Showing 18,739 complaints for LINCOLN
Incident date: Jul 22, 2014
THE A/C WENT OUT, BLOWING HOT AIR. SO TOOK IT TO THE MECH. HE SAID LOOKED LIKE WEAR FROM A TUBE PLACED TO TIGHT AND NEAR THE CONDENSER RUBBED A HOLE IN IT. APPROX REPAIR COST 1500.00. WE BOUGHT THE CAR IN 2011, USED AT LYBERGERS ANCHORAGE AK,PUCHASED CUSTOM EDGE, WARRENTECH AUTO INC, BEDFORD, TX, EXTENDED WARRANTY. FOR $3000.00..SO OF COURSE AFTER A BATTLE WITH WARRENTECH, THEY DENIED CLAIM
... THEY SAID A ROCK HIT THE CONDENSER. WE WERE LOOKING FOR INFO FROM LINCOLN FOR OTHERS WITH PROBLEM OF C/C CONDENSER. THANKSRead more
Incident date: Jul 27, 2015
TL* THE CONTACT OWNS A 2013 LINCOLN MKZ. WHILE DRIVING APPROXIMATELY 50 MPH, THE FRONT PASSENGER SIDE DOOR OPENED WITHOUT WARNING. UPON INSPECTION, THE CONTACT DISCOVERED THAT THE DOOR WOULD NOT STAY CLOSED. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE DOOR LATCH WAS FAULTY. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 10,000.
Incident date: Jun 15, 2015
TL* THE CONTACT OWNS A 2008 LINCOLN MKZ. UPON STARTING THE VEHICLE, AN ABNORMAL NOISE EMITTED FROM THE ENGINE. THE CONTACT STATED THAT THIS WAS A RECURRING FAILURE. THE VEHICLE WAS INSPECTED BY AN INDEPENDENT MECHANIC AT THE CONTACT'S RESIDENCE. THE TECHNICIAN DIAGNOSED THAT THE STRUT MOUNT ON THE BOTTOM OF THE ENGINE NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOT NOTIFI
... ED OF THE FAILURE. THE FAILURE MILEAGE WAS 100,002. THE VIN WAS NOT AVAILABLE.Read more
Incident date: Jul 15, 2014
TL* THE CONTACT OWNS A 1993 LINCOLN TOWN CAR. ONCE THE VEHICLE WAS STARTED, IT BEGAN TO MAKE A JERKING MOTION AND ALL OF THE WARNING LIGHTS ILLUMINATED ON THE INSTRUMENT PANEL. THE VEHICLE STALLED. THE FAILURES RECURRED MULTIPLE TIMES. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURES. THE APPROXIMATE FAILURE MILEAGE WAS 100,000.
Incident date: Jul 15, 2014
TL* THE CONTACT OWNS A 1993 LINCOLN TOWN CAR. ONCE THE VEHICLE WAS STARTED, IT BEGAN TO MAKE A JERKING MOTION AND ALL OF THE WARNING LIGHTS ILLUMINATED ON THE INSTRUMENT PANEL. THE VEHICLE STALLED. THE FAILURES RECURRED MULTIPLE TIMES. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURES. THE APPROXIMATE FAILURE MILEAGE WAS 100,000.
Incident date: Jan 9, 2015
TL* THE CONTACT OWNS A 2013 LINCOLN MKS. WHILE DRIVING 10 MPH, THE STEERING WHEEL LOST POWER AND MADE A GROWLING NOISE AT EVERY TURN. THE VEHICLE WAS TAKEN TO A DEALER, WHERE IT WAS DIAGNOSED THAT THE STEERING WAS ERRATIC AND THAT THE POWER STEERING CONTROL (PSC) MODULE NEEDED TO BE REPROGRAMMED. THE VEHICLE WAS REPAIRED. THE FAILURE MILEAGE WAS 15,923. UPDATED 09/14/15*LJ UPDATED 12/12/2017
... *CNRead more
Incident date: Jul 28, 2015
THE CAR HAS DEVELOPED POOR RETURN TO CENTER WHEN TURNING. IT ALSO SEEMS TO BE STICKY IN NORMAL HIGHWAY DRIVING, THAT IS, A MINOR CORRECTION SEEMS TO STAY UNTIL CORRECTED THE OTHER DIRECTION. THIS MAKES THE CAR WANDER BACK AND FORTH. I HAD ONE MECHANIC IN TOWN DIAGNOSE IT AS LOWER STEERING SHAFT AND I HAVE AN APPOINTMENT WITH MY LOCAL FORD DEALER TO EVALUATE THE PROBLEM. I NOTE THERE WAS A RECA
... LL FOR THIS PROBLEM FOR 2005 AND LATER MODEL YEARS. THERE HAVE BEEN ACCIDENTS FROM STEERING FAILURE REPORTED.Read more
Incident date: Jun 2, 2015
DRIVING SLOWLY ON A SUBURBAN STREET AT TWILIGHT THE HEADLIGHTS AND DASHBOARD LIGHTS WENT OUT. THE SAME THING OCCURRED A THREE TIMES WEEK LATER ON THE INTERSTATE AT 65 MPH ABOUT 10 P.M. THE AUTOMATIC DELAYED HEADLIGHT OFF SETTING NO LONGER FUNCTIONS. THE LIGHTS CAN BE TURNED ON IN THE MANUAL POSITION.APPARENTLY, THE LIGHT CONTROL MODULE HAS FAULTY RELAYS WHICH FAIL SUDDENLY DURING THE COURSE OF NO
... RMAL USE.Read more
Incident date: Jun 2, 2015
DRIVING SLOWLY ON A SUBURBAN STREET AT TWILIGHT THE HEADLIGHTS AND DASHBOARD LIGHTS WENT OUT. THE SAME THING OCCURRED A THREE TIMES WEEK LATER ON THE INTERSTATE AT 65 MPH ABOUT 10 P.M. THE AUTOMATIC DELAYED HEADLIGHT OFF SETTING NO LONGER FUNCTIONS. THE LIGHTS CAN BE TURNED ON IN THE MANUAL POSITION.APPARENTLY, THE LIGHT CONTROL MODULE HAS FAULTY RELAYS WHICH FAIL SUDDENLY DURING THE COURSE OF NO
... RMAL USE.Read more
Incident date: Jul 26, 2015
THE BRAKES ARE VERY HARD TO PRESS AND UPON "PUMPING" ALMOST COMPLETELY FAIL. FAIL LIKE PUT THE CAR IN NEUTRAL OR DON'T STOP! STILL PASSED INSPECTION TODAY EVEN WITH THE I THINK IT IS YOUR "BOOSTER". I KNOW NOTHING BUT FOUND SEVERAL(MANY ) COMPLAINTS THAT WERE EXACTLY AS MINE. THIS IS NOT A DEFECT? THIS IS A PART THAT ALL WOULD SAY COULD OR SHOULD WEAR OUT. MY WIFE DRIVES THIS CAR ,ARE YOU KI
... DDING ME? I ALSO READ THAT IT COULD COST BETWEEN $750-$1,000 FOR THE REPLACEMENT! HOW COULD THIS NOT BE A RECALL. WE HAVE OWNED THIS VEHICLE FOR 4 YEARS AND IT WENT BAD FAST! LIKE YESTERDAY! NO HELP FROM OUR GOV?Read more
Incident date: Jun 15, 2015
TL* THE CONTACT OWNS A 2015 LINCOLN MKC. TWO WEEKS AFTER THE VEHICLE WAS PURCHASED, THE VEHICLE FAILED TO START. THE VEHICLE WAS TOWED TO A LOCAL DEALER WHERE IT WAS DIAGNOSED THAT THE BATTERY WAS FAULTY. THE BATTERY WAS REPLACED. THE FAILURE RECURRED AND THE VEHICLE WAS TOWED BACK TO THE DEALER. THE VEHICLE WAS NOT DIAGNOSED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS A
... PPROXIMATELY 3,000.Read more
Incident date: Jun 13, 2015
THE TRUCK STARTED ON FIRE AROUND THE FRONT PASSENGER SEAT WHILE I WAS DRIVING ,I PULLED OVER RESCUED MY DOG RAN TO THE GRASS AREA AND WATCH IT BURN TO THE GROUND. THIS WAS JUNE 13,2015
Fire
Incident date: Jun 2, 2014
THIS HAS BEEN A CONTINUOUS ISSUE WHEN USING THE CRUISE CONTROL AT ANY SPEED. WHEN THE CRUISE CONTROL IS ON, AND THE VEHICLE IS TRAVELING ON A DOWNHILL SLOPE, THERE IS A NOISE COMING FROM UNDER THE HOOD WHILE IT IS TRYING TO MAINTAIN THE SPEED. THE SOUND IS SOMETHING LIKE A HUMMING/GRINDING/TICKING NOISE. I HAVE HAD MULTIPLE TECHNICIANS GO FOR A DRIVE WITH ME TO TRY DIAGNOSE THE ISSUE AND THEY HAVE
... ALL SAID THAT THERE IS AN ISSUE. HOWEVER, TO DATE, THEY HAVE NOT BEEN ABLE TO FIX IT AND THE LAST TECHNICIAN SAID IT MUST BE A NORMAL NOISE, EVEN THOUGH NO OTHER LINCOLN I HAVE TEST DROVE CAN RECREATE THE NOISE.Read more
Incident date: Jul 21, 2015
OWNER OF 2005 LINCOLN AVIATOR. I WAS NOT ABLE TO GET THE GEAR SHIFT OUT OF PARK. I HAD THE AVIATOR TOWED TO A FAMILY MEMBER'S AUTOMOTIVE GARAGE AND WAS TOLD THAT I WILL NEED TO HAVE THE ENTIRE GEAR SHIFT REPLACED. UPON DOING SOME RESEARCH, IT SEEMS THAT THIS IS A VERY COMMON PROBLEM IN THIS YEAR, MAKE, AND MODEL. I HAVE READ ENDLESS TESTIMONIES FROM OTHER VEHICLE OWNERS WITH THE EXACT DISPUTE.
... THE PART AND LABOR WILL COST ME APPROXIMATELY $1100.00 AT MY FAMILY'S GARAGE, ONE CAN ONLY GUESS THE DOLLAR AMOUNT WILL DOUBLE AT THE LOCAL DEALERSHIP. MY CAR IS DRIVEABLE, HOWEVER, WHEN IN PARK, I WILL HAVE TO PUT MY EMERGENCY BRAKE ON. I WAS ALSO INFORMED THAT THE GEAR SHIFT, IF BUMPED, MAY MOVE OUT OF PARK EVEN WITHOUT THE KEY IN THE IGNITION. I AM APPALLED THAT FORD/LINCOLN MOTOR COMPANY HAS NOT TAKEN RESPONSIBILITY OF THE DEFECTED MECHANISM. IT IS UNACCEPTABLE AND RAISES MANY QUESTIONS ON HOW IMPORTANT VEHICLE SAFETY IS TO FORD/LINCOLN MOTOR COMPANY, NOT TO MENTION A TOTAL INCONVENIENCE FINANCIALLY! THIS IS MY FOURTH VEHICLE FROM FORD/LINCOLN MOTOR COMPANY AND I HIGHLY DOUBT I WILL PURCHASE ANOTHER BASED ON THE COMPANY'S LACK IN ADDRESSING THE MATTER. I AM A MOTHER OF ONE CHILD AND NOW DO NOT FEEL SECURE DRIVING A VEHICLE THAT I ONCE FELT VERY PROTECTED IN.Read more
Incident date: Jul 17, 2015
WE HAVE A FLEET OF LINCOLN TOWN CARS USED IN A GROUND TRANSPORTATION SERVICE. THE DRIVER REPORTED THAT "THE STEERING FELT (VERY) TIGHT". ANOTHER CAR WAS DISPATCHED TO COVER THE LIVERY, AND THE AFFECTED CAR WAS TOWED BACK TO OUR FACILITY. OUR SENIOR MECHANIC EXAMINED THE CAR AND THE ISSUE IS THE LOWER STEERING SHAFT ASSEMBLY. IT IS SEVERELY CORRODED, AND THE "U-JOINTS" CONTAINED IN IT ARE ALMOST I
... MPOSSIBLE TO MOVE. WE CONTACTED THE DEALER, PROVIDED THE VIN, AND WAS TOLD THERE IS NO RECALL ON THIS VEHICLE THIS IS NOT A NEW FOMOCO PROBLEM, THERE HAVE BEEN SEVERAL RECALLS OF SEVERAL OTHER YEARS (AND MODELS) FOR THE VERY ISSUE. IT IS THE EXACT SAME PART THAT HAS FAILED IN SEVERAL YEARS OF TOWN CAR (AND SIMILAR). THEY ARE PLAYING GAME WITH RECALL STATUS ON THIS VEHICLE THESE CARS (THAT ALL HAVE THE SAME STEERING SHAFT DESIGN) SHOULD BE RECALLED THE SCOPE OF THIS RECALL NEEDS TO BE EXPANDEDRead more
Incident date: Jul 20, 2015
AS I WAS GOING TO PULL OUT OF A PARALLEL PARKING SPOT, THE CAR IMMEDIATELY STALLED AND LOST ALL POWER WHILE IN DRIVE. I PLACED THE CAR IN PARK AND ATTEMPTED TO TURN THE CAR BACK ON. THE CAR TURNED BACK ON THEN AS I WAS ABOUT TO LEAVE THE PARKING SPOT AGAIN IT SHUT OFF IMMEDIATELY AS I PRESSED THE ACCELERATION. THIS IS VERY DANGEROUS AND LEFT ME OUT IN THE MIDDLE OF THE STREET WITH ON COMING TRAFFI
... C. *TRRead more
Incident date: Jul 17, 2015
I WAS DOING 65 ON THE 60 FREEWAY IN CITY OF WALNUT CA. AND ALL OF A SUDDEN MY CAR BEGAN TO ACCELERATE FULL SPEED, I LOOKED AT MY DASH JUST TO SEE IF CRUISE CONTROL WAS ON, "WHICH IT WAS NOT" SO I PRESSED THE BRAKE BUT THE CAR KEPT ON ACCELERATING SO I HAD TO HOLD THE BRAKE DOWN AS HARD AS I COULD BUT DESPITE DOING THAT I WAS DOING BETWEEN 60 AND 70 MPH, I COULD NOT EVEN GET THE CAR TO GO LESS THAN
... 60 MPH NO MATTER WHAT, MY EXIT CAME AND I COULD NOT EVEN GET OFF BY THIS TIME I HAD TO SWERVE AROUND CARS BECAUSE I COULD NOT SLOW DOWN I WAS ALREADY PANICKING I REALLY THOUGHT I WAS GOING TO DIE FINALLY AFTER A FEW MORE SECONDS THE CAR STOPPED ACCELERATING AND I WAS IN CONTROL I NEED HELP TO HAVE THIS CORRECTED AS SOON AS POSSIBLE PLEASE. THANK YOURead more
Incident date: Jul 16, 2015
I WAS ON A HIGHWAY,GOING AROUND 50~55 MILES PER HOUR.SUDDENLY I LOST POWER IN STEERING WHEEL.THERE WAS NO WARNING SIGN,NO SOUND AT ALL.I TURNED MY RIGHT SIGNAL BUT IT WAS STOPPED WORKING AS WELL.I PUT MY FLASHERS ON AND PULLED OVER TO RIGHT SHOULDER.IT WAS IMPOSSIBLE FOR ME TO MOVE A STEERING WHEEL IN EITHER DIRECTION.HAD TO TOW THE CAR BACK TO MY HOME.ON FRIDAY THE 17TH,I CALLED FORD DEALER IN QU
... EENS(,WHICH HAPPEN TO BE NEAR MY HOME)SHE PUT ME ON HOLD AND NEVER CAME BACK ON LINE.I HAD SOME IMPORTANT THINGS TO DO TODAY,WHICH I DID.I CHECKED FORD DEALERS WEB SITE IN QUEENS.THE NEXT AVAILABLE DAY IS JULY 24TH. I DRIVE FOR LIVING SO ITS IMPOSSIBLE FOR ME TO SIT HOME FOR ONE WEEK.I WILL WALK IN TO DEALER FIRST THING ON MONDAY THE 20TH OF JULY.Read more
Incident date: Feb 3, 2015
I AM ORIGINAL OWNER OF 2007 MKX. RECEIVED RECALL NOTICE IN DEC.2014. UNABLE TO GET VEHICLE TO DEALERSHIP UNTIL 02/03/15. I HAVE NOT HAD MY VEHICLE SINCE THAT DATE. CORROSION AT FUEL TANK AND LEAKING. DLR INFORMED ME THE VEHICLE CANNOT BE DRIVEN. HE HAD NO IDEA WHEN THE PART(S) WOULD BE AVAILABLE. IT WOULD BE MONTHS. I WAS PROVIDED INITIALLY WITH VEHICLE FROM DEALERSHIP. AFTER WEEK OR SO I WAS HAND
... ED OVER TO RENTAL AGENCY AT FORD'S EXPENSE. I AM NOW IN MY 3RD VEHICLE AS OF JUNE. HAVE CONTACTED FORD MOTOR COMPANY NUMEROUS TIMES SINCE EARLY FEB. WHO APOLOGIZES PROFUSELY AND SAY THEY DO NOT KNOW WHEN TANKS WILL BE AVAILABLE. THEY ARE AT MERCY OF THEIR SUPPLIER. NO DATES MAYBE LATE SUMMER. RECALL NOTICE INDICATES 3RD QTR. DEALERSHIP AS OF 7/7/15 SAYING FOURTH QTR. NO EXACT DATE OR TIME. I PURCHASED THAT VEHICLE FOR INTENDED USE WITH BUSINESS AND FAMILY. FAMILY MEMBERS UNDER 25 AND FREQUENT OUT OF TOWN FAMILY GUESTS CANNOT DRIVE THE RENTAL AND UNTIL EARLY JUNE PREVIOUS VEHICLES I HAD DID NOT MEET MY BUSINESS NEEDS. THIS HAS BEEN AN UNREASONABLE AND UNACCEPTABLE AMOUNT OF TIME. I AM VERY CONCERNED HOW MY VEHICLE WILL OPERATE AFTER HAVING BEEN IDLE FOR MANY MONTHS, NEARLY A YEAR. FORD MOTOR SHOULD PURCHASE THESE VEHICLES AT FMV WITH ADDITIONAL AMOUNT COVERING THE RENTAL PAYOUTS AND THE INCONVENIENCE THROUGH THEIR UNKNOWN REPAIR DATE. THEY MIGHT STILL HAVE SATISFIED CUSTOMERS. ONLY OFFER THEY HAVE COME UP WITH IN EARLY APRIL HAS BEEN DEALER VALUE + $2500.00 TOWARDS ANOTHER FORD PRODUCT. NOT ACCEPTABLE.Read more
Incident date: Apr 1, 2014
TL* THE CONTACT OWNS A 2003 LINCOLN AVIATOR. WHILE SHIFTING INTO REVERSE, THE VEHICLE HESITATED. THE VEHICLE WAS TOWED TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE TRANSMISSION SHIFTER CABLE FRACTURED AND NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED; HOWEVER, SEVERAL MONTHS AFTER THE REPAIR, THE CONTACT WAS MADE AWARE OF NHTSA CAMPAIGN NUMBER: 02V313000 (POWER TRAIN). THE MANUFACTURER WAS NOTI
... FIED OF THE FAILURE AND STATED THAT THE VEHICLE WAS NOT INCLUDED IN THE RECALL. THE FAILURE MILEAGE WAS 90,000.Read more
Incident date: Jul 9, 2015
TL* THE CONTACT OWNS A 2004 LINCOLN AVIATOR. WHILE DRIVING APPROXIMATELY 60 MPH, THE AIR BAGS DEPLOYED INADVERTENTLY. THERE WAS NO CRASH INVOLVED. THE VEHICLE WAS TAKEN TO A DEALER WHERE THEY DIAGNOSED THAT THERE WAS A CRASH DETECTION. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 59,000.
Incident date: Jun 1, 2015
TL* THE CONTACT OWNS A 2002 LINCOLN LS. THE CONTACT STATED THAT THE TRANSMISSION WAS SLIPPING OUT OF GEAR. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHO REPLACED THE TRANSMISSION. IN ADDITION, THE VEHICLE WAS OVERHEATING WITHOUT WARNING. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO REPLACED THE THERMOSTAT, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE A
... PPROXIMATE FAILURE MILEAGE WAS 125,000.Read more
Incident date: Jun 1, 2015
TL* THE CONTACT OWNS A 2002 LINCOLN LS. THE CONTACT STATED THAT THE TRANSMISSION WAS SLIPPING OUT OF GEAR. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHO REPLACED THE TRANSMISSION. IN ADDITION, THE VEHICLE WAS OVERHEATING WITHOUT WARNING. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO REPLACED THE THERMOSTAT, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE A
... PPROXIMATE FAILURE MILEAGE WAS 125,000.Read more
Incident date: Jul 2, 2015
THE INTAKE MANIFOLD ON MY 1999 LINCOLN TOWN CAR DEVELOPED A CRACK AND BEGAN LEAKING ALL OVER THE ENGINE . WE BOUGHT THE CAR IN 2008 AND THE MANIFOLD HAD NOT BEEN CHANGED AND WE KNEW NOTHING OF THE "SETTLEMENT" WITH FORD TO REPLACE THEM.. I CONTACTED FORD AND THEY TOLD ME THAT AGREEMENT ENDED MARCH 16, 2006.. NOW THE FORD DEALER WANTS $1000 TO REPLACE IT.. WHY SHOULD THE CAR OWNER HAVE TO PAY AN E
... XCESSIVE AMOUNT WHEN FORD IS RESPONSIBLE FOR INSTALLING PLASTIC IN AN ENGINE COMPARTMENT THAT GETS HOT AND IS BOUND TO CRACK AT SOME POINT.. JUST A WARNING .. DON'T BUY A TOWN CAR WITHOUT CHECKING ON RECALLS, BULLETINS, AND SETTLEMENTS...Read more
Incident date: Jul 7, 2015
TL* THE CONTACT OWNS A 2000 LINCOLN LS. WHILE DRIVING APPROXIMATELY 5 MPH, THE CONTACT FELT A VIBRATION FROM THE FLOOR OF THE VEHICLE AND NOTICED AN ABNORMAL NOISE COMING FROM THE FRONT END OF THE VEHICLE. THE VEHICLE WAS TAKEN TO A MECHANIC WHO STATED THAT THE LOWER BALL JOINT AND LOWER CONTROL ARM NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAI
... LURE. THE APPROXIMATE FAILURE MILEAGE WAS 157,000.Read more
Incident date: May 5, 2015
LOUD GRADING NOISE FRONT PASSAGE WHEEL
Incident date: May 5, 2015
LOUD GRADING NOISE FRONT PASSAGE WHEEL
Incident date: Jul 6, 2015
THE DRIVERS AND PASSENGER SEATS TILT BACKWARDS DURING ACCELERATION (USUALLY HARD START). THE SEATS WOULD ALSO TILT FORWARD ON HARD BRAKING. AFTER SOME RESEARCH ONLINE, I FOUND A LOT OF FORD AND LINCOLN OWNERS COMPLAINING ABOUT THE ISSUE ON BOTH LOW AND HIGH MILEAGE CARS. IT SEEMS TO BE A COMMON PROBLEM ON ALL LINCON MKX AND FORD EDGE. IT SEEMS FROM THE COMMENTS ON VARIOUS ONLINE FORUMS THE PROBLE
... M IS MORE COMMON IN CARS WITH POWER SEATS. I AM AFRAID THAT WITH THE "PLAY" IN THE SEAT TRACKS, THE CAR WOULD BECOME UNSAFE DURING AN ACCIDENT. IT SEEMS SOME FORD DEALERSHIP ARE AWARE OF THIS ISSUE ALREADY AND CONSIDER IT "NORMAL" BEHAVIOR, SOME ARE FIXING IT UNDER WARRANTY. OWNERS WITH NO WARRANTY ARE EXPOSED TO POTENTIALLY DANGEROUS DEFECT OF THE VEHICLE.Read more
Incident date: Jul 2, 2015
THE CAR WAS IDLING AS I WAS PREPARING TO LEAVE MY EMPLOYER'S PARKING LOT. MY FOOT WAS ON THE BRAKE. AT THE MOMENT I SHIFTED THE CAR INTO DRIVE, THE ENGINE RACED AND LUNGED FORWARD. WITH MY FOOT FIRMLY ON THE BRAKE, THE REAR TIRES SCREECHED, BUT THE BRAKES KEPT THE CAR FROM MOVING MORE THAN SEVERAL FEET.. WITHIN SEVERAL SECONDS, I WAS ABLE TURN OFF THE KEY AND RETURN THE SHIFT LEVER TO PARK. I TR
... IED TO DUPLICATE THE PROBLEM IN A SAFE AREA, BUT COULD NOT. MY FOOT WAS NOT ON BOTH PEDALS (BRAKE AND ACCELERATOR) SIMULTANEOUSLY AS THE ENGINE WAS AS IDLING WHEN I SHIFTED INTO DRIVE. THERE IS NO FLOOR MAT TO INTERFERE WITH NORMAL OPERATION. THE BRAKE PEDAL WAS IN A "RAISED" POSITION- A FEATURE OF THE CAR. I WAS NOT FAMILIAR WITH THE "SUDDEN ACCELERATION" PROBLEM OTHER DRIVERS HAD REPORTED PREVIOUSLY, BUT I DID READ ABOUT PROBLEMS ASSOCIATED WITH THE RAISED BRAKE PEDAL AND THE CLOSE PROXIMITY OF THE ACCELERATOR PEDAL (WITHIN THE PAST FEW DAYS). BEFORE RESEARCHING THE POSSIBLE CAUSE OF THIS INCIDENT, I THOUGHT THE PROBLEM MIGHT HAVE BEEN ASSOCIATED WITH THE LINKAGE OF THE TWO PEDALS. NOW, I'M CONVINCED THE ISSUE WILL NOT BE AN EASY FIX.Read more
Incident date: Jun 28, 2015
TL* THE CONTACT OWNS A 2003 LINCOLN NAVIGATOR. WHILE ATTEMPTING TO SHIFT, THE TRANSMISSION FAILED TO SHIFT INTO THE PARK POSITION. THE CONTACT STATED THAT THE DRIVER HAD TO ENGAGE THE EMERGENCY BRAKE IN ORDER TO PREVENT THE VEHICLE FROM ROLLING AWAY. THE VEHICLE WAS NOT TAKEN TO A DEALER OR DIAGNOSED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 158,000.
Incident date: Jan 16, 2015
TL* THE CONTACT OWNED A 2009 LINCOLN MKZ. WHILE DRIVING AT 60 MPH, ANOTHER VEHICLE CRASHED INTO THE REAR PASSENGER SIDE OF THE CONTACT'S VEHICLE, CAUSING IT TO CRASH INTO THE GUARDRAIL. THE CONTACT MENTIONED THAT THE AIR BAGS DEPLOYED WITH EXCESSIVE FORCE AND BURNED THE CONTACT'S NECK. THE CONTACT REQUIRED MEDICAL ATTENTION. A POLICE REPORT WAS FILED. THE VEHICLE WAS DESTROYED AND TOWED TO A SALVA
... GE YARD. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 116,000.Read more
Crash
1 injured
Incident date: Jun 29, 2015
RECEIVED AN "IMPORTANT SAFETY RECALL" LETTER, CALLED THE DEALER TO SETUP AN APPT, AND LEARNED THAT THE PARTS ARE NOT AVAILABLE. I THEN CALL FORD CORP, AND THEY COULD NOT GIVE ME AN ESTIMATE OF WHEN THE PARTS WILL BE AVAILABLE. FORD CORP TOLD ME THAT IF I HAD THE CURRENT PROBLEMS WITH STEERING, THEN THEY MIGHT BE ABLE TO ACCELERATE THE PARTS. I AM NOT HAVING CURRENT PROBLEMS, BUT THIS IS RIDI
... CULOUS SINCE THE CAR IS BEING RECALLED TO AVOID THE PROBLEMS....SAFETY RECALL NOTICE 15S14 NHTSA RECALL 15V-250..UPDATED 11/12/15 *BF THE CONSUMER STATED THE ISSUE WAS RESOLVED. UPDATED 12/15/15. *JBRead more
Incident date: Apr 30, 2015
AS PART OF THE RECENT FORD STEERING RECALL, AN EMERGENCY INSPECTION WAS DONE ON 11/18/13 AT 69,104 AND DECLARED SAFE TO DRIVE. ON 3/18/14 DRIVING TO THE DEALER TO HAVE RECALL WORK PERFORMED, THE STEERING COLUMN LOCKED-UP SOLID AT THE TURN WAS MADE ENTERING THE DEALERS PROPERTY.A REPAIR WAS DONE REPLACING THE LOWER SHAFT ONLY AS SHOWN IN PICTURE #1. THEN LESS THAN 14 MONTHS LATER A REPEAT FAILURE O
... F THE UPPER SHAFT ASSEMBLY SHOWN IN PICTURE #2. THERE WAS NO SECONDARY RECALL ISSUED, SO A SEARCH BY VIN SHOWED NO OUTSTANDING RECALL, AND THE DEALERS INSISTENT ED THIS WAS NOT A RECALL ISSUE, BUT. IT WAS, AS THE COMPLETE UPPER AND LOWER SHAFT SHOULD HAVE BEEN REPLACED DURING THE REPAIR. THE UNPREDICTABLE LOCKING OF THE STEERING WHEEL POSES A SERIOUS INJURY/DEATH RISK. ALL VEHICLES PART OF THE INITIAL RECALL SHOULD BE INSPECTED TO INSURE THE REPAIR WAS DON COMPLETELY AND CORRECTLY. PICTURES AVAILABLE ON REQUEST (CAN'T SEEM TO ATTACH N THIS FORM) ALSO SEE PREVIOUS FOR FILED WHEN FIRST FAILURE OCCURRED DESPITE INSPECTION THAT DECLARED VEHICLE SAFE TO DRIVE.Read more
Crash
Incident date: Apr 30, 2015
AS PART OF THE RECENT FORD STEERING RECALL, AN EMERGENCY INSPECTION WAS DONE ON 11/18/13 AT 69,104 AND DECLARED SAFE TO DRIVE. ON 3/18/14 DRIVING TO THE DEALER TO HAVE RECALL WORK PERFORMED, THE STEERING COLUMN LOCKED-UP SOLID AT THE TURN WAS MADE ENTERING THE DEALERS PROPERTY.A REPAIR WAS DONE REPLACING THE LOWER SHAFT ONLY AS SHOWN IN PICTURE #1. THEN LESS THAN 14 MONTHS LATER A REPEAT FAILURE O
... F THE UPPER SHAFT ASSEMBLY SHOWN IN PICTURE #2. THERE WAS NO SECONDARY RECALL ISSUED, SO A SEARCH BY VIN SHOWED NO OUTSTANDING RECALL, AND THE DEALERS INSISTENT ED THIS WAS NOT A RECALL ISSUE, BUT. IT WAS, AS THE COMPLETE UPPER AND LOWER SHAFT SHOULD HAVE BEEN REPLACED DURING THE REPAIR. THE UNPREDICTABLE LOCKING OF THE STEERING WHEEL POSES A SERIOUS INJURY/DEATH RISK. ALL VEHICLES PART OF THE INITIAL RECALL SHOULD BE INSPECTED TO INSURE THE REPAIR WAS DON COMPLETELY AND CORRECTLY. PICTURES AVAILABLE ON REQUEST (CAN'T SEEM TO ATTACH N THIS FORM) ALSO SEE PREVIOUS FOR FILED WHEN FIRST FAILURE OCCURRED DESPITE INSPECTION THAT DECLARED VEHICLE SAFE TO DRIVE.Read more
Crash
Incident date: Jun 15, 2015
APPROXIMATELY MARCH OF 2013. I WAS DRIVING NORTH ON MOULTON BLVD, SUDDENLY THE CAR LOST SPEED AND A RED TRIANGLE SHAPED CAME ON AND STATED "DRIVE TO SIDE OF ROAD SAFELY AND SHUT OFF THE CAR ENGINE" I TOOK IT TO LINCOLN GARAGE AND THEY KEPT MY CAR FOR A WEEK, WAITING FOR DIRECTIONS OF PROCEDURE FROM DETROIT, THEY TOLD ME THEY HAD REPLACED THE HYBRID BATTERY. THE CAR RAN GREAT AGAIN. JUNE 15, 201
... 5 IT SHUT DOWN AGAIN, LIKE BEFORE, I TOOK IT TO THE LINCOLN DEALER, THEY SAID THERE WERE NOT ANY CODES, BUT TOLD ME IT WAS A BAD THROTTLE BODY, OF WHICH THEY CHANGED. JUNE 24,2015, THE CAR SHUT DOWN AGAIN, THE RED TRIANGLE SHAPE LIGHT CAME ON, TOOK IT INTO LINCOLN DEALER THE SAME DAY, THEY TOLD ME THE COMPUTER SAID THE CAR SHUT DOWN, BUT NO COMPUTER CODES. THIS MAKES ME THINK THAT A NEW THROTTLE BODY WAS NOT NECESSARY. A LINCOLN TECHNICIAN HAS BEEN DRIVING MY AUTOMOBILE FOR THE LAST FEW DAYS AND WILL DO SO OVER THIS WEEK-END. HE HAS A COMPUTER ATTACHED TO THE AUTO ENGINE, LOOKING FOR THE CAUSE. WHEN THE CAR SHUTS DOWN, PRESSING THE ACCELERATOR GETS NO RESPONSE.Read more
Incident date: Jun 15, 2015
APPROXIMATELY MARCH OF 2013. I WAS DRIVING NORTH ON MOULTON BLVD, SUDDENLY THE CAR LOST SPEED AND A RED TRIANGLE SHAPED CAME ON AND STATED "DRIVE TO SIDE OF ROAD SAFELY AND SHUT OFF THE CAR ENGINE" I TOOK IT TO LINCOLN GARAGE AND THEY KEPT MY CAR FOR A WEEK, WAITING FOR DIRECTIONS OF PROCEDURE FROM DETROIT, THEY TOLD ME THEY HAD REPLACED THE HYBRID BATTERY. THE CAR RAN GREAT AGAIN. JUNE 15, 201
... 5 IT SHUT DOWN AGAIN, LIKE BEFORE, I TOOK IT TO THE LINCOLN DEALER, THEY SAID THERE WERE NOT ANY CODES, BUT TOLD ME IT WAS A BAD THROTTLE BODY, OF WHICH THEY CHANGED. JUNE 24,2015, THE CAR SHUT DOWN AGAIN, THE RED TRIANGLE SHAPE LIGHT CAME ON, TOOK IT INTO LINCOLN DEALER THE SAME DAY, THEY TOLD ME THE COMPUTER SAID THE CAR SHUT DOWN, BUT NO COMPUTER CODES. THIS MAKES ME THINK THAT A NEW THROTTLE BODY WAS NOT NECESSARY. A LINCOLN TECHNICIAN HAS BEEN DRIVING MY AUTOMOBILE FOR THE LAST FEW DAYS AND WILL DO SO OVER THIS WEEK-END. HE HAS A COMPUTER ATTACHED TO THE AUTO ENGINE, LOOKING FOR THE CAUSE. WHEN THE CAR SHUTS DOWN, PRESSING THE ACCELERATOR GETS NO RESPONSE.Read more
Incident date: Jun 12, 2015
MY 2004 LINCOLN NAVIGATOR DROPPED DOWN ON THE DRIVERS SIDE FRONT. I TOOK IT TO A MECANIC AND HE SAID IT WAS THE HEIGHT SENSOR IN THE MEANWHILE WHILE THEY ORDERED THE PART AND A WEEK LATER IT GOT TO THE SHOP I DROVE IT AND OF COURSE WITH ALL THE BUMPING AROUND THE FRONT PASSENGER SIDE DROPPED NOW THE LINCOLN REALLY BOUNCES I TOOK IT TO THE SHOP TO GET THE SENSOR INSTALLED WENT BACK TO PICK IT THEY
... TELL ME THAT WASNT THE PROBLEM NOW MY PUMP DONT WORK AND MY FRONT END IS REALLY LOW. NOW IM STUCK WITH NO SUSPENSION AND SOMETHING MORE THAN LIKELY IS GOING TO HAPPEN EITHER A BLOWN TIRE BECAUSE OF THE RUBBING ON THE TIRE WALL OR A CAR ACCIDENT. THIS IS MY DAILY DRIVER BACK AND FORTH TO WORK I ALSO AM AFRAID TO TAKE MY THREE CHILDREN ANYWHERE BECAUSE OF THIS. IM AND EMPLOYEE OF GM SOMEONE NEEDS TO DO A RECALL THIS IS A SAFETY ISSUE TO THE DRIVER AND OTHER DRIVERS AS WELL.Read more
Incident date: Dec 13, 2013
MY WIFE AND I WERE INVOLVED IN A COLLISION AFTER A WOMAN, WHO CLAIMS TO HAVE FALLEN ASLEEP, SIDESWIPED THE CAR IMMEDIATELY AHEAD OF US ON A 2-LANE ROAD. IN AN ATTEMPT TO AVOID A HEAD-ON COLLISION, I SWERVED OFF THE ROAD TO THE RIGHT. SHE ACCELERATED, TURNED LEFT AND GOT IN FRONT OF US AND WE COLLIDED WITH HE RIGHT FRONT FENDER AT THE WHEEL-WELL. THE CAR WAS TOTALED. THE AIRBAGS DEPLOYED AND THE FR
... ONT END WAS CRUSHED. I WAS DRIVING AND MY LEFT ARM WAS BROKEN. THE LITTLE AIRBAG IN THE STEERING COLUMN HIT ME IN THE CHEST, BRUISED ME, AND CAUSED SEVERE PAIN. MY WIFE WAS IN THE FRONT PASSENGER SEAT. HER SEATBELT WAS SECURELY FASTENED, BUT IT DID NOT HOLD HER IN PLACE AS IT WAS DESIGNED TO DO. ON IMPACT, SHE MET THE AIRBAG HALFWAY AND MOST OF HER RIBS WERE FRACTURED. FOUR (4) OF HER VERTEBRAE WERE FRACTURED, AS WAS HER RIGHT ANKLE. HER LUNGS WERE BRUISED AND ONE WAS PUNCTURED. HER LEFT KNEE HIT THE DASHBOARD AND DROVE HER FEMUR THROUGH HER PELVIS. SHE WAS TAKEN TO UMD SHOCK-TRAUMA CENTER WHERE SHE WAS INTUBATED, SEDATED AND PUT IN TRACTION FOR SEVERAL DAYS BEFORE A 7 HOUR SURGERY TO REBUILD HER HIP AND FEMUR. SHE WAS IN A FULL-TORSO CAST AND USED A WHEELCHAIR FOR >6 WEEKS. SHE IS STILL REBOUNDING FROM THE EFFECTS OF THE INEFFECTIVE SEATBELT, WHICH DID NOT WORK AS DESIGNED.Read more
Crash
2 injured
Incident date: Jun 25, 2015
I GOT TO WORK AND I COULDN'T OPEN MY DRIVER'S SIDE DOOR TO EXIT THE CAR. I TRIED LOCKING AND UNLOCKING, USING THE KEY FAB TO LOCK AND UNLOCK AND EVENTUALLY I HAD TO CLIMB OVER THE PASSENGER SEAT AND EXIT VIA THE PASSENGER DOOR.
Incident date: Oct 9, 2014
WHEN DRIVING FROM UP GRADE AT ABOUT 1200 RPM, THERE IS A RATTLE NOISE COMING FROM ENGINE
Incident date: Feb 16, 2015
WHEN AIR CONDITION IS SET BELOW 72, PASSENGER FRONT SIDE IS MAKING LOUD CLICKING NOISE FOR ABOUT 1 MINUTE THEN GOES AWAY.
Incident date: May 1, 2015
FRONT PASSENGER WINDOW WILL NOT OPEN OR CLOSE. IF ATTEMPTED, WINDOW WILL MAKE CRACKING NOISE.
Incident date: Jun 16, 2015
IN THE LAST FIVE YEARS MY 255/ 75 17 CONTITRAC TIRES 5 OF THEM HAVE BLOWN OUT OR COME APART IN SOME MANNER! THE LAST TIME A FEW DAYS AGO WAS PRETTY CLOSE TO A HIGH SPEED ACCIDENT 65MPH THERE IS AN ABSOLUTE MAJOR PROBLEM WITH THESE TIRES !! THIS IS THE SECOND SET THAT HAS BEEN ON THIS TRUCK~! CONTINENTAL NO LONGER MAKES THIS SIZE AND THEY ARE NON RESPONSIVE TO MY COMPLAINTS PLEASE HELP.
Incident date: Feb 25, 2015
2014 LINCOLN MKZ. CONSUMER WRITES IN REGARDS TO VEHICLE TIRE ISSUES AND REIMBURSEMENT FOR TIRE REPLACEMENTS. *SMD THE CONSUMER STATED THE VEHICLE DID NOT PASS INSPECTION, BECAUSE A BUBBLE HAD FORMED ON THE RIGHT FRONT TIRE IN THE SIDEWALL. THE TIRE WAS REPLACED AT A COST OF $ 250. ON MARCH 16, 2015, THE RIGHT REAR TIRE WAS REPLACED DUE TO A BUBBLE FOUND IN THE SIDEWALL. ON MAY 13, 2015 DURIN
... G A SERVICE VISIT AT THE DEALER, THE CONSUMER WAS INFORMED THE FRONT TIRES HAD SIDEWALL BUBBLES AND NEEDED TO BE REPLACED. *JB THE CONSUMER STATED FIVE TIRES OVER THE LAST FOUR MONTHS HAD SIDEWALL BUBBLES. UPDATED 02/01/16.*JBRead more
Incident date: Feb 2, 2015
TL* THE CONTACT OWNS A 2012 LINCOLN MKZ. WHILE DRIVING APPROXIMATELY 40 MPH, THE STEERING WHEEL SEIZED WITHOUT WARNING AND EXCESSIVE FORCE WAS REQUIRED. AS A RESULT OF THE FAILURE, THE VEHICLE DROVE ONTO A CURB AND FRACTURED THE RIMS AND TIRES. THE FAILURE RECURRED MULTIPLE TIMES. THE VEHICLE WAS TAKEN TO THE DEALER, BUT THEY COULD NOT DIAGNOSE THE FAILURE. THE TIRES WERE REPLACED. THE MANUFACTURE
... R WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 29,000.Read more
Incident date: Jul 9, 2014
ALTHOUGH THE VEHICLE HAD ONLY 15,000 MILES ON IT, THE DEALER REPORTED TO ME THAT A TIRE REPLACEMENT WAS RECOMMENDED THESE WERE ORIGINAL EQUIPMENT MICHELIN TIRES..AFTER INSPECTION, MICHELIN AGREED TO REPLACE TIRES FOR A FEE OF $100 PER TIRE.
Incident date: May 15, 2015
ELECTRICAL SHORT IN THROTTLE BODY. THE VEHICLE WOULD STOP AT ANYTIME WHILE DRIVING. PULLED OFF STREET AND RE-STARTED. INCIDENT HAPPENED FOUR TIMES.....UPDATED 07/23/15 *BF *TR
Incident date: Jun 20, 2015
TL* THE CONTACT OWNS A 2010 LINCOLN MKZ. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 20 MPH, THE FRONT DRIVER SIDE DOOR OPENED INDEPENDENTLY. IN ADDITION, THE CONTACT STATED THAT THE FRONT DRIVER SIDE DOOR FAILED TO RELATCH. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND STATED THAT THE VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 15V246000 (L
... ATCHES/LOCKS/LINKAGES). THE FAILURE MILEAGE WAS 117,000.Read more
Incident date: Jun 1, 2015
THE GAS TANK HAS CORRODED SO I HAVE GAS LEAKING UNDER MY VEHICLE. THE MAINTENANCE MAN TOLD ME I COULD NOT DRIVE IT DUE TO DANGER OF A SPARK AND FIRE RISK. THE 2007 AND 2008'S HAVE THIS SAME PROBLEM WHICH ARE RECALLED SO WHY AREN'T THE 2009'S AS WELL. IT IS THE SAME FAULTY GAS TANK.
Incident date: Jun 16, 2015
WHILE DRIVING 55 MPH ON HIGHWAY, RED TRIANGLE WITH "!" IN THE MIDDLE WITH TEXT "STOP SAFELY NOW" APPEARED ON DASHBOARD. AT THE SAME TIME THE ENGINE SHUT OFF (ALONG WITH THE AIR CONDITIONER AND RADIO). THE CAR WOULD NOT RESTART IN NEUTRAL. I HAD TO COAST TO THE SHOULDER OF THE HIGHWAY TO STOP, PUT THE CAR IN PARK, TURN THE KEY TO RESTART AND THEN DRIVE AGAIN. THIS HAPPENED 3 TIMES IN 45 MINUTES
... . I TOOK THE CAR TO A LINCOLN DEALERSHIP. THEY COULD NOT FIND ANYTHING WRONG OTHER THAN RECOMMENDING I PURCHASE A NEW BATTERY. I WAS SKEPTICAL, BUT DID SO JUST IN CASE. I PICKED UP THE CAR ON 6/16/15. ON 6/19/15 THE CAR TURNED OFF AGAIN WHILE DRIVING ON A HIGHWAY. THIS HAD HAPPENED PREVIOUSLY IN 2013 AND 2014. BOTH TIMES THE DEALERSHIP COULD NOT FIND ANYTHING WRONG WITH THE CAR. IT IS NOT SAFE FOR A CAR TO TURN OFF ON A HIGHWAY.Read more