLEMENTED. *TRRead more
Incident date: Jun 29, 2009
WE HAD A SUDDEN UNINTENDED ACCELERATION OF OUR CAR. WE WERE TRAVELING WEST ON THE NEW YORK STATE THRUWAY (I-90) TOWARDS NIAGARA FALLS. AS WE EXITED INTO A REST AREA, SUDDENLY THE ENGINE RACED AS IF THE GAS PEDAL WERE FLOORED. THE DRIVER PRESSED ON THE BRAKE VERY VERY HARD, AND THE CAR ALMOST STOPPED, MOVING FORWARD SLOWLY. THE DRIVER THEN SHIFTED INTO NEUTRAL, AND THE ENGINE SLOWEDAND WE STOPP
... ED--ABOUT 50 FEET BEYOND WHERE THE SUDDEN UNINTENDED ACCELERATION STARTED. WE TURNED THE ENGINE OFF, AND EXAMINED THE FLOORMAT--IT WAS NOT IN A POSITION TO PRESS THE GAS PEDAL. WE CHECKED UNDER THE HOOD, AND DID NOT FIND ANYTHING THAT SEEMED RELATED TO CAUSING THE SUDDEN UNINTENDED ACCELERATION. WE LATER CHECKED IF THE DRIVER COULD PRESS THE GAS AND BRAKE PEDALS AT THE SAME TIME, BUT ON OUR CAR THEY ARE SO FAR APART THAT THIS IS NOT POSSIBLE. WE THINK IT IS POSSIBLE THAT THIS OCCURRENCE WAS DUE TO INADEQUATE SHIELDING, AND INADEQUATE PROGRAMMING, OF THE GAS PEDAL COMPUTER WHICH SENDS SIGNALS TO THE ACCELERATION SYSTEM. AT THE TIME OF THE INCIDENT, WE HAD A GPS, CELL PHONES, AND GAME MACHINES IN OPERATION, AND THE REST AREA WE WERE PULLING INTO HAD WIFI. THUS, THE ACCELERATION SYSTEM COMPUTER WAS RECEIVING MANY SIGNALS FROM "NOISE." IF THEY CAME IN A CERTAIN SEQUENCE, IT WOULD CAUSE AN SUA, UNLESS THE CAR HAD ADEQUATE CODING TO PREVENT THAT OCCURRENCE. THE FIX FOR THIS WOULD BE TO EITHER HARD WIRE THE GAS PEDAL, OR TO PUT ADEQUATE PROGRAMMING TO PREVENT STRAY SIGNALS FROM BEING ACCEPTED. WE WOULD LIKE TO SEE ONE OF THESE FIXES IMPLEMENTED. *TRRead more
Incident date: May 3, 2010
LINCOLN LS TRANSMISSION SHOWING E AND DRIVING ROUGH. *TR
Incident date: Apr 30, 2010
I WAS DRIVING 62 MPH IN CRUISE AND DECIDED I WANTED TO GO 70 MPH. I THEN PROCEEDED TO HOLD DOWN THE "SET +" BUTTON UNTIL MY SPEED REACHED 70 AT WHICH POINT I RELEASED THE BUTTON. TO MY SURPRISE THE VEHICLE ACCELERATED TO 95 MPH AND HELD THAT SPEED. I THEN SLOWED THE CAR WITH MY BRAKES TO 65 AND AGAIN HELD THE "SET+" BUTTON UNTIL I REACHED 70MPH. THIS TIME THE VEHICLE ACCELERATED TO 80MPH AND HELD
... THIS SPEED. *TRRead more
Incident date: Apr 25, 2010
WHENEVER THE CAR IS WASHED OR IF IT SNOWS OR RAINS THE CAR EXPERIENCES SPONTANEOUS ELECTRICAL ACTIVITY WHEN NO KEY OR PERSON IS PRESENT USING ANY ASPECT OF THE VEHICLE. FOR EXAMPLE, AFTER WASHING THE CAR, THE VEHICLE WILL DRIVE PERFECTLY FINE, BUT UPON BEING PARKED, SOMETIMES HOURS AFTER BEING PARKED, THE VEHICLE WILL THEN BE OBSERVED TRIGGERING POWER SEATS, AIRBAG WARNING LIGHTS, AND CLICKING
... SOUNDS CAN BE HEARD. THE VEHICLE HAS HAD A POWER WINDOW MOTOR BURN OUT AND A WIRING HARNESS RELATED TO THE POWER SEATS CORRODE AND FAIL COSTING OVER $700 IN REPAIRS. WE BELIEVE THE REASON FOR THESE PROBLEMS IS DUE TO THE WINDSHIELD LEAKING ON TO SOME KIND OF ELECTRONIC CONTROL DEVICE SUCH AS THE GEM MODULE AND THEN CAUSING THE DEVICE TO SHORT CIRCUIT AND TRIGGER VARIOUS ELECTRONIC LIGHTS/SWITCHES. MORE RECENTLY, THE VEHICLE WAS LEFT OUTSIDE FOR TWO WEEKS WITH NO USE AND SEVERAL FEET OF SNOW FELL ALONG WITH SOME RAIN AND THE VEHICLE'S BATTERY IS NOW COMPLETELY DISCHARGED DUE TO THE ELECTRONIC PROBLEMS/MOISTURE LEAKAGE. *TRRead more
Incident date: Apr 2, 2010
MY LINCOLN LS 2005 WAS DOING FINE THAN 53000 MILES HITS THAT'S NOTHING ON VEHICLES AND. MY TRANSMISSION IS JUMPING GEARS FOUR AND FIVE ARE HORRIBLE I CANT EXCEED 55MPH ..ID UNDERSTAND ON A VEHICLE THAT HAS 160000 MILES BUT I MEAN 53000 GIVE ME A FINANCIAL BREAK. I BOUGHT THIS CAR THINKING NICE SHAPE MINT CONDITION BUT NEVER DID I REALIZE NOR READ UP THAT THESE THINGS GIVE OUT AND THAT THE TRANSMIS
... SION HAVE HAD ALL KINDS OF DIFFICULTIES..THESE NEED TO BE RECALLED INSTEAD OF 100S OF LINCOLN LS OWNERS TO BE HANDED ANOTHER FINANCIAL BURDEN..HELP US OUT YOU ALL MAKE A KILLING ANYHOW. PUT YOURSELVES IN OUR SHOES... *TRRead more
Incident date: Apr 23, 2010
TL*THE CONTACT OWNS A 2003 LINCOLN AVIATOR. WHILE SHIFTING INTO PARK, THE SHIFTER LEVER BROKE. THE VEHICLE HAD NOT BEEN REPAIRED AT THE TIME OF THE COMPLAINT BUT THE CONTACT PLANNED TO HAVE IT TOWED TO AN AUTHORIZED DEALERSHIP. THE FAILURE AND MILEAGE WAS 127,467.
Incident date: Jan 1, 2010
I HAVE HAD MY 2004 LINCOLN LS IN THE SHOP AT MY LOCAL FORD DEALERSHIP ON NUMEROUS OCCASIONS. STARTING AT AROUND 80,000 MILES ON IT, I HAD A VARIETY OF PROBLEMS ON IT WHICH COST ME SEVERAL THOUSAND DOLLARS. BUT MOST RECENTLY AND THE BIGGEST PROBLEM THAT I HAVE NOW IS WITH IT RUNNING HOT. AS A MATTER OF FACT, THIS IS MY 5TH TIME TAKEN TO THE SHOP FOR THIS SAME PROBLEM. THEY REPLACED MY THERMOSTAT F
... OR $200, NEXT TRIP THEY REPLACED MY COOLANT RESERVOIR $200, 3RD TRIP THEY REPLACED AN 0 RING $310 AND NOW IT'S IN THERE RIGHT NOW WHICH THE SAME PROBLEM. I HAVE TALKED TO THE GUYS IN THE SHOP AND THEY TELL ME THEY HAVE SEEN A TON OF PROBLEMS WITH THESE LS'S AND HAVE ALSO TALKED TO SEVERAL PEOPLE AROUND TOWN THAT HAVE HAD BAD EXPERIENCES AND PROBLEMS WITH THESE LS'S ALSO. WHICH LEADS ME TO BELIEVE THAT THERE IS PROBABLY A TON OF OTHER COMPLAINTS OUT THERE AS WELL. I BELIEVE THESE CARS ARE POORLY BUILT AND FOR THE MONEY THAT THEY COST, THEY SHOULD BE ALOT MORE DEPENDABLE THAN THIS. US LINCOLN OWNERS NEED SOME HELP WITH GETTING SOME RECALLS DONE ON ALOT OF THESE PROBLEMS. FORD MADE A TON OF MONEY ON THESE CARS WHEN THEY WERE SOLD. MINE COST $45,900 NEW AND THIS IS RIDICULOUS. *TRRead more
Incident date: Jan 16, 2010
TL*THE CONTACT OWNS A 2003 LINCOLN AVIATOR. WHILE DRIVING AT ANY SPEED, THE VEHICLE SUDDENLY LOST POWER. THE CONTACT CALLED THE MANUFACTURER AND WAS INFORMED ABOUT RECALL 02V313000 (POWERTRAIN: AUTOMATIC TRANSMISSION) WHICH CITED THE SAME FAILURE AS THE ONE THE CONTACT EXPERIENCED. HOWEVER, THE CONTACT WAS INFORMED THAT HER VEHICLE WAS NOT INCLUDED IN THE RECALL. THE VEHICLE HAD NOT BEEN REPAIRED
... AT THE TIME OF THE COMPLAINT. THE CURRENT MILEAGE WAS APPROXIMATELY 73,250. THE FAILURE MILEAGE WAS APPROXIMATELY 73,150. UPDATED 06/21/10 *BF UPDATED 06/24/10.*JBRead more
Incident date: Apr 19, 2010
TL*THE CONTACT OWNS A 1997 LINCOLN TOWN CAR. WHILE DRIVING AT 2 MPH, THE CONTACT HEARD A LOUD SOUND. SECONDS LATER, THE FRONT END OF THE VEHICLE SUDDENLY FELL TO THE GROUND. AFTER INSPECTING THE VEHICLE, THE CONTACT NOTICED THAT THE FRONT DRIVER SIDE BALL JOINT HAD SEPARATED FROM THE VEHICLE. A FEW WEEKS PRIOR TO THE FAILURE, THE CONTACT NOTICED THAT THE VEHICLE MADE A CREAKING SOUND WHENEVER OPER
... ATED. THE CONTACT CALLED THE DEALERSHIP AND WAS INFORMED THAT RECALL 98V322000 (SUSPENSION: FRONT: CONTROL ARM: LOWER BALL JOINT) DID NOT INCLUDE HIS VEHICLE. THE VEHICLE HAD NOT BEEN REPAIRED AT THE TIME OF THE COMPLAINT. THE CURRENT AND FAILURE MILEAGES WERE APPROXIMATELY 175,000.Read more
Incident date: Apr 18, 2010
2006 LINCOLN MARK LT WENT INTO "ENGINE FAILSAFE MODE" FOR NO REASON. THIS CREATED A VERY DANGEROUS CONDITION WITH THE TRUCK GOING INTO AN IDLE. PULLED TRUCK OVER AND RESTARTED ENGINE. *TR
Incident date: Apr 24, 2010
TL*THE CONTACT OWNS A 2003 LINCOLN TOWN CAR. WHILE DRIVING APPROXIMATELY 5 MPH, THE AXLE SHAFT SUDDENLY CRACKED. THE CONTACT COASTED THE VEHICLE ONTO THE EMERGENCY LANE. THE VEHICLE WAS TOWED TO AN AUTHORIZED DEALER. THE CONTACT REFERENCED RECALL 04V328000 (SUSPENSION: REAR). THE DEALER STATED THAT THE FAILURE WAS IDENTICAL TO THE RECALL; HOWEVER, THE MANUFACTURER STATED THAT HIS VIN WAS NOT INC
... LUDED. THE MANUFACTURER OFFERED HIM A 20% DISCOUNT OFF OF THE REPAIR EXPENSES. THE CURRENT AND FAILURE MILEAGES WERE 54,230.Read more
Incident date: Apr 7, 2010
I OWN A 2006 LINCOLN TOWN CAR, PURCHASED NEW. APPROXIMATELY ONCE OR TWICE PER YEAR THE VEHICLE WILL TRY TO ACCELERATE AS I AM BRAKING FOR A RED LIGHT OR A STOP SIGN. PLACING TRANSMISSION INTO NEUTRAL POSITION SEEMS TO RESULT IN ENGINE SLOWING DOWN. TAKEN TO LINCOLN-MERCURY DEALERSHIP IN 3/07 AND 4/10. THEY CAN NOT DUPLICATE THE PROBLEM AND THEY STATE THAT THEY CAN NOT EXPLAIN WHAT IS CAUSING THIS.
... *TRRead more
Incident date: Apr 7, 2010
I OWN A 2006 LINCOLN TOWN CAR, PURCHASED NEW. APPROXIMATELY ONCE OR TWICE PER YEAR THE VEHICLE WILL TRY TO ACCELERATE AS I AM BRAKING FOR A RED LIGHT OR A STOP SIGN. PLACING TRANSMISSION INTO NEUTRAL POSITION SEEMS TO RESULT IN ENGINE SLOWING DOWN. TAKEN TO LINCOLN-MERCURY DEALERSHIP IN 3/07 AND 4/10. THEY CAN NOT DUPLICATE THE PROBLEM AND THEY STATE THAT THEY CAN NOT EXPLAIN WHAT IS CAUSING THIS.
... *TRRead more
Incident date: Nov 19, 2009
2005 LINCOLN AVIATOR HAS CRACK IN REAR APPLIQUE PANEL. THIS CRACK OCCURRED WITH NO ACCIDENT JUST APPEARED AFTER A FROST. THIS PROBLEM WAS RELAYED TO FORD? LINCOLN HOME OFFICE BUT NOTHING WAS DONE TO REPAIR THE PROBLEM BY FORD. THE LEAK WILL DESTROY THE INSIDE PANEL AND WILL EVENTUALLY ROT THE BACK TAILGATE. *TR
Incident date: Oct 1, 2009
TL* THE CONTACT OWNS A 2007 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 40 TO 45 MPH DOWN A RAMP, HE ENGAGED THE BRAKES AND THE VEHICLE ABNORMALLY ACCELERATED. HE CONTINUED TO ENGAGE THE BRAKES USING BOTH FEET TO AVOID A POTENTIAL CRASH. HE WAS ABLE TO BRING SLOW THE VEHICLE DOWN AND DRIVE ONTO AN EMERGENCY LANE. THE CONTACT STATED THAT THE VEHICLE HAD BEEN TAKEN TO THE D
... EALER SEVERAL TIMES REGARDING THE FAILURE. THE DEALER WAS UNABLE TO DUPLICATE THE FAILURE. THE MANUFACTURER WAS CONTACTED AND REFERRED HIM BACK TO THE DEALER WHERE A MONITOR EQUIPPED WITH A KILL SWITCH WAS INSTALLED ON THE VEHICLE. THE CONTACT STATED THAT THE FAILURE DID NOT PERSIST AND THE MONITOR WAS REMOVED FROM THE VEHICLE. THE APPROXIMATE FAILURE MILEAGE WAS 37,000 AND THE CURRENT MILEAGE WAS 46,500.Read more
Incident date: Jan 28, 2010
WHEELS CORRODING CAUSING TIRE TO DEFLATE. *TR
Incident date: Dec 18, 2008
TL*THE CONTACT OWNS A 2004 LINCOLN NAVIGATOR. THE FRONT STRUTS BROKE AND THE FRONT END OF THE VEHICLE FELL DOWN, ALMOST TOUCHING THE GROUND. THERE WAS BARELY ANY SUSPENSION WHEN THE CONTACT DROVE TO AN AUTHORIZED DEALERSHIP; THE DEALER REPLACED THE FRONT STRUTS. THE CONTACT CALLED THE MANUFACTURER AND WAS INFORMED THAT THERE WERE NO RECALLS OR WARRANTY'S ON THE VEHICLE. THE FAILURE MILEAGE WAS APP
... ROXIMATELY 63,000. THE CURRENT MILEAGE IS APPROXIMATELY 70,000. UPDATED 10/28/10 *BF THE CONSUMER WAS INFORMED BY FORD, IT WAS A KNOWN PROBLEM AND THEY INCREASED THEIR WAREHOUSE SUPPLY IN ARIZONA T MEET THE DEMAND. UPDATED 11/01/10Read more
Incident date: Apr 2, 2010
FUSE/RELAY FUSES GET BURNED ONCE EVERY TWO DAYS THE SUV TURNS OFF WHILE IN MOTION. ALMOST CAUSED AN ACCIDENT IN A HEAVY TRAFFIC INTERSECTION. HAS HAPPENED FOR 5-6 TIMES. TOOK THE SUV TO AN ELECTRICIAN FOUND NO PROBLEM, CALLED FORD DEALER APPOINTMENT IN TWO WEEKS. *TR
Incident date: Feb 27, 2010
2004 LINCOLN TOWN CAR PURCHASED NEW FROM DEALER WITH DEFECTIVE WHEEL BEARINGS. WHEN WE PURCHASED THE CAR IT HAD LOUD CABIN NOISE, THE DEALER INFORMED US THAT THE OUTSIDE NOISE WAS CAUSED BY THE REAR WINDOW AND A SPECIALIST WAS BROUGHT IN TWO DAYS LATER TO ALIGN THE WINDOW. CABIN NOISE CONTINUED UNTIL THE BEARINGS GAVE OUT AT 98,709 MILES. AS PER THE WINDOW THAT WAS ALIGN, IT IS NOW THE ONLY WI
... NDOW THAT YOU CAN OPEN BUT NOT CLOSE. *TRRead more
Incident date: Feb 27, 2010
2004 LINCOLN TOWN CAR PURCHASED NEW FROM DEALER WITH DEFECTIVE WHEEL BEARINGS. WHEN WE PURCHASED THE CAR IT HAD LOUD CABIN NOISE, THE DEALER INFORMED US THAT THE OUTSIDE NOISE WAS CAUSED BY THE REAR WINDOW AND A SPECIALIST WAS BROUGHT IN TWO DAYS LATER TO ALIGN THE WINDOW. CABIN NOISE CONTINUED UNTIL THE BEARINGS GAVE OUT AT 98,709 MILES. AS PER THE WINDOW THAT WAS ALIGN, IT IS NOW THE ONLY WI
... NDOW THAT YOU CAN OPEN BUT NOT CLOSE. *TRRead more
Incident date: Feb 27, 2010
2004 LINCOLN TOWN CAR PURCHASED NEW FROM DEALER WITH DEFECTIVE WHEEL BEARINGS. WHEN WE PURCHASED THE CAR IT HAD LOUD CABIN NOISE, THE DEALER INFORMED US THAT THE OUTSIDE NOISE WAS CAUSED BY THE REAR WINDOW AND A SPECIALIST WAS BROUGHT IN TWO DAYS LATER TO ALIGN THE WINDOW. CABIN NOISE CONTINUED UNTIL THE BEARINGS GAVE OUT AT 98,709 MILES. AS PER THE WINDOW THAT WAS ALIGN, IT IS NOW THE ONLY WI
... NDOW THAT YOU CAN OPEN BUT NOT CLOSE. *TRRead more
Incident date: Jan 1, 1901
2007 LINCOLN TOWN CAR ACCELERATION. THE CONSUMERS WIFE WAS APPROACHING A TRAFFIC SIGNAL, WHEN SUDDENLY THE ENGINE REVVED EXTREMELY HIGH AS SHE WAS ATTEMPTING TO APPLY THE BRAKE TO COME TO A NORMAL STOP. AS THE ENGINE WAS OUT OF CONTROL AND THE BRAKING SYSTEM WAS NOT SUFFICIENT TO STOP, SHE QUICKLY PLACED THE GEAR INTO NEUTRAL. AFTER SHIFTING TO NEUTRAL, THE BRAKES WERE SUFFICIENT WITH ONLY
... A FEW INCHES TO SPARE AVOIDING A SERIOUS COLLISION. THE VEHICLE CONTINUED RUNNING AT A HIGH RATE DURING THE WAIT. THE CONSUMER TOOK THE VEHICLE TO THE DEALER, BUT THEY WERE UNABLE TO FIND ANY PROBLEMS. *JB UPDATED 04/12/11Read more
Incident date: Jan 1, 1901
2000 LINCOLN LS. CONSUMER STATES PROBLEM WITH A SENSOR. *TGW THE CONSUMER STATED A DIAGNOSTIC TROUBLE CODE WAS FOUND FOR THE DRIVER SIDE AND PASSENGER SIDE AIR BAGS. THE MECHANIC LOOK UP THE CODE AND FOUND TSB 02-12-7 WHICH HE STATED HAD A BROKEN CIRCUIT IN THE CONNECTOR AND PIGTAIL UNDER THE SEAT. FORD STATED THEY WOULD NOT PAY FOR THE REPAIRS, AS IT WAS ONLY GOOD FOR 5 YEARS. *JB
Incident date: May 26, 2009
TL*THE CONTACT OWNS A 2006 LINCOLN NAVIGATOR. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH, THE VEHICLE SUDDENLY STALLED AND CRASHED INTO THE REAR OF ANOTHER VEHICLE. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALERSHIP FOR A DIAGNOSTIC TEST BUT THE DEALER COULD FIND NO PROBLEMS. ANOTHER DEALER INFORMED THE CONTACT THAT THE POWER STEERING, TRANSMISSION AND ENGINE NEEDED TO BE REPAIRE
... D AS THE STEERING ALSO MALFUNCTIONED. THE FAILURE MILEAGE WAS APPROXIMATELY 12,000. THE CURRENT MILEAGE WAS APPROXIMATELY 42,000.Read more
Incident date: May 26, 2009
TL*THE CONTACT OWNS A 2006 LINCOLN NAVIGATOR. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH, THE VEHICLE SUDDENLY STALLED AND CRASHED INTO THE REAR OF ANOTHER VEHICLE. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALERSHIP FOR A DIAGNOSTIC TEST BUT THE DEALER COULD FIND NO PROBLEMS. ANOTHER DEALER INFORMED THE CONTACT THAT THE POWER STEERING, TRANSMISSION AND ENGINE NEEDED TO BE REPAIRE
... D AS THE STEERING ALSO MALFUNCTIONED. THE FAILURE MILEAGE WAS APPROXIMATELY 12,000. THE CURRENT MILEAGE WAS APPROXIMATELY 42,000.Read more
Incident date: May 26, 2009
TL*THE CONTACT OWNS A 2006 LINCOLN NAVIGATOR. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH, THE VEHICLE SUDDENLY STALLED AND CRASHED INTO THE REAR OF ANOTHER VEHICLE. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALERSHIP FOR A DIAGNOSTIC TEST BUT THE DEALER COULD FIND NO PROBLEMS. ANOTHER DEALER INFORMED THE CONTACT THAT THE POWER STEERING, TRANSMISSION AND ENGINE NEEDED TO BE REPAIRE
... D AS THE STEERING ALSO MALFUNCTIONED. THE FAILURE MILEAGE WAS APPROXIMATELY 12,000. THE CURRENT MILEAGE WAS APPROXIMATELY 42,000.Read more
Incident date: Apr 11, 2001
2001 LINCOLN LS--FRONT PASSENGER WHEEL- THERE WAS ALOT OF SQUEAKING NOISES COMING FROM THE WHEEL BEFORE INCIDENT OCCURRED. YESTERDAY, GOING THROUGH A DRIVE-THRU, I HEARD A POP. I GOT OUT AND INSPECTED THE VEHICLE. THE FENDER WAS RESTING ON THE TIRE. I CALLED A TOW TRUCK AND AS HE WAS TRYING TO PUT THE CAR ON THE TOW TRUCK, HE SHOWED ME THE DAMAGE. THE BOLT THAT HOLDS THE BALL JOINT AND CONTROL A
... RM TO THE WHEEL CAME OFF. PLEASE INVESTIGATE THIS FOR ME, AND CONTACT ME WHEN YOU FIND SOMETHING OUT! THX *TRRead more
Incident date: Apr 11, 2001
2001 LINCOLN LS--FRONT PASSENGER WHEEL- THERE WAS ALOT OF SQUEAKING NOISES COMING FROM THE WHEEL BEFORE INCIDENT OCCURRED. YESTERDAY, GOING THROUGH A DRIVE-THRU, I HEARD A POP. I GOT OUT AND INSPECTED THE VEHICLE. THE FENDER WAS RESTING ON THE TIRE. I CALLED A TOW TRUCK AND AS HE WAS TRYING TO PUT THE CAR ON THE TOW TRUCK, HE SHOWED ME THE DAMAGE. THE BOLT THAT HOLDS THE BALL JOINT AND CONTROL A
... RM TO THE WHEEL CAME OFF. PLEASE INVESTIGATE THIS FOR ME, AND CONTACT ME WHEN YOU FIND SOMETHING OUT! THX *TRRead more
Incident date: Apr 11, 2001
2001 LINCOLN LS--FRONT PASSENGER WHEEL- THERE WAS ALOT OF SQUEAKING NOISES COMING FROM THE WHEEL BEFORE INCIDENT OCCURRED. YESTERDAY, GOING THROUGH A DRIVE-THRU, I HEARD A POP. I GOT OUT AND INSPECTED THE VEHICLE. THE FENDER WAS RESTING ON THE TIRE. I CALLED A TOW TRUCK AND AS HE WAS TRYING TO PUT THE CAR ON THE TOW TRUCK, HE SHOWED ME THE DAMAGE. THE BOLT THAT HOLDS THE BALL JOINT AND CONTROL A
... RM TO THE WHEEL CAME OFF. PLEASE INVESTIGATE THIS FOR ME, AND CONTACT ME WHEN YOU FIND SOMETHING OUT! THX *TRRead more
Incident date: Apr 9, 2010
TL*THE CONTACT OWNS A 2009 LINCOLN TOWN CAR. WHILE THE CONTACT WAS DRIVING 45 MPH THE BRAKE PEDAL WAS ENGAGED, FOLLOWED BY AN UNINTENDED ACCELERATION AND THE SPEED INCREASED TO APPROXIMATELY 70 MPH. THE GEAR WAS SHIFTED FROM DRIVE TO NEUTRAL AND THE VEHICLE WAS ABLE TO SLOW DOWN. THE VEHICLE HAD NOT BEEN REPAIRED AT THE TIME OF THE COMPLAINT. THE FAILURE MILEAGE WAS 10,000. THE CURRENT MILEAGE WAS
... 10,500. UPDATED 06/08/10.*LJ UPDATED 07/12/10*JBRead more
Incident date: Apr 7, 2010
TL*THE CONTACT OWNS A 1999 LINCOLN TOWN CAR. THE CONTACT WAS DRIVING APPROXIMATELY 3 MPH IN A PARKING LOT. THE LOWER BALL JOINTS DETACHED WITHOUT WARNING. THE VEHICLE WAS TOWED TO AN AUTHORIZED DEALER. A RECALL REPAIR WAS PERFORMED UNDER NHTSA CAMPAIGN ID NUMBER 098V322000 (SUSPENSION: FRONT: CONTROL ARM: LOWER BALL JOINT). THE FAILURE MILEAGE WAS 75,397. THE CURRENT MILEAGE WAS 75,412. UPDAT
... ED 6/1/10 *CN UPDATED 06/04/10*LJ UPDATED 09/02/10*JBRead more
Incident date: Apr 12, 2010
I NOTICED A CRACK ALONG THE REAR HATCHDOOR LIFT GATE ALONG THE BEZEL OR EMBLEM THAT RUNS VERTICALLY DOWN THE LIFT GATE, IT WAS BOUGHT TO MY ATTENTION FORM OTHER AVIATOR OWNERS WITH THE SAME EXACT DEFECT ON THEIR REAR HATCH DOOR LIFTGATES, THAT THIS IS A DEFECT ALL AVIATOR HAVE. I STARTED TO NOTICE OTHER AVIATOR AND SURE ENOUGH THEY ALL HAVE THE SAME CRACK, MY NEIGHBOR WAS ABLE TO DET HIS FIXED WI
... TH THE LINCOLN DEALER IN PEMBROKE PINES, WHO ACKNOWLEDGES THIS AS BEING A COMMON DEFECT. ALTHOUGH I WENT TO THE DEALER, AND THEY WERE WILLING TO COVER PART OF THE COST, BUT I WILL STILL BE HELD RESPONSIBLE FOR A PORTION, I FELT THIS SHOULD NOT BE MY RESPONSIBILITY BUT LINCOLNS FOR THE POOR DESIGN. I ALSO DID RESEARCH ONLINE AND DID FIND OTHERS WITH THE SAME SITUATION, WITH THE CONCLUSION THAT THE DEFECT IS CAUSED BY STRESS ON THE DOOR, FROM OPENING AND CLOSING, AND MANY OF THESE CRACKED PANELS HAVE BEEN REPLACED. LINCOLN IS NOT TAKING FULL RESPONSIBILITY BECAUSE IT HAS NOT BECOME A RECALL. I THINK IT IS ABOUT TIME TO ACKNOWLEDGE THIS AS A MANUFACTURER DEFECT DUE TO THE EXCESS NUMBER OF VEHICLES WITH THE SAME DEFECT GOING BACK TO 2003 MODELS. THE LINCOLN AVIATOR MODELS HAS A DEFECT ALONG THE REAR HATCH DOOR LIFT GATE, THE A STRAIGHT CRACK APPEARS AFTER. *TRRead more
Incident date: Apr 8, 2010
ON JUNE 5, 2008 I WAS IN LINE ON A HILL TO GET INTO A CAR WASH & ACCELERATED INTO THE CAR ON LINE IN FRONT OF ME. I DID FILE A POLICE REPORT AT THAT TIME. I THOUGHT MY FOOT SLIPPED OFF THE BRAKE & THAT IT COULD HAVE BEEN MY FAULT. HOWEVER,ON APRIL 8, 2010 I WAS WAITING IN LINE AT THE SAME CAR WASH IN EXACTLY THE SAME SPOT.I TAPPED THE ACCELERATOR SLIGHTLY TO MOVE UP IN LINE AND MY CAR LURCHED FORW
... ARD OUT OF CONTROL. DESPITE PRESSING HARD ON THE BRAKE PEDAL MY CAR STILL ACCELERATED INTO THE CAR IN LINE IN FRONT OF ME. I DID NOT FILE A POLICE REPORT ON APRIL 8, 2010. *TRRead more
Crash
Incident date: May 1, 2009
TL*THE CONTACT OWNS A 2006 LINCOLN TOWNCAR. WHILE DRIVING AT SPEEDS OF 20 MPH, THE PASSENGER SIDE FRONT TIRE ROD FAILED. THE CONTACT LOSS CONTROL OF THE VEHICLE CAUSING A CRASH. THE POLICE WERE CALLED TO THE SCENE. THERE WERE NO INJURIES. THE VEHICLE WAS TOWED TO AN INSURANCE COMPANY REPAIR SHOP FOR REPAIRS. THE FAILURE HAS NOT RECURRED. THE FAILURE MILEAGE WAS 55,000 AND THE CURRENT MILEAGE WAS 6
... 5,000.Read more
Crash
Incident date: Mar 28, 2010
TL* THE CONTACT OWNS A 2001 LINCOLN LS. THE CONTACT STATED WHILE DRIVING AT APPROXIMATELY 3 MPH AND APPROACHING A DRIVEWAY, THE LOWER BALL JOINTS FRACTURED FROM THE VEHICLE CAUSING THE FRONT PASSENGERS SIDE TIRE TO COLLAPSE OUTWARD. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE REPAIRS WERE MADE ACCORDINGLY. THE MANUFACTURER ADVISED THERE WERE NO RECALLS OR COMPLAINTS PERTAINING TO THIS
... ISSUE. THE FAILURE MILEAGE WAS 89,300 AND THE CURRENT MILEAGE WAS 89,400.Read more
Incident date: Apr 8, 2010
TL* THE CONTACT OWNS A 2003 LINCOLN NAVIGATOR. THE CONTACT STATED THAT THE RUNNING BOARDS ON BOTH SIDES OF VEHICLES WERE EXHIBITING ROTTING. THE BRACKETS WERE RUSTED AND CORRODED AND THE SHEET METAL UNDERNEATH THE BOARDS WAS MISSING. THE CONTACT ATTEMPTED TO CONSULT WITH THE DEALER ON SEVERAL OCCASIONS BUT TO NO AVAIL. THE FAILURE MILEAGE WAS APPROXIMATELY 96,800.
Incident date: Mar 15, 2010
2004 LINCOLN LS SAFETY ISSUE DUE TO THROTTLE BODY FAILURE ON THE HIGHWAY CAR WENT INTO A SAFETY MODE AT FULL SPEED ON THE MAIN INTERSTATE AND ALMOST GOT MYSELF AND FAMILY KILLED. *TR
Incident date: Apr 3, 2010
TL* THE CONTACT OWNS A 2003 LINCOLN AVIATOR. THE CONTACT STATED THAT WHILE ATTEMPTING TO PARK IN THE DRIVE POSITION, THE VEHICLE BEGAN TO ABNORMALLY ACCELERATE IN THE REVERSE POSITION WITHOUT WARNING. THE CONTACT WAS ABLE TO STOP THE VEHICLE WITHOUT INCIDENT. UPON FURTHER INSPECTION, HE FOUND THAT THE SHIFTER CABLE WAS DISCONNECTED. HE WAS ABLE TO CONNECT THE CABLE AND PARK THE VEHICLE; HOWEVER; T
... HE CABLE DISCONNECTED A SECOND TIME WHILE PARKING. THE DEALER ADVISED THE CONTACT THAT THE FAILURE WAS DIRECTLY RELATED TO NHTSA CAMPAIGN ID NUMBER 02V313000: POWER TRAIN: AUTOMATIC TRANSMISSION. THE FAILURE AND CURRENT MILEAGES WERE 62,000.Read more
Incident date: Mar 7, 2010
TL* THE CONTACT OWNS A 2009 LINCOLN MKS. THE CONTACT STATED THAT WHILE DRIVING AT SPEEDS OF 40 MPH, HE ATTEMPTED TO CHANGE LANES AND NOTICED THAT THE REAR HEAD RESTRAINT WAS BLOCKING HIS LINE OF VISION. THE HEAD RESTRAINT CAUSED A BLIND SPOT ON BOTH SIDES OF THE REAR WINDOWS. THE DEALER WAS NOTIFIED AND THEY ADVISED REMOVING THE HEAD RESTRAINTS OR ADJUSTING THEM IN A LOWER POSITION. THE MANUFACTUR
... ER ADVISED HAVING THE DEALER OFFER THEIR ASSISTANCE. THE CONTACT STATED THAT NEITHER THE DEALER NOR THE MANUFACTURER HAD BEEN ABLE TO ASSIST HIM. THE FAILURE MILEAGE WAS 9,000 AND THE CURRENT MILEAGE WAS 9,800.Read more
Incident date: Mar 31, 2010
TL*THE CONTACT OWNS A 1998 LINCOLN TOWN CAR. WHILE DRIVING APPROXIMATELY 65 MPH, THE CONTACT STATED THAT THE SCREW INSIDE THE REFLECTIVE CONE OF THE BULB WAS LOOSE WHICH CAUSED THE BULB TO SHATTER AND FAIL. THE VEHICLE WAS TAKEN TO THE DEALERSHIP WHERE THE DEALER ATTEMPTED TO SELL THE CONTACT A NEW BULB INSTEAD OF REPAIR THE PROBLEM. THE VIN WAS UNAVAILABLE. THE CURRENT AND FAILURE MILEAGES WERE A
... PPROXIMATELY 500,800.Read more
Incident date: Mar 31, 2010
MY VEHICLE IS A 2005 LINCOLN NAVIGATOR. THE VEHICLE CAME TO A STALL WHILE DRIVING ON THE EXPRESSWAY. THE MOTOR WAS RUNNING BUT THE VEHICLE WOULD NOT ACCELERATE. THIS IS VERY FRIGHTENING AS VEHICLES FOLLOWING CLOSELY ARE UNABLE TO DETERMINE WHEN MY VEHICLE IS SLOWING DOWN BECAUSE THE BRAKES ARE NOT APPLIED. THE VEHICLE SLOWS RAPIDLY AND THERE IS NO WAY TO DRIVE THE VEHICLE TO A SAFE PLACE OUT OF TR
... AFFIC.Read more
Incident date: Apr 30, 2009
TL*THE CONTACT OWNS A 2009 LINCOLN MKS. THE CONTACT WAS DRIVING APPROXIMATELY 3 MPH, APPROACHING A STOP SIGN. WHEN THE BRAKE PEDAL WAS APPLIED A THE CONTACT HEARD A GRINDING NOISE. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSTIC TESTING. THE TECHNICIAN RESURFACED THE BRAKE PADS; HOWEVER, THE FAILURE CONTINUED AFTER THE SERVICE REPAIR. THE FAILURE MILEAGE WAS 2,432. THE CURRENT MILEAGE WAS 16,00
... 0.Read more
Incident date: Mar 28, 2010
I HAVE A 2000 LINCOLN LS 3.9L V8 WITH APPROXIMATELY 115,000 MILES AND I HAVE BEEN EXPERIENCING UNINTENDED ACCELERATION IN MY VEHICLE. ALTHOUGH THE EXPERIENCE IS DIFFERENT THAN THE TOYOTAS THAT ACCELERATED TO 100+ MPH IT MAY BE ABLE TO PROVIDE SOME INSIGHT UPON WHAT IS GOING ON WITH THE CURRENT PROBLEM AT HAND. FIRST I HAVE TO NOTE THAT MY VEHICLE DOES NOT HAVE A CHECK ENGINE LIGHT ON AND SEEMS TO
... BE IN GOOD WORKING ORDER BEING THAT I DRIVE IT EVERY DAY TO AND FROM SCHOOL. I AM VERY ATTACHED TO MY CAR AND SERVICE IT REGULARLY. WHEN I START MY CAR PUT IT IN GEAR AND PRESS ON THE GAS THE CAR WILL START TO REV UNCONTROLLABLY AND ACCELERATE, I HAVE TO JAM ON THE BREAKS TO STOP THE VEHICLE WHILE THIS IS HAPPENING. WHEN I JAM THE TRANSMISSION INTO PARK THE CAR CONTINUES TO REV WITHOUT INPUT FROM ME BUT THE ACCELERATION STOPS. THE CAR HAS BEEN TO THE DEALERSHIP FOR A FUEL INJECTION SERVICE BECAUSE I THOUGHT IT MAY BE THE THROTTLE GETTING STUCK. TO NO AVAIL IT DIDNT SOLVE MY PROBLEM AND I HOPE IT CAN PROVIDE SOME INSIGHT TO SAVE LIVES.Read more
Incident date: Mar 30, 2010
LEAKY WINSHIELD CAUSING FAULTY WIREING AND CAR SHUTTING OFF WHILE MOVING WIPERS STOP WORKING AMONG OTHER THINGS FORD NOES OF THIS ISSUE AND IS NOT DOING ANTHING TO FIX ISSUE THIS IS A SAFTY ISSUE AS IT COULD CAUSE A FIRE OR EVEN LOSS OF CONTROL OF VEHICLE WHILE DRIVING AS IT SHUTS OFF SPERATICALLY AND SOMETIMES WONT RESTART