Showing 18,739 complaints for LINCOLN
Incident date: Jan 3, 2013
THIS LOW MILEAGE VEHICLE (20,300 MILES) SHIFTS FROM PARK INTO REVERSE WITH A SUDDEN LURCH AND THUD. ALSO WHEN ACCELERATING IN DAILY DRIVING VEHICLE PAUSES AND THEN A HARD SHIFT OR TWO WITH LURCH FORWARD. OCCURRENCES ARE INCREASING IN FREQUENCY. NO COMPUTER CODES OR WARNING LIGHTS ILLUMINATE. CALLED FORD/LINCOLN CUSTOMER SERVICE AND WAS TOLD THAT PROBLEM WAS SIMILAR TO TSB 05612 BUT BUILD DATE FOR
... VIN IS 6/2005 SO NO FURTHER ASSISTANCE OFFERED. SAFETY IS BECOMING AN ISSUE. *TRRead more
Incident date: Dec 17, 2012
TL* THE CONTACT OWNS A 2011 LINCOLN TOWN CAR EQUIPPED WITH MICHELIN RADIAL XSE TIRES, SIZE P225/60/R17. THE CONTACT NOTICED THE TIRE WAS COMPLETELY FLAT WITH A 3 INCH GASH ON IT. THE CONTACT TOOK THE TIRE TO A DEALER WHO STATED THAT HE MUST HAVE HIT A POT HOLE IN ORDER FOR THE TIRE TO SUCH EXTENSIVE DAMAGE. THE TIRE WAS REPLACED BUT ANOTHER FAILURE RECURRED ON THE REAR DRIVERS SIDE TIRE. THE CONTA
... CT STATED THAT THERE WAS ALSO A BLISTER ON THE TIRE. THE FAILURE MILEAGE OF THE TIRE AND VEHICLE WAS 6,000. THE DOT NUMBER WAS UNAVAILABLE.Read more
Incident date: Jul 13, 2008
TRAVELING FROM DALLAS, TX TO ATHENS, AL 7:30PM LIGHTS SO DIM I COULD BARELY SEE THE ROAD AHEAD. I HAVE USED CLEANING KITS SEVERAL TIMES TO CLEAN THE HEADLIGHT LENS WITH NO RESULTS. I ALSO PURCHASED AND INSTALLED REPLACEMENT HEADLIGHT ASSEMBLIES FROM EBAY WITH NO IMPROVEMENT IN THE LIGHTING. I HAVE TRIED SEVERAL DIFFERENT BULBS WITH NO IMPROVEMENT. THIS IS REALLY A SAFETY PROBLEM. I HAVE BEEN LUCKY
... SO FAR. ..UPDATED 01/17/2013 *BFRead more
Incident date: Jul 13, 2008
TRAVELING FROM DALLAS, TX TO ATHENS, AL 7:30PM LIGHTS SO DIM I COULD BARELY SEE THE ROAD AHEAD. I HAVE USED CLEANING KITS SEVERAL TIMES TO CLEAN THE HEADLIGHT LENS WITH NO RESULTS. I ALSO PURCHASED AND INSTALLED REPLACEMENT HEADLIGHT ASSEMBLIES FROM EBAY WITH NO IMPROVEMENT IN THE LIGHTING. I HAVE TRIED SEVERAL DIFFERENT BULBS WITH NO IMPROVEMENT. THIS IS REALLY A SAFETY PROBLEM. I HAVE BEEN LUCKY
... SO FAR. ..UPDATED 01/17/2013 *BFRead more
Incident date: Jan 11, 2013
I AM A 66 YR OLD WIDOW, OWNER OF A 2001 LS PURCHASED JUNE 2001, A RECALL FIX WAS TO HAVE BEEN DONE BEFORE MY PURCHASE IN MARCH OF 2001 TO CORRECT A PROBLEM WITH BALL JOINTS. I READ ONLINE THAT MANY OF THESE VEHICLES HAVE THE DAMAGE THAT WAS SUPPOSE TO BE CORRECTED FOR WHEN THEY GET TO ABOUT 67000 MILES, I AM AT 67000 MILES, TOOK MY CAR IN FOR INSPECTION AND NEED AN 1800 DOLLAR FIX TO CORRECT THE I
... SSUE THAT WAS SUPPOSE TO BE AVOIDED BY THE RECALL. FORD SAID, TOO LONG AGO, NO WARRANTY BEYOND THE NORM FOR RECALL FIXES. I CAN NOT BELIEVE WITH THE AMOUNT OF EVIDENCE THAT THESE CARS ALL REQUIRE A FIX AT 67000 MILES THAT FORD ISN'T FORCED TO ADDRESS THIS DANGEROUS CONDITION. I ALSO DON'T KNOW IF IT'S SAFE TO DRIVE A WHILE LONGER, I JUST DON'T KNOW HOW THEY GOT AWAY WITH A RECALL THAT DID NOT PROVIDE THE FIX. *TRRead more
Incident date: Jan 11, 2013
I AM A 66 YR OLD WIDOW, OWNER OF A 2001 LS PURCHASED JUNE 2001, A RECALL FIX WAS TO HAVE BEEN DONE BEFORE MY PURCHASE IN MARCH OF 2001 TO CORRECT A PROBLEM WITH BALL JOINTS. I READ ONLINE THAT MANY OF THESE VEHICLES HAVE THE DAMAGE THAT WAS SUPPOSE TO BE CORRECTED FOR WHEN THEY GET TO ABOUT 67000 MILES, I AM AT 67000 MILES, TOOK MY CAR IN FOR INSPECTION AND NEED AN 1800 DOLLAR FIX TO CORRECT THE I
... SSUE THAT WAS SUPPOSE TO BE AVOIDED BY THE RECALL. FORD SAID, TOO LONG AGO, NO WARRANTY BEYOND THE NORM FOR RECALL FIXES. I CAN NOT BELIEVE WITH THE AMOUNT OF EVIDENCE THAT THESE CARS ALL REQUIRE A FIX AT 67000 MILES THAT FORD ISN'T FORCED TO ADDRESS THIS DANGEROUS CONDITION. I ALSO DON'T KNOW IF IT'S SAFE TO DRIVE A WHILE LONGER, I JUST DON'T KNOW HOW THEY GOT AWAY WITH A RECALL THAT DID NOT PROVIDE THE FIX. *TRRead more
Incident date: Dec 12, 2012
TL* THE CONTACT OWNS A 2005 LINCOLN LS. THE CONTACT STATED THAT WHILE DRIVING, THE CONTACT DECELERATED AND THE VEHICLE ERRONEOUSLY ACCELERATED. THE CONTACT SHIFTED INTO PARK TO STOP THE VEHICLE. THE CONTACT ALSO STATED THAT THE FAILURE RECURRED SEVERAL TIMES AND EVENTUALLY BECAME PERMANENT. THE VEHICLE IS CURRENTLY BEING DIAGNOSED BY THE DEALER. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE AP
... PROXIMATE FAILURE MILEAGE WAS 100,000.Read more
Incident date: Dec 7, 2012
UPON ENTERING GA 400 NORTHBOUND FROM US 285 WEST IN ATLANTA, I STRUCK AN OBJECT IN THE ROADWAY RESULTING IN A DELAYED BLOWOUT APPROXIMATELY 30 SECONDS LATER ON THE FRONT LEFT TIRE. THIS RESULTED IN LOSS OF CONTROL OF MY VEHICLE CAUSING IT TO PULL HARD TO THE LEFT. I CROSSED 4 LANES OF TRAFFIC, STRIKING ANOTHER VEHICLE IN THE REAR IN THE THIRD LANE AND THEN CONTINUING ACROSS TWO OTHER LANES AND STR
... IKING THE CENTER CONCRETE DIVIDER WALL HEAD ON. THE AIR BAG FAILED TO DEPLOY ON IMPACT. I WAS WEARING MY SEATBELT AT THE TIME. I SUSTAINED MULTIPLE RIB FRACTURES, INTERNAL INJURIES RESULTING IN BLEEDING, AND FACIAL LACERATIONS. I SPENT 15 DAYS IN THE HOSPITAL RECOVERING. *TRRead more
Crash
1 injured
Incident date: May 5, 2012
1993 THROUGH EARLY 1996 LINCOLN MARK VIII'S HAVE A SERIOUS VISIBILITY PROBLEM AT NIGHT DUE TO THEIR INFERIOR HEADLIGHT DESIGN. BECAUSE THE HEADLIGHT PROFILE IS SO SLIM AND THE LENSES YELLOW SO EASILY WITH USE, YOU CAN'T SEE ANYTHING WHEN IT IS DARK. I FIND MYSELF CHECKING TO MAKE SURE MY HEADLIGHTS ARE IN FACT ON THEY ARE SO BAD. NO PRECAUTIONS CAN BE TAKEN TO PREVENT THIS LOW VISIBILITY SITUATION
... , IT IS A BAD DESIGN. FORD SWITCHED OVER TO HID IN 1996 TO CORRECT THE PROBLEM, BUT US OLDER VEHICLE OWNERS WERE LEFT OUT WITH A DANGEROUS CAR AND OUR ONLY CHOICE IS TO PAY ONE THOUSAND PLUS DOLLARS FOR A RETROFIT KIT THAT WE SHOULD NOT HAVE TO PAY FOR. *TRRead more
Incident date: May 5, 2012
1993 THROUGH EARLY 1996 LINCOLN MARK VIII'S HAVE A SERIOUS VISIBILITY PROBLEM AT NIGHT DUE TO THEIR INFERIOR HEADLIGHT DESIGN. BECAUSE THE HEADLIGHT PROFILE IS SO SLIM AND THE LENSES YELLOW SO EASILY WITH USE, YOU CAN'T SEE ANYTHING WHEN IT IS DARK. I FIND MYSELF CHECKING TO MAKE SURE MY HEADLIGHTS ARE IN FACT ON THEY ARE SO BAD. NO PRECAUTIONS CAN BE TAKEN TO PREVENT THIS LOW VISIBILITY SITUATION
... , IT IS A BAD DESIGN. FORD SWITCHED OVER TO HID IN 1996 TO CORRECT THE PROBLEM, BUT US OLDER VEHICLE OWNERS WERE LEFT OUT WITH A DANGEROUS CAR AND OUR ONLY CHOICE IS TO PAY ONE THOUSAND PLUS DOLLARS FOR A RETROFIT KIT THAT WE SHOULD NOT HAVE TO PAY FOR. *TRRead more
Incident date: Jan 6, 2013
TL* THE CONTACT OWNS A 2006 LINCOLN NAVIGATOR. THE CONTACT STATED THAT THE ENGINE FAIL SAFE MODE WARNING LIGHT ILLUMINATED AS THE VEHICLE STALLED. THE VEHICLE WAS ABLE TO BE RESTARTED AND BEGAN TO FUNCTION NORMALLY. THE VEHICLE WAS NOT TAKEN TO A MECHANIC AND WAS NOT REPAIRED. THE MANUFACTURER WAS CONTACTED ABOUT THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 140,000.
Incident date: Jan 5, 2013
WE HAD DRIVEN THE VEHICLE ABOUT ONE MILE FROM THE BEACH TO A RESTAURANT, WHERE WE PARKED AS USUAL AND ENTERED TO DINE. WE HAD BEEN IN THE RESTAURANT APPROXIMATELY 15 - 20 MINUTES WHEN THE WAITER ANNOUNCED THAT THERE WAS A "CAR ON FIRE" IN THE PARKING LOT. MY FAMILY AND I, ALONG WITH EVERYONE ELSE IN THE RESTAURANT, RUSHED OUTSIDE, WHERE I WAS HORRIFIED TO SEE MY LINCOLN NAVIGATOR SURROUNDED BY P
... OLICE CARS AND ENGULFED IN FLAMES. I HAVE PHOTOS ON MY PHONE IF NECESSARY. THE FIRE HAD VERY OBVIOUSLY STARTED IN THE ENGINE COMPARTMENT AND PROBABLY ON THE DRIVER'S SIDE, AS THE FRONT TIRE ON THAT SIDE HAD MELTED AND WAS FLAT, BUT THE OTHER TIRES WERE ALL INTACT. I HAVE SINCE BEEN MADE AWARE OF A FAULTY SWITCH RELATED TO THE CRUISE CONTROL THAT CAN CAUSE THESE PROBLEMS. I AM ALMOST CERTAIN THAT WE TOOK OUR VEHICLE IN AND HAD THAT RECALL DEALT WITH YEARS AGO. I WILL SEARCH FOR PAPERWORK. I REMEMBER SOME REPAIR BEING DONE AT THE DEALER, BUT I CANNOT REMEMBER IF IT WAS A RECALL OR JUST SOMETHING THEY CONTACTED US TO RECOMMEND BEING REPAIRED. EITHER WAY, MY PARKED VEHICLE WAS DESTROYED BY FIRE WHILE I DINED. *TRRead more
Fire
Incident date: Jul 25, 2012
TL* THE CONTACT OWNS A 2005 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHILE DRIVING 20 MPH, HE ENGAGED THE FRONT WINDSHIELD WIPERS AND THEY BEGAN TO MALFUNCTION ERRATICALLY. THE CONTACT TURNED THE WIPERS SWITCH OFF BUT THEY CONTINUED TO OPERATE. THE VEHICLE WAS TAKEN TO THE DEALER FOR INSPECTION WHERE THEY ADVISED THE CONTACT THAT THE WINDSHIELD WIPER MOTOR NEEDED TO BE REPLACED. THE VEHICLE WAS
... REPAIRED BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 73,000.Read more
Incident date: Dec 29, 2012
TL* THE CONTACT OWNS A 2006 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHILE DRIVING 10 MPH, SHE HEARD A LOUD SCRATCHING SOUND. AFTER INSPECTING THE VEHICLE, SHE NOTICED THAT THE FUEL TANK HAD BECOME DETACHED FROM THE VEHICLE. THE VEHICLE WAS TOWED TO THE DEALER WHERE IT WAS FOUND THAT THE FUEL TANK STRAPS HAD FAILED DUE TO CORROSION AND NEEDED TO BE REPLACED ALONG WITH THE FUEL TANK. THE MANUFACT
... URER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 52,000.Read more
Incident date: Dec 29, 2012
WE HEARD A SCRAPING SOUND AND PULLED INTO A PARKING SPACE,ANOTHER MOTORIST JUMPED OUT OF THEIR CAR AND SAID YOUR GAS TANK IS DRAGGING ON THE GROUND! THE VEHICLE WAS TOWED TO THE DEALERSHIP. *TR
Incident date: Dec 18, 2012
THE CAR ALWAYS BEEPS OVERHEATS AND LOSES STEERING. *TR
Crash
Incident date: Dec 18, 2012
THE CAR ALWAYS BEEPS OVERHEATS AND LOSES STEERING. *TR
Crash
Incident date: Dec 18, 2012
THE CAR ALWAYS BEEPS OVERHEATS AND LOSES STEERING. *TR
Crash
Incident date: Jan 10, 2012
HAD A FLAT TIRE GOING DOWN THE HIGHWAY. DIDN'T THINK MUCH ABOUT IT...IT HAPPENS. GOT A COUPLE OF NEW TIRES PUT ON AND A FEW MONTHS LATER IT HAPPENS AGAIN. RUINING THE $250 TIRE AGAIN. MY MECHANIC SAYS THE CHROME IS PEELING OFF MY RIMS AND THAT IS WHAT IS CAUSING ME TO LOSE AIR PRESSURE IN THE TIRE,AND THAT I SHOULD REPLACE THE RIMS. THEY ARE ABOUT $550 A PIECE SO THATS NOT GOING TO HAPPEN. THESE C
... ARS THAT HAVE LOW PROFILE TIRES NEED TO HAVE TIRE PRESSURE MONITORING SYSTEMS BECAUSE YOU CAN'T LOOK AT THE TIRE AND TELL ITS LOW. IF FORD DOESN'T FEEL THIS IS A SAFETY ISSUE THEY ARE WRONG.I WORK AT A FORD DEALERSHIP AND I SEE STUPID RECALLS FOR THINGS THAT MIGHT HAPPEN ONE TIME IN A THOUSAND. BUT I BET THIS IS HAPPENING TO ALL THE ZEPHYR,FUSIONS,MILANS, OR ANYTHING THEY ARE PUTTING THESE JUNK RIMS ON. *TRRead more
Incident date: Feb 16, 2011
TL* THE CONTACT OWNS A 2002 LINCOLN LS. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 40 MPH, THE VEHICLE WOULD NOT SHIFT FROM FOURTH GEAR TO FIFTH GEAR. THE CONTACT ALSO STATED THAT THE CHECK ENGINE WARNING LIGHT WAS ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSTIC TESTING. THE TECHNICIAN STATED THAT THE POWER TRANSMISSION NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE
... AWARE OF THE FAILURE. THE VEHICLE WAS REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 120,000 AND THE CURRENT MILEAGE WAS 125,000.Read more
Incident date: Dec 18, 2012
TL* THE CONTACT OWNS A 2005 LINCOLN NAVIGATOR. THE CONTACT STATED THAT WHILE SITTING IDLE IN TRAFFIC, THE THROTTLE WARNING LIGHT ILLUMINATED AS THE VEHICLE STALLED SIMULTANEOUSLY. THE CONTACT WAS ABLE TO RESTART THE ENGINE. THE VEHICLE WAS NOT TAKEN TO THE DEALER TO HAVE A DIAGNOSTIC PERFORMED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND THE C
... URRENT MILEAGE WAS 55,875.Read more
Incident date: Dec 14, 2012
THE VEHICLE WAS IN OUR GARAGE WITH THE DOOR CLOSED AND THE REAR HATCH WINDOW SHATTERED. THE WINDOW IS COMPLETELY SHATTERED WITH TWO SOFTBALL SIZED HOLES WHERE THE GLASS WAS BLOWN OUT ONTO THE GARAGE FLOOR. NO ONE WAS IN THE CAR NOR THE GARAGE WHEN THIS HAPPENED AND THERE WERE NO ITEMS IN THE CAR THAT COULD HAVE CAUSED THE DAMAGE. WE HAVE NOT MOVED THE VEHICLE HOPING LINCOLN WOULD CARE ENOUGH TO
... COME AND SEE WHAT HAS HAPPENED. THEY TOLD US THEY WOULD NOT SEND ANYONE TO VIEW THE WINDOW. THE CONCERN IS THAT THIS IS A SAFETY ISSUE THAT COULD POSSIBLY INJURE A PASSENGER. THIS REPORT IS PROVIDE EVIDENCE OF OUR EXPERIENCE. *TRRead more
Incident date: Dec 12, 2012
TL* LTHE CONTACT OWNS A 2010 LINCOLN MKS. THE CONTACT STATED THAT WHILE DRIVING WITH CRUISE CONTROL ON APPROXIMATELY 70 MPH, AND CHANGING LANES, THE VEHICLE SUDDENLY ACCELERATED. THE CONTACT DEPRESSED THE BRAKES AND THE VEHICLE ACCELERATED EVEN FARTHER. AFTER KICKING THE ACCELERATOR PEDAL FORCEFULLY, THE VEHICLE DECELERATED. THE CONTACT TOOK THE VEHICLE TO THE DEALER FOR DIAGNOSIS WHERE HE WAS AD
... VISED THAT THE PANEL FOR THE CONSOLE BECAME LOOSE AND JAMMED THE PEDAL, CAUSING THE SUDDEN ACCELERATION FAILURE. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS CONTACTED AND OFFERED NO ASSISTANCE. THE FAILURE AND CURRENT MILEAGES WERE 28,385....UPDATED 01/30/13 *BF UPDATED 02/04/2013 *JSRead more
Incident date: Dec 10, 2012
TL* THE CONTACT OWNS A 2009 LINCOLN NAVIGATOR. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 55 MPH, THE CONTACT HORN FAILED TO RESPOND WHEN ENGAGED. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSTIC TESTING. THE TECHNICIAN STATED THAT THE WIRES CONNECTED TO THE HORN NEEDED TO BE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND STATED THAT THE VEHICLE WAS NOT INCLUDED IN ANY RE
... CALL. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE AND CURRENT MILEAGE WAS 57,114.Read more
Incident date: Dec 8, 2012
TL* THE CONTACT OWNS A 2003 LINCOLN TOWN CAR. THE CONTACT WAS HAVING ROUTINE MAINTENANCE PERFORMED ON THE VEHICLE WHEN THE TECHNICIAN ADVISED THAT THE REAR BEARINGS FAILED, CAUSING WEAR TO THE REAR AXLE. THE TECHNICIAN ADVISED THE CONTACT TO REPLACE THE BEARINGS, AXLE AND THE SEALS. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS CONTACTED ABOUT THE ISSUE AND OFFERED NO ASSISTANCE. THE FAILURE
... AND CURRENT MILEAGES WERE APPROXIMATELY 89,000.Read more
Incident date: Nov 29, 2012
TL* THE CONTACT OWNS A 2010 LINCOLN NAVIGATOR. THE CONTACT STATED THAT WHILE PARKED, HE NOTICED COOLANT LEAKING FROM THE UNDER BODY OF VEHICLE. THE CONTACT INSPECTED THE VEHICLE AND NOTICED THE AUXILIARY SUPPLY TUBE WHICH LAYS ON TOP OF A STEEL BRACKET WAS LEAKING COOLANT. THE CONTACT MENTIONED THAT THE STEEL BRACKET HAD RUBBED A HOLE ONTO THE AUXILIARY SUPPLY TUBE. THE VEHICLE WAS TAKEN TO THE DE
... ALER FOR DIAGNOSTIC TESTING. THE TECHNICIAN STATED THE AUXILIARY SUPPLY TUBE NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 76,000.Read more
Incident date: Dec 2, 2012
FILLED CAR WITH GAS. PULLED UP TO ENTER ROADWAY AND HAD TO STOP FOR TRAFFIC. WHEN I TRIED TO MOVE FORWARD EMERGENCY BRAKE CAME ON. PUT CAR IN PARK SHUT OFF ENGINE AND RESTARTED AND EMERGENCY BRAKE RELEASED. THIS IS THE SECOND TIME THIS HAS HAPPENED IN TWO DAYS. LEAVING GAS STATION. PULLED UP TO ENTER ROAD. HAD TO STOP FOR TRAFFIC. TRIED TO MOVE FORWARD, BUT
... EMERGENCY BRAKE CAME ON. PUT CAR IN PARK, SHUT OFF ENGINE. RESTARTED AND EMERGENCY BRAKE CAME OFF. THIS IS THE SECOND TIME THIS HAS HAPPENED. *TRRead more
Incident date: Dec 2, 2012
FILLED CAR WITH GAS. PULLED UP TO ENTER ROADWAY AND HAD TO STOP FOR TRAFFIC. WHEN I TRIED TO MOVE FORWARD EMERGENCY BRAKE CAME ON. PUT CAR IN PARK SHUT OFF ENGINE AND RESTARTED AND EMERGENCY BRAKE RELEASED. THIS IS THE SECOND TIME THIS HAS HAPPENED IN TWO DAYS. LEAVING GAS STATION. PULLED UP TO ENTER ROAD. HAD TO STOP FOR TRAFFIC. TRIED TO MOVE FORWARD, BUT
... EMERGENCY BRAKE CAME ON. PUT CAR IN PARK, SHUT OFF ENGINE. RESTARTED AND EMERGENCY BRAKE CAME OFF. THIS IS THE SECOND TIME THIS HAS HAPPENED. *TRRead more
Incident date: Oct 15, 2012
POWER LIFTGATE OPENED WITHOUT COMMAND WHILE BEING DRIVEN ON HIGHWAY WITHOUT COMMAND AND WOULD NOT RESPOND TO INTERIOR CONTROL OR KEYFOB TO CLOSE AND HAD TO CLOSE MANUALLY. LIFTGATE OPENED ON THREE ADDITIONAL OCCASIONS WITHIN 45 MINS OF THE FIRST OCCURRENCE. THE THIRD OCCURRENCE RESULTED IN THE LIFTGATE BEING DAMAGED, (REPAIR EST AT $2,500), WHILE ENTERING AN UNDERGROUND PARKING GARAGE. IN ALL OCCU
... RRENCES, THE LIFTGATE HAD TO BE CLOSED MANUALLY AS IT WOULD NOT RESPOND TO THE INTERIOR CONTROL OR KEYFOB. VEHICLE WAS TAKEN TO A LOCAL LINCOLN DEALERSHIP WHERE IT REMAINED FOR 42 DAYS WITHOUT BEING REPAIRED. DEALERSHIP COULD NOT DUPLICATE CONDITION AND REPAIRS WERE NOT MADE. FORD OGC DENIED CLAIM TO REPAIR RESULTING DAMAGE TO DUE TO MALFUNCTION. OWNERS OPINION IS THAT THE VEHICLE HAS A SERIOUS SAFETY DEFECT WHICH COULD RESULT IN CARGO FALLING FROM THE VEHICLE WHILE BEING DRIVEN ON THE HIGHWAY AND CAUSE AN ACCIDENT OR MULTI VEHICLE PILE-UP DUE TO DRIVERS ATTEMPTING TO AVOID OR COLLIDING WITH OBJECTS FALLING FROM THE VEHICLE IF THE LIFTGATE OPENS AGAIN WITHOUT COMMAND. FORD/LINCOLN CUSTOMER COMPLAINT CASE [XXX] FILED 16 OCT 12. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Oct 15, 2012
POWER LIFTGATE OPENED WITHOUT COMMAND WHILE BEING DRIVEN ON HIGHWAY WITHOUT COMMAND AND WOULD NOT RESPOND TO INTERIOR CONTROL OR KEYFOB TO CLOSE AND HAD TO CLOSE MANUALLY. LIFTGATE OPENED ON THREE ADDITIONAL OCCASIONS WITHIN 45 MINS OF THE FIRST OCCURRENCE. THE THIRD OCCURRENCE RESULTED IN THE LIFTGATE BEING DAMAGED, (REPAIR EST AT $2,500), WHILE ENTERING AN UNDERGROUND PARKING GARAGE. IN ALL OCCU
... RRENCES, THE LIFTGATE HAD TO BE CLOSED MANUALLY AS IT WOULD NOT RESPOND TO THE INTERIOR CONTROL OR KEYFOB. VEHICLE WAS TAKEN TO A LOCAL LINCOLN DEALERSHIP WHERE IT REMAINED FOR 42 DAYS WITHOUT BEING REPAIRED. DEALERSHIP COULD NOT DUPLICATE CONDITION AND REPAIRS WERE NOT MADE. FORD OGC DENIED CLAIM TO REPAIR RESULTING DAMAGE TO DUE TO MALFUNCTION. OWNERS OPINION IS THAT THE VEHICLE HAS A SERIOUS SAFETY DEFECT WHICH COULD RESULT IN CARGO FALLING FROM THE VEHICLE WHILE BEING DRIVEN ON THE HIGHWAY AND CAUSE AN ACCIDENT OR MULTI VEHICLE PILE-UP DUE TO DRIVERS ATTEMPTING TO AVOID OR COLLIDING WITH OBJECTS FALLING FROM THE VEHICLE IF THE LIFTGATE OPENS AGAIN WITHOUT COMMAND. FORD/LINCOLN CUSTOMER COMPLAINT CASE [XXX] FILED 16 OCT 12. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TRRead more
Incident date: Mar 10, 2012
SIDE STEP BOARDS DON'T WORK. WINDOWS STOP WORKING DUE TO THE DESIGN OF VEHICLE AND WATER GETTING IN. POWER HEATING AND COOLING SEATS DON'T WORK. BACK REAR GATE KEEPS CLOSING HAS HIT THE KIDS AND MYSELF MANY TIMES TRYING TO GET ITEMS OUT OF BACK. CASING AROUND DOOR HANDLE BROKE OFF. THIS IS AN EXPENSIVE VEHICLE THESE COMPLAINT ARE MADE BY NUMEROUS PEOPLE OWNING THIS VEHICLE AND SHOULD BE RECALLED.
... *TRRead more
Incident date: Dec 1, 2012
I AM NOT SURE IF THIS IS THE RIGHT PLACE TO PRESENT THIS ISSUE, BUT WILL EXPLAIN MY CONCERN HERE. I HAVE AN ISSUE WITH THE LOCATION OF THE DRIVER'S SEAT LOCATION IN MY LINCOLN MKX. I AM 6'2" TALL AND HAVE LONG LEGS. I HAVE HAD A KNEE REPLACEMENT WHICH LEFT ME WITH REDUCED RANGE OF MOTION IN MY LEG. MY ISSUE IS THAT I CANNOT STRAIGHTEN MY LEG OUT ENOUGH TO BE COMFORTABLE WHILE DRIVING DUE TO TH
... E LIMITED REARWARD MOTION OF THE SEAT. IN SPEAKING WITH THE SERVICE MANAGER AT THE DEALER WHERE I PURCHASED THE VEHICLE, HE SUGGESTED THAT I CONTACT FORD/LINCOLN DIRECTLY. IN DOING SO, THEY ADVISED THAT CONTACT YOU PEOPLE AT THIS E-MAIL ADDRESS. IT IS MY INTENTION TO POINT OUT THIS MATTER TO YOU AND SEEK SOME ADVICE AND DIRECTION. MY PROPOSAL IS TO RAISE THE SEAT HEIGHT APPROXIMATELY 3" AND ADD A PIECE OF FLAT METAL UNDER THE SEAT TRACK WHICH COULD BE REDRILLED TO ALLOW THE SEAT TO MOVE REARWARD APPROXIMATELY 3+". THESE MODIFICATIONS WOULD USE THE SAME HOLES IN THE SEAT TRACK AND THE ATTACHMENT LOCATIONS IN THE FLOOR THAT EXIST NOW. ANY REPLACEMENT BOLTS THAT WOULD BE USED WOULD OF EQUAL GRADE OF THE ORIGINAL BOLTS. THIS MODIFICATION WOULD ALLOW ME TO SIT HIGHER AND FURTHER BACK FROM THE BRAKE AND GAS PEDALS WHILE ALLOWING MY LEG TO BE STRAIGHTER, THEREFORE MORE COMFORTABLE. I HAVE SEEN THIS TYPE OF MODIFICATION DONE ON OTHER VEHICLES AND IT WORKS. IF DONE PROPERLY IT WOULD NOT ALTER THE LEVEL OF SAFETY IN THE VEHICLE. AT THIS POINT FORD/LINCOLN WILL NOT SUPPORT THIS MODIFICATION WITHOUT MY PRESENTING THE IDEA TO YOU PEOPLE FOR YOUR SUPPORT ON THE MODIFICATION. IF YOU COULD REVIEW THIS REQUEST AND ADVISE ME ON THIS MATTER BY RETURN E-MAIL, I WOULD APPRECIATE IT. *TRRead more
Incident date: Jan 1, 2009
TL* THE CONTACT OWNS A 2003 LINCOLN NAVIGATOR. THE CONTACT STATED THAT THE DRIVER'S SEAT FAILED TO ADJUST AND COULD NOT BE MOVED FORWARD. THE METAL BAR FOR THE DRIVER'S SEAT FRACTURED AND THE SEAT BECAME LOCKED IN PLACE, WHICH WAS ABNORMALLY FAR FROM THE STEERING WHEEL. AS A RESULT, THE CONTACT WAS UNABLE TO REACH THE STEERING WHEEL OR THE ACCELERATOR PEDAL. THE VEHICLE WAS TAKEN TO THE DEALER WHO
... ADVISED THAT THE METAL BAR ADJUSTER FOR THE DRIVER'S SEAT FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 60,000 AND THE CURRENT MILEAGE WAS 81,000.Read more
Incident date: Nov 1, 2012
2006 LINCOLN ZEPHYR. CONSUMER WRITES IN REGARDS TO DEFECTIVE WHEEL RIMS. *SMD THE CONSUMER STATED FOR THE LAST YEAR-AND-A-HALF, HE HAS BEEN LOSING AIR IN AT LEAST ONE OF HIS TIRES. APPROXIMATELY SIX MONTHS AGO, HE NOTICED HE HAD BEEN LOSING AIR IN THREE TIRES. AN INDEPENDENT DEALER INFORM HIM THAT THE LOSS OF AIR WAS DUE TO CORROSION AND CHROME FLAKING OFF THE WHEEL RIM. HE RECOMMENDED THAT THE C
... ONSUMER REPLACE ALL FOUR OF THE WHEELS RIMS. BECAUSE OF THE HIGH COST OF THE WHEEL RIMS, THE CONSUMER DECIDED TO MONITOR THE AIR LOSS AND ADD AIR AS NEEDED. OVER THE LAST FEW MONTHS, IN THREE TIRES, HE BEGAN LOSING BETWEEN 10-20 POUNDS OF AIR OVER A FOUR OR FIVE DAY PERIOD. THE OTHER TIRE MAINTAINED AIR PRESSURE. THE MANUFACTURER AGREED TO REPLACE TWO OF THE RIMS. *JBRead more
Incident date: Jun 1, 2012
TL* THE CONTACT OWNS A 2013 LINCOLN MKT. THE CONTACT STATED THAT THE BATTERY DRAINED COMPLETELY AND THERE WAS NO ACCESS TO THE TRUNK. THE CONTACT STATED THAT THERE WAS NOT A MECHANICAL OVERRIDE TO OPEN THE TRUNK. THE VEHICLE WAS TAKEN TO SEVERAL DEALERS AND THE CONTACT WAS ADVISED BY EACH OF THEM THAT THERE WAS NO REMEDY FOR THE FAILURE BECAUSE THE VEHICLE WAS OPERATING AS DESIGNED. THE DEALER THE
... N REFERRED HIM TO THE MANUFACTURER. THE MANUFACTURER WAS CONTACTED AND REFERRED HIM TO PAGE 79 OF THE OWNER'S MANUAL, WHICH EXPLAINED HOW TO OVERRIDE THE SYSTEM. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 900 AND THE CURRENT MILEAGE WAS 13,000. UPDATED 02/26/13*LJ UPDATED 03/1/2013 *JSRead more
Incident date: Jun 1, 2012
TL* THE CONTACT OWNS A 2013 LINCOLN MKT. THE CONTACT STATED THAT THE BATTERY DRAINED COMPLETELY AND THERE WAS NO ACCESS TO THE TRUNK. THE CONTACT STATED THAT THERE WAS NOT A MECHANICAL OVERRIDE TO OPEN THE TRUNK. THE VEHICLE WAS TAKEN TO SEVERAL DEALERS AND THE CONTACT WAS ADVISED BY EACH OF THEM THAT THERE WAS NO REMEDY FOR THE FAILURE BECAUSE THE VEHICLE WAS OPERATING AS DESIGNED. THE DEALER THE
... N REFERRED HIM TO THE MANUFACTURER. THE MANUFACTURER WAS CONTACTED AND REFERRED HIM TO PAGE 79 OF THE OWNER'S MANUAL, WHICH EXPLAINED HOW TO OVERRIDE THE SYSTEM. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 900 AND THE CURRENT MILEAGE WAS 13,000. UPDATED 02/26/13*LJ UPDATED 03/1/2013 *JSRead more
Incident date: Jun 5, 2012
TL* THE CONTACT OWNS A 2006 LINCOLN ZEPHYR. WHILE DRIVING APPROXIMATELY 55 MPH, THE VEHICLE SUDDENLY HESITATED TO ACCELERATE. THE FAILURE RECURRED INTERMITTENTLY. THE CONTACT LATER NOTICED SMOKE COMING FROM UNDER THE VEHICLE WHILE DRIVING. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC FOR DIAGNOSTIC TESTING. THE MECHANIC ADVISED THE CONTACT THAT THE FIFTH ENGINE COIL HAD MELTED AND CAUSED A SMA
... LL ENGINE FIRE. THE MECHANIC REPLACED THE SPARK PLUG AND THE COIL. AFTER THE REPAIR THE FAILURE CONTINUED. THE VEHICLE WAS TAKEN TO THE DEALER FOR DIAGNOSTIC TESTING. THE TECHNICIAN ADVISED THE CONTACT THAT THE PCM WAS DAMAGED DURING THE FIRE AND WOULD HAVE TO BE REPLACED AND RECALIBRATED. ALL OF THE COILS WOULD HAVE TO BE REPLACED AS WELL. THE VEHICLE WAS REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 93,000. ... UPDATED 02/28/13 *BFRead more
Fire
Incident date: Aug 2, 2012
TL* THE CONTACT OWNS A 2002 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE STEERING WHEEL SUDDENLY BECAME LOOSE AS THE VEHICLE BECAME UNCONTROLLABLE WITHOUT WARNING. THE VEHICLE ALSO WENT AIRBORNE, ROLLED OVER AND SPUN THREE TIMES BEFORE COMING TO A STOP. THE FRONT WINDSHIELD WAS FRACTURED AND THE REAR WINDSHIELD BECAME DETACHED FROM THE VEHICLE. NONE OF THE AIR BAGS DEPLOYED
... . THREE OCCUPANTS AND A PET DOG WERE SEVERELY INJURED AND WERE TRANSPORTED TO THE HOSPITAL FOR TREATMENT. A POLICE REPORT WAS FILED OF THE INCIDENT. THE VEHICLE WAS DESTROYED AND WAS INSPECTED FOR THE CAUSE OF THE STEERING OR AIR BAG FAILURES. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 129,000. UPDATED 08/06/13*LJ THE CONSUMER STATED THE VEHICLE WAS INSPECTED BY HERNDON AND ASSOCIATES EGINEERING FIRM. THE REPORT WAS SENT TO FORD, WHICH FORD DISSMISSED IN FOUR (4) DAYS. UPDATED 08/5/2013 *JSRead more
Crash
3 injured
Incident date: Aug 2, 2012
TL* THE CONTACT OWNS A 2002 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHILE DRIVING 70 MPH, THE STEERING WHEEL SUDDENLY BECAME LOOSE AS THE VEHICLE BECAME UNCONTROLLABLE WITHOUT WARNING. THE VEHICLE ALSO WENT AIRBORNE, ROLLED OVER AND SPUN THREE TIMES BEFORE COMING TO A STOP. THE FRONT WINDSHIELD WAS FRACTURED AND THE REAR WINDSHIELD BECAME DETACHED FROM THE VEHICLE. NONE OF THE AIR BAGS DEPLOYED
... . THREE OCCUPANTS AND A PET DOG WERE SEVERELY INJURED AND WERE TRANSPORTED TO THE HOSPITAL FOR TREATMENT. A POLICE REPORT WAS FILED OF THE INCIDENT. THE VEHICLE WAS DESTROYED AND WAS INSPECTED FOR THE CAUSE OF THE STEERING OR AIR BAG FAILURES. THE MANUFACTURER WAS NOT NOTIFIED. THE FAILURE MILEAGE WAS 129,000. UPDATED 08/06/13*LJ THE CONSUMER STATED THE VEHICLE WAS INSPECTED BY HERNDON AND ASSOCIATES EGINEERING FIRM. THE REPORT WAS SENT TO FORD, WHICH FORD DISSMISSED IN FOUR (4) DAYS. UPDATED 08/5/2013 *JSRead more
Crash
3 injured
Incident date: Nov 11, 2012
HELLO, LUCKILY I MADE IT HOME BEFORE THIS HAPPENED AS I WAS TOWING MY TRAILER WITH A COUCH AND CHAIR ON IT. I GOT HOME AND STOPPED IN FRONT OF MY HOUSE, THEN HAD TO MOVE THE TRUCK. WHEN I STEPPED ON THE GAS TO MOVE, THERE WAS A HORRENDOUS BANG, A CLUNKING NOISE AND THE REAR OF THE VEHICLE DROPPED DOWN ALMOST TO THE GROUND. UPON JACKING THE VEHICLE UP AND EXAMINING THE DAMAGE, THE REAR LOWER
... CONTROL ARMS ROTTED ON BOTH SIDE AND COLLAPSED LIKE PRETZELS, ALLOWING THE REAR DIFFERENTIAL TO TWIST, SNAPPING THE DRIVESHAFT FLANGE WHERE THE UNIVERSAL GOES AND BLOWING OUT BOTH REAR SUSPENSION AIR SPRINGS. AS I SAID, LUCKILY IT WAITED UNTIL I WAS HOME FOR THIS TO HAPPEN. IF IT HAD HAPPEN ON ROUTE 287 ON MY WAY HOME AT 65MPH, I'M SURE THE RESULTS WOULD HAVE BEEN CATASTROPHIC. I CAN'T IMAGINE THAT I WOULD HAVE BEEN ABLE TO CONTROL THE VEHICLE. EXAMINING THE UPPER CONTROL ARMS SHOWED THEY ARE ROTTED TO! I CONTACTED THE FORD DEALER I HAVE USED FOR REPAIRS AND FORD CUSTOMER SERVICE. THE DEALERSHIP SAID THEY HAVE SEEN IT BEFORE, BUT TO THEIR KNOWLEDGE, FORD IS NOT ASSISTING FOR THIS PROBLEM. WHEN I CONTACTED FORD CUSTOMER SERVICE, THEY TOOK MY VIN NUMBER AND SAID THERE WERE NO OPEN RECALLS ON THE VEHICLE SO FORD WOULD NOT ASSIST EITHER. READING ON LINE THIS SEEMS TO BE A COMMON PROBLEM AND I THINK FORD SHOULD BEE HELD RESPONSIBLE FOR IT. I AM 49 YEARS OLD AND HAVE OWNED ALOT OF CARS, I'VE NEVER SEEN ANYTHING LIKE THIS! I WORK FOR AN AUDI DEALERSHIP, NEEDLESS TO SAY I DON'T THINK I WOULD BUY ANOTHER FORD. *TRRead more
Incident date: Nov 11, 2012
HELLO, LUCKILY I MADE IT HOME BEFORE THIS HAPPENED AS I WAS TOWING MY TRAILER WITH A COUCH AND CHAIR ON IT. I GOT HOME AND STOPPED IN FRONT OF MY HOUSE, THEN HAD TO MOVE THE TRUCK. WHEN I STEPPED ON THE GAS TO MOVE, THERE WAS A HORRENDOUS BANG, A CLUNKING NOISE AND THE REAR OF THE VEHICLE DROPPED DOWN ALMOST TO THE GROUND. UPON JACKING THE VEHICLE UP AND EXAMINING THE DAMAGE, THE REAR LOWER
... CONTROL ARMS ROTTED ON BOTH SIDE AND COLLAPSED LIKE PRETZELS, ALLOWING THE REAR DIFFERENTIAL TO TWIST, SNAPPING THE DRIVESHAFT FLANGE WHERE THE UNIVERSAL GOES AND BLOWING OUT BOTH REAR SUSPENSION AIR SPRINGS. AS I SAID, LUCKILY IT WAITED UNTIL I WAS HOME FOR THIS TO HAPPEN. IF IT HAD HAPPEN ON ROUTE 287 ON MY WAY HOME AT 65MPH, I'M SURE THE RESULTS WOULD HAVE BEEN CATASTROPHIC. I CAN'T IMAGINE THAT I WOULD HAVE BEEN ABLE TO CONTROL THE VEHICLE. EXAMINING THE UPPER CONTROL ARMS SHOWED THEY ARE ROTTED TO! I CONTACTED THE FORD DEALER I HAVE USED FOR REPAIRS AND FORD CUSTOMER SERVICE. THE DEALERSHIP SAID THEY HAVE SEEN IT BEFORE, BUT TO THEIR KNOWLEDGE, FORD IS NOT ASSISTING FOR THIS PROBLEM. WHEN I CONTACTED FORD CUSTOMER SERVICE, THEY TOOK MY VIN NUMBER AND SAID THERE WERE NO OPEN RECALLS ON THE VEHICLE SO FORD WOULD NOT ASSIST EITHER. READING ON LINE THIS SEEMS TO BE A COMMON PROBLEM AND I THINK FORD SHOULD BEE HELD RESPONSIBLE FOR IT. I AM 49 YEARS OLD AND HAVE OWNED ALOT OF CARS, I'VE NEVER SEEN ANYTHING LIKE THIS! I WORK FOR AN AUDI DEALERSHIP, NEEDLESS TO SAY I DON'T THINK I WOULD BUY ANOTHER FORD. *TRRead more
Incident date: May 1, 2012
WHEN GOING ABOUT 35 MPH THE CAR WOULD VIBRATE. SOMETIMES IT WOULD STALL AND THEN SLAM INTO GEAR. NOW THE CAR STARTED GRUMBLING AND I BELIEVE THE PROBLEM IS THE POWER TRANSFER UNIT.. THE CAR WILL DRIVE FINE WITHOUT THE DRIVE SHAFT BUT WHEN THE DRIVE SHAFT IS IN YOU CAN'T GO OVER 5 MPH AND THE CAR WILL START SHAKING AND MAKING A LOUD GRUMBLING NOISE.. LIKE WHEN YOUR GOING OVER THE RUMBLE STRIPS ON T
... HE SIDE OF THE ROAD THERE IS OBVIOUSLY A PROBLEM WITH THESE AND HOPEFULLY FORD WILL FIX IT.. *TRRead more
Incident date: Sep 27, 2012
2003 LINCOLN CONTINENTAL CARTIER. CONSUMER WRITES IN REGARDS TO PROBLEMS WITH VEHICLE WHEELS REAR AXLES *TGW THE CONSUMER STATED HE WAS ALMOST AT HIS DESTINATION, WHEN HE HEARD THE TIRES MAKING A VERY LOUD NOISE. HE EXITED THE HIGHWAY, AND AS HE TURNED THE STEERING WHEEL TO MAKE A TURN, THERE WAS A CREAKING NOISE COMING FROM UNDER THE VEHICLE. THE NEXT DAY, THE CONSUMER WENT TO THE DEALER, WHERE
... THE VEHICLE WAS PLACED ON THE RACK. IT WAS DISCOVERED THE REAR WHEEL HAD 1/2 INCH PLAY IN IT. THE REAR AXLE HAD A 1/4 INCH DEEP AND 1/4 INCH WIDE CUT. THE OTHER AXLE WAS STARTING WAS EXHIBITING THE SAME PROBLEM. THE MECHANIC STATED BOTH AXLES WOULD NEED TO BE REPLACED AND THE DAMAGE HAD CONTAMINATED OTHER COMPONENTS AND IT COULD HAVE BEEN CAUSED BY THE AXLE NOT BEING TEMPERED PROPERLY FOR HARDNESS. THE DEALER REPLACED THE REAR AXLES, BEARINGS AND SEALS. *JBRead more
Incident date: Nov 2, 2012
TL* THE CONTACT OWNS A 2011 LINCOLN MKZ. THE CONTACT STATED THAT THE VEHICLE SUDDENLY ACCELERATED WHILE SHE WAS ATTEMPTING TO PARK WITH THE BRAKE DEPRESSED. THE VEHICLE PROCEEDED TO JUMP OVER A CURB AND CAME TO A STOP WHEN IT CRASHED INTO A CEMENT PILLAR. THE CONTACT SUFFERED INJURIES TO THE BACK. A POLICE REPORT WAS FILED. THE CONTACT ALSO STATED THAT BEFORE THE FAILURE, THE ENGINE EXHIBITED A RE
... VING SOUND BUT THE CONTACT THOUGHT THAT THE NOISE WAS NORMAL. THE VEHICLE WAS TOWED TO A LOCAL COLLISION SPECIALIST. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE AND CURRENT MILEAGE WAS 18,500. UPDATED 12/21/12 *CN THE CONSUMER STATED THE VEHICLE WAS DECLARED A TOTAL LOSS. THERE WAS ALSO HEAVTY DAMAGE TO THE BUILDING. UPDATED 01/15/2013 *JSRead more
Crash
1 injured
Incident date: Nov 2, 2012
TL* THE CONTACT OWNS A 2011 LINCOLN MKZ. THE CONTACT STATED THAT THE VEHICLE SUDDENLY ACCELERATED WHILE SHE WAS ATTEMPTING TO PARK WITH THE BRAKE DEPRESSED. THE VEHICLE PROCEEDED TO JUMP OVER A CURB AND CAME TO A STOP WHEN IT CRASHED INTO A CEMENT PILLAR. THE CONTACT SUFFERED INJURIES TO THE BACK. A POLICE REPORT WAS FILED. THE CONTACT ALSO STATED THAT BEFORE THE FAILURE, THE ENGINE EXHIBITED A RE
... VING SOUND BUT THE CONTACT THOUGHT THAT THE NOISE WAS NORMAL. THE VEHICLE WAS TOWED TO A LOCAL COLLISION SPECIALIST. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE AND CURRENT MILEAGE WAS 18,500. UPDATED 12/21/12 *CN THE CONSUMER STATED THE VEHICLE WAS DECLARED A TOTAL LOSS. THERE WAS ALSO HEAVTY DAMAGE TO THE BUILDING. UPDATED 01/15/2013 *JSRead more
Crash
1 injured
Incident date: Oct 17, 2012
THE 2006 LINCOLN ZEPHYR WAS TRAVELING AT A SPEED OF 40 AND THE REAR PASSENGER TIRE SUDDENLY BLEW UP. THE MECHANIC INSPECTED THE CAUSE AND CONCLUDED THAT THE ORIGINAL ALUMINUM LINCOLN-FACTORY WHEEL WAS DEFECTIVE. THE MECHANIC ALSO INSPECTED THE OTHER THREE WHEELS AND THE SAME PROBLEM IS CONTINUING TO OCCUR WITH ALL THE 2006 LINCOLN ZEPHYR WHEELS. THE MANUFACTURING DEFECT WAS DESCRIBED BY THE MECHAN
... IC AS FOLLOWS: THE CHROME IS PEELING OFF THE WHEEL, WHICH PREVENTS A GOOD SEAL BETWEEN THE WHEEL AND THE TIRE, RESULTING IN THE LOSS OF AIR PRESSURE. THE SUDDEN LOSS OF AIR PRESSURE MAY CAUSE SERIOUS INJURY OR DEATH. *TRRead more
Crash
1 injured
Incident date: Nov 5, 2012
TL* THE CONTACT OWNS A 2010 LINCOLN MKS. THE CONTACT WAS DRIVING APPROXIMATELY 50 MPH WITH THE CRUISE CONTROL ACTIVATED. AS THE BRAKE PEDAL WAS ENGAGED, THE CRUISE CONTROL DEACTIVATED WITH AN ABNORMAL ACCELERATION. THE VEHICLE THEN CRASHED INTO ANOTHER VEHICLE. THERE WERE NO INJURIES. A POLICE REPORT WAS FILED OF THE INCIDENT. THE VEHICLE WAS TOWED TO AN INDEPENDENT AUTO MECHANIC AND HAD NOT BEEN
... DIAGNOSED FOR THE FAILURE. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM. THE APPROXIMATE FAILURE MILEAGE WAS 21,000.Read more
Crash
Incident date: Sep 11, 2012
TL* THE CONTACT OWNS A 2006 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHEN HE TURNS THE IGNITION ON THE AIR BAG LIGHT HAD ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER AND THEY ADVISED HIM THAT THE RIGHT SIDE SEAT BELT PRE TENSIONER AND BUCKLE FAILED. THE VEHICLE WAS REPAIRED FOR THAT COMPONENT. APPROXIMATELY ONE MONTH LATER THE LEFT SIDE AIR BAG WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN
... BACK TO THE DEALER AND THEY ADVISED HIM THAT THE LEFT FRONT PRE TENSIONER AND BUCKLE FAILED AND NEEDED TO BE REPLACED. THE VEHICLE HAS NOT BEEN REPAIRED. THE MANUFACTURER WAS NOT CONTACTED. THE FAILURE MILEAGE WAS APPROXIMATELY 30,000. THE CURRENT MILEAGE WAS APROXIMATELY 31,500. UPDATED 1/3/2013 *JSRead more
Incident date: Sep 11, 2012
TL* THE CONTACT OWNS A 2006 LINCOLN TOWN CAR. THE CONTACT STATED THAT WHEN HE TURNS THE IGNITION ON THE AIR BAG LIGHT HAD ILLUMINATED. THE VEHICLE WAS TAKEN TO THE DEALER AND THEY ADVISED HIM THAT THE RIGHT SIDE SEAT BELT PRE TENSIONER AND BUCKLE FAILED. THE VEHICLE WAS REPAIRED FOR THAT COMPONENT. APPROXIMATELY ONE MONTH LATER THE LEFT SIDE AIR BAG WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN
... BACK TO THE DEALER AND THEY ADVISED HIM THAT THE LEFT FRONT PRE TENSIONER AND BUCKLE FAILED AND NEEDED TO BE REPLACED. THE VEHICLE HAS NOT BEEN REPAIRED. THE MANUFACTURER WAS NOT CONTACTED. THE FAILURE MILEAGE WAS APPROXIMATELY 30,000. THE CURRENT MILEAGE WAS APROXIMATELY 31,500. UPDATED 1/3/2013 *JSRead more
Incident date: Jun 1, 2012
2006 LINCOLN ZEPHYR. CONSUMER WRITES IN REGARDS TO VEHICLE SMELLS OF FUMES WHILE DRIVING *TGW THE CONSUMER ALSO STATED THERE WAS A SMELL OF BURNING RUBBER AND FIRE COMING FROM UNDER THE VEHICLE, THROUGHOUT THE PASSENGER CABIN AND THROUGH THE CRACKS BETWEEN THE HOOD AND FENDER WHEEL. HE NOTICED THE VEHICLE WAS KNOCKING AND RUNNING ROUGH, SO HE TURNED IT OFF. HE THEN LIFTED THE HOOD, AND DISCOVERED
... SMOKE POURING OUT OF THE MOTOR. THE VEHICLE WAS TOWED TO A REPAIR SHOP. AN INSPECTION REVEALED A BAD COIL WENT BAD ON THE MOTOR, WHICH CAUSED THE ENGINE ROUGHNESS. THE COIL HAD MELTED SEVERELY. THE REPAIR SHOP INFORMED THE CONSUMER, THE COIL WOULD NOT CONNECT WITH THE COMPUTER. THE REPAIR SHOP INFORMED THE CONSUMER, THE DEALERSHIP WOULD NEED TO PROGRAM IT. THE DEALER INFORMED THE CONSUMER FIVE MORE COIL NEEDED TO BE REPLACED AS WELL AS THE COMPUTER.Read more