Showing 15,126 complaints for LEXUS
Incident date: Aug 26, 2015
I WAS DRIVING ON A ROAD, MY VEHICLE BEGAN TO SHAKE UNTIL EVENTUALLY DROPPING TO THE ROAD AND DRAGGING UNTIL I COULD GAIN CONTROL OF IT , BY APPLYING THE BRAKES. I NOTICED OUT OF MY DRIVER'S SIDE WINDOW ACROSS THE ROAD WAS MY TIRE ROLLING AT A RAPID SPEED. I CALLED 911 TO RECEIVE ASSISTANCE TO STOP THE TRAFFIC AND TO HELP WITH MY DISABLED VEHICLE. OFFICERS ASSISTED WITH HELPING MYSELF, MY MOTHER AN
... D MY TWO TODDLERS OUT OF THE VEHICLE AND TO RETRIEVE MY TIRE. THE TIRE HAD FALLEN OFF OF MY VEHICLE, AT THE RIM, LEAVING THE BOLTS AND THE MIDDLE PORTION OF THE RIM STILL ATTACHED TO THE VEHICLE, WHILE THE REMAINING MAJORITY OF THE RIM WAS STILL ATTACHED TO MY TIRE ROLLING DOWN THE ROAD. THE VEHICLE WAS IN PROPER WORKING CONDITION PRIOR TO THIS INCIDENT. I DID NOT HIT A POTHOLE NOR WAS I IN AN ACCIDENT. MY VEHICLE WAS TOWED TO MY RESIDENCE, THE FOLLOWING DAY AFTER CONTACTING LEXUS AND ADVISING THEM OF THE INCIDENT, I WAS INSTRUCTED BY LEXUS TO HAVE THE VEHICLE TOWED TO THEIR PROPERTY FOR AN INSPECTION. AFTER THE VEHICLE ARRIVED TO THEIR PROPERTY, THEY CONTACTED ME AND STATED THAT THE THE INCIDENT WAS NOT A MANUFACTURERS DEFECT, THAT HAD IT BEEN A MANUFACTURES DEFECT IT WOULD HAVE HAPPENED WITHIN THE FIRST YEAR THE VEHICLE WAS MANUFACTURED. LEXUS THEN INFORMED MYSELF THAT I NEEDED TO MAKE A CLAIM WITH MY INSURANCE COMPANY FOR DAMAGES THAT HAVE BEEN INCURRED. PRIOR TO THIS INCIDENT THIS VEHICLE WAS IN PERFECT WORKING ORDER. ALL PREVIOUS SERVICES WERE PERFORMED BY AUTO LENDERS AND THE MOST RECENT WAS JUNE 23, 2015, WHEN A ROUTINE OIL AND FILTER CHANGE OCCURRED, AS WELL AS, THE BRAKE PADS AND ROTORS BEING REPLACED. THE SAFETY OF OURSELVES AND OUR CHILDREN ARE A GREAT CONCERN GOING FORWARD IN THIS VEHICLE AND WE DO NOT FEEL THAT THE MANUFACTURER IS IN FACT CONCERNED WITH OUR SAFETY AND WELL BEING AND IF THIS IS AN ISSUE WITH OTHER LEXUS VEHICLES, IT IS A SAFETY CONCERN FOR ALL.Read more
Incident date: Aug 26, 2015
I WAS DRIVING ON A ROAD, MY VEHICLE BEGAN TO SHAKE UNTIL EVENTUALLY DROPPING TO THE ROAD AND DRAGGING UNTIL I COULD GAIN CONTROL OF IT , BY APPLYING THE BRAKES. I NOTICED OUT OF MY DRIVER'S SIDE WINDOW ACROSS THE ROAD WAS MY TIRE ROLLING AT A RAPID SPEED. I CALLED 911 TO RECEIVE ASSISTANCE TO STOP THE TRAFFIC AND TO HELP WITH MY DISABLED VEHICLE. OFFICERS ASSISTED WITH HELPING MYSELF, MY MOTHER AN
... D MY TWO TODDLERS OUT OF THE VEHICLE AND TO RETRIEVE MY TIRE. THE TIRE HAD FALLEN OFF OF MY VEHICLE, AT THE RIM, LEAVING THE BOLTS AND THE MIDDLE PORTION OF THE RIM STILL ATTACHED TO THE VEHICLE, WHILE THE REMAINING MAJORITY OF THE RIM WAS STILL ATTACHED TO MY TIRE ROLLING DOWN THE ROAD. THE VEHICLE WAS IN PROPER WORKING CONDITION PRIOR TO THIS INCIDENT. I DID NOT HIT A POTHOLE NOR WAS I IN AN ACCIDENT. MY VEHICLE WAS TOWED TO MY RESIDENCE, THE FOLLOWING DAY AFTER CONTACTING LEXUS AND ADVISING THEM OF THE INCIDENT, I WAS INSTRUCTED BY LEXUS TO HAVE THE VEHICLE TOWED TO THEIR PROPERTY FOR AN INSPECTION. AFTER THE VEHICLE ARRIVED TO THEIR PROPERTY, THEY CONTACTED ME AND STATED THAT THE THE INCIDENT WAS NOT A MANUFACTURERS DEFECT, THAT HAD IT BEEN A MANUFACTURES DEFECT IT WOULD HAVE HAPPENED WITHIN THE FIRST YEAR THE VEHICLE WAS MANUFACTURED. LEXUS THEN INFORMED MYSELF THAT I NEEDED TO MAKE A CLAIM WITH MY INSURANCE COMPANY FOR DAMAGES THAT HAVE BEEN INCURRED. PRIOR TO THIS INCIDENT THIS VEHICLE WAS IN PERFECT WORKING ORDER. ALL PREVIOUS SERVICES WERE PERFORMED BY AUTO LENDERS AND THE MOST RECENT WAS JUNE 23, 2015, WHEN A ROUTINE OIL AND FILTER CHANGE OCCURRED, AS WELL AS, THE BRAKE PADS AND ROTORS BEING REPLACED. THE SAFETY OF OURSELVES AND OUR CHILDREN ARE A GREAT CONCERN GOING FORWARD IN THIS VEHICLE AND WE DO NOT FEEL THAT THE MANUFACTURER IS IN FACT CONCERNED WITH OUR SAFETY AND WELL BEING AND IF THIS IS AN ISSUE WITH OTHER LEXUS VEHICLES, IT IS A SAFETY CONCERN FOR ALL.Read more
Incident date: May 7, 2015
AFTER STARTING ENGINE WE BEGAN TO HEAR CRACKLING NOISES SIMILAR TO ELECTRICAL SOUNDS. THIS PERSISTED FOR ABOUT 30 MINUTES. WE VISITED OUR DEALER AND WERE TOLD THAT IT IS NORMAL. WE DO NOT BELIEVE THIS. THE CRACKLING NOISES WOULD ONLY BE EVIDENT FOR A SHORT TIME AFTER THIS. NOW WE ARE HEARING THESE NOISES LOUDER AND MORE OFTEN THROUGHOUT THE DAY. WE HAVE NO IDEA WHETHER WE HAVE A SAFETY ISSUE
... OR NOT, HOWEVER WE FEEL UNSAFE. WE NOTIFIED LEXUS AND ARE WAITING FOR A RESPONSE.Read more
Incident date: Aug 27, 2015
RECEIVED RECALL NOTICE AND SCHEDULED APPOINTMENT FOR AIR BAG RECALL TO BE REPAIRED. THE LEXUS DEALER HELD THE CAR FOR FOUR DAYS BEFORE REALIZING THEY DID NOT HAVE THE PARTS TO MAKE THE REPAIR. WE WERE TOLD TO PICK UP THE CAR AND THEY COULD NOT TELL US WHEN THE PARTS WOULD BE AVAILABLE TO REMEDY THE RECALL DEFECT. THE NOTICE SAYS NOT TO OPERATE THE CAR WITH A PASSENGER UNTIL THE REPAIRS ARE COMP
... LETE.Read more
Incident date: Jun 19, 2015
I BOUGHT PRE-OWNED 2013 LEXUS ES300H CAR IN MOTH OF APRIL AND STARTED HAVING SEVER BACK PAIN, I CONTACTED LEXUS CUSTOMER SERVICE WITH FACT THAT SOMETHING WRONG WITH SEAT, PLEASE HELP ME AS I AM HAVING SEVER BACK PAIN EVERY SINGLE TIME I USE THE CAR. LEXUS REPRESENTATIVE HAS BEEN GOING ROUND ABOUT AND NOT ADDRESSING THE ISSUE, THEY DID NOT EVEN PROPERLY INSPECTED THE SEAT AND DISMISSED THE CASE.
... NO GOOD SOLUTION PROVIDED. (LEXUS ASK ME TO SELL THE CAR!!!) I URGE NHTSA TO INTERVENE TO RESOLVE THE ISSUE, IT NOT EASY TO SELL AND BUY CAR, I WILL LOSE LOT OF MONEY. I AM FEELING THAT COMMON MAN HAS NO SAY IN FRONT OF THESE BIG CORPORATIONS, THIS IS EXACT SAME WAY HOW LEXUS TREATED THIS CASE.Read more
Incident date: Apr 10, 2015
I PARKED THE CAR IN MY INDOOR GARAGE (PART OF THE INTERIOR OF MY HOME). SEVERAL HOURS LATER, I BEGAN TO FEEL ILL AND COLLAPSED ON THE FLOOR. I WAS ABLE TO CALL 911 AND AN EMERGENCY CREW RESPONDED TO MY HOME. I WAS UNABLE TO OPEN THE DOOR, BUT THEY WERE ABLE TO GAIN ACCESS. THEY IMMEDIATELY DETERMINED THAT MY HOME WAS FILLED WITH CARBON MONOXIDE AND FOUND THAT THE SOURCE WAS THE CAR IN THE GARA
... GE. THEY DETERMINED THAT THE CAR'S ENGINE HAD BEEN LEFT ON AND THE BATTERY WAS DEAD. THIS WAS THE RESULT OF ME WALKING AWAY FROM THE CAR, WHICH HAS A "SMART-KEY" IGNITION, WITH THE ENGINE STILL RUNNING. I DID NOT HEAR ANY ALERT FROM THE CAR WARNING ME THAT THE ENGINE WAS RUNNING. THE MEDICS SAID THAT 5 MORE MINUTES IN MY HOME WOULD HAVE BEEN FATAL, AND I WAS RUSHED BY AMBULANCE TO A HOSPITAL, WHERE I REMAINED FOR 3 DAYS.Read more
1 injured
Incident date: Jul 16, 2015
TL* THE CONTACT OWNS A 2005 LEXUS SC430. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V285000 (AIR BAGS) HOWEVER, THE PART TO DO THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME TO PROVIDE THE PART FOR THE REPAIR. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Aug 22, 2015
I WANT TO REPORT THAT I EXPERIENCED UN-INTENDED ACCELERATION ON MY LEXUS IS 250C, 2012 MODEL PURCHASED IN DECEMBER 2011 AS A RESULT OF WHICH MY VEHICLE CRASHED AND WENT TURTLE.
Crash
Incident date: Aug 22, 2015
I WANT TO REPORT THAT I EXPERIENCED UN-INTENDED ACCELERATION ON MY LEXUS IS 250C, 2012 MODEL PURCHASED IN DECEMBER 2011 AS A RESULT OF WHICH MY VEHICLE CRASHED AND WENT TURTLE.
Crash
Incident date: Aug 22, 2015
I WANT TO REPORT THAT I EXPERIENCED UN-INTENDED ACCELERATION ON MY LEXUS IS 250C, 2012 MODEL PURCHASED IN DECEMBER 2011 AS A RESULT OF WHICH MY VEHICLE CRASHED AND WENT TURTLE.
Crash
Incident date: Aug 27, 2015
PARTS NOT AVAILABE TO RESOLVE RECALL TO WHOM IT CONCERNS: PLEASE ALLOW ME TO EXPRESS MY FUSTRATION AT TRYING TO REMEDY A SAFETY NETICE RECALL FOR A PASSENGER AIRBAG INFLATER FOR MY 2004 LEXUS SC430. ON 8/12/2015 I MADE A APPOINTMENT AT WILKIE LEXUS OF HAVERTOWN. MY APPOINTMENT CONFIRMATION IS BELOW : WHILE COURTEOUS, THE SERVICE MANAGE INDICATED THAT HE DID NOT HAVE THE PARTS AND THEY ARE
... BACK ORDERED BY AT LEAST TWO WEEKS. EVEN THOUGH I MADE MY APPOINTMENT 8/12 (WEEKS AGO) INDICATING "FRONT PASSENGER AIRBAG INFLATED MODULE" AS THE REASON FOR THE SERVICE VISIT. CONFIRMATION CODE: X0258RN6EJ DATE AND TIME: 08/27/2015 09:00 AM VEHICLE: 2004 LEXUS SC 430 FURTHER, THE SERVICE MANAGER DID NOT PROVIDE A FUTURE APPOINTMENT OR OFFER TO CONTACT ME WHEN THE PARTS WERE AVAILABLE. IF THE SERVICE RECALL IS A SERIOUS AS INDICATED BY THE RECALL NOTICE, THE PARTS SHOULD HAVE BEEN AVAILABLE FOR THE APPOINTMENT, OR IF THE PARTS WERE NOT AVAILABLE I SHOULD HAVE BEEN RESCHEDULED FOR A FUTURE APPOINTMENT. I FEEL AS THIS IS A SERIOUS ISSUE, HOWEVER NOT HAVING THE PARTS FOR A RECALL IS REFLECTIVE OF THE SERVICE CENTER AND LEXUS NOT TAKING THE RECALL NOTICE SERIOUSLY AND THUS PLACING MY FAMILY AT RISK. PLEASE ADVISE THAT I WILL BE FORWARDING THIS COMPLAINT THE THE NATIONAL HIGHWAY TRAFIC SAFETY ADMINISTRATION AS IS INDICATED THE RECALL NOTICE.Read more
Incident date: Jul 23, 2015
TL* THE CONTACT OWNS A 2007 LEXUS SC430. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V286000 (AIR BAGS) HOWEVER, THE RECALL PART WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Jan 1, 2015
WHILE CAR NEWLY MADE REMOTE KEY CRANK CAR THAT HAD BEEN SITTING WITHOUT BEING DRIVEN 30 +DAYS , I CRANK CAR AND ALARM SOUNDED AND FLASHING LIGHTS CAME ON AND WOULD NOT TURN OFF WHEN CAR KEY TAKEN OUT OF IGNITION. THEN THE CAR BEGAN TO CRANK ALL BY ITSELF WITHOUT THE KEY EVEN IN THE IGNITION!!! I UNHINGED THE BATTERY CABLES AND THE CAR WRNT DEAD. ALSO SMOKE WAS COMING FROM BACK ENGINE AREA!! I T
... OWED CAR TO LEXUS DEALER AND THEY REPLACED THE STARTER. THE GEAR SHIFT LOCKED AND THE CAR DROVE FOR ABOUT A MONTH WHE CHECK ENGINE LIGHT CAME ON REPORTING ELECTRICAL/OXYGEN SENSOR CODE. THE CAR STARTED MAKING A CLICKING CHIRPING LOW SOUND COMING FROM BEHIND DASH BOARD. I REPORTED IT TO LEXUS DEALER SERVICE A AGAIN BUT NOTHING DONE ABOUT IT. AN OUTSIDE MECHANIC SAID IT COULD BE AN ELECTRICAL PROBLEM OR FAULTY ALTERNATOR.Read more
Incident date: Jan 1, 2015
WHILE CAR NEWLY MADE REMOTE KEY CRANK CAR THAT HAD BEEN SITTING WITHOUT BEING DRIVEN 30 +DAYS , I CRANK CAR AND ALARM SOUNDED AND FLASHING LIGHTS CAME ON AND WOULD NOT TURN OFF WHEN CAR KEY TAKEN OUT OF IGNITION. THEN THE CAR BEGAN TO CRANK ALL BY ITSELF WITHOUT THE KEY EVEN IN THE IGNITION!!! I UNHINGED THE BATTERY CABLES AND THE CAR WRNT DEAD. ALSO SMOKE WAS COMING FROM BACK ENGINE AREA!! I T
... OWED CAR TO LEXUS DEALER AND THEY REPLACED THE STARTER. THE GEAR SHIFT LOCKED AND THE CAR DROVE FOR ABOUT A MONTH WHE CHECK ENGINE LIGHT CAME ON REPORTING ELECTRICAL/OXYGEN SENSOR CODE. THE CAR STARTED MAKING A CLICKING CHIRPING LOW SOUND COMING FROM BEHIND DASH BOARD. I REPORTED IT TO LEXUS DEALER SERVICE A AGAIN BUT NOTHING DONE ABOUT IT. AN OUTSIDE MECHANIC SAID IT COULD BE AN ELECTRICAL PROBLEM OR FAULTY ALTERNATOR.Read more
Incident date: Jan 1, 2015
WHILE CAR NEWLY MADE REMOTE KEY CRANK CAR THAT HAD BEEN SITTING WITHOUT BEING DRIVEN 30 +DAYS , I CRANK CAR AND ALARM SOUNDED AND FLASHING LIGHTS CAME ON AND WOULD NOT TURN OFF WHEN CAR KEY TAKEN OUT OF IGNITION. THEN THE CAR BEGAN TO CRANK ALL BY ITSELF WITHOUT THE KEY EVEN IN THE IGNITION!!! I UNHINGED THE BATTERY CABLES AND THE CAR WRNT DEAD. ALSO SMOKE WAS COMING FROM BACK ENGINE AREA!! I T
... OWED CAR TO LEXUS DEALER AND THEY REPLACED THE STARTER. THE GEAR SHIFT LOCKED AND THE CAR DROVE FOR ABOUT A MONTH WHE CHECK ENGINE LIGHT CAME ON REPORTING ELECTRICAL/OXYGEN SENSOR CODE. THE CAR STARTED MAKING A CLICKING CHIRPING LOW SOUND COMING FROM BEHIND DASH BOARD. I REPORTED IT TO LEXUS DEALER SERVICE A AGAIN BUT NOTHING DONE ABOUT IT. AN OUTSIDE MECHANIC SAID IT COULD BE AN ELECTRICAL PROBLEM OR FAULTY ALTERNATOR.Read more
Incident date: May 1, 2015
THE ENTIRE DASHBOARD IS MELTING AND HAS A GOOEY, STICKY SUBSTANCE ALL OVER THE DASHBOARD. THE STICKY SUBSTANCE IS ALL OVER MY WINDSHIELD AND CANNOT COME OFF DUE TO THE LOCATION OF THE GOOEY SUBSTANCE. IT IS CAUSING A GLARE. I HAVE TAKEN THE CAR TO THE LEXUS DEALERSHIP IN JACKSONVILLE, FL AND THEY ACKNOWLEDGE THAT IT NEEDS TO BE REPLACED (WE HAVE PICTURES). WE HAVE ALSO DIRECTLY CONTACTED LEXUS AND
... THEY STATE THEY WILL NOT COVER REPLACEMENT BECAUSE OUR VIN NUMBER IS OUTSIDE OF THE VIN NUMBERS THEIR ENGINEERS SELECTED, NOR DID THEY OFFER OTHER OPTIONS TO ASSIST WITH REPLACEMENT OF THE DASHBOARD.Read more
Incident date: May 1, 2015
THE ENTIRE DASHBOARD IS MELTING AND HAS A GOOEY, STICKY SUBSTANCE ALL OVER THE DASHBOARD. THE STICKY SUBSTANCE IS ALL OVER MY WINDSHIELD AND CANNOT COME OFF DUE TO THE LOCATION OF THE GOOEY SUBSTANCE. IT IS CAUSING A GLARE. I HAVE TAKEN THE CAR TO THE LEXUS DEALERSHIP IN JACKSONVILLE, FL AND THEY ACKNOWLEDGE THAT IT NEEDS TO BE REPLACED (WE HAVE PICTURES). WE HAVE ALSO DIRECTLY CONTACTED LEXUS AND
... THEY STATE THEY WILL NOT COVER REPLACEMENT BECAUSE OUR VIN NUMBER IS OUTSIDE OF THE VIN NUMBERS THEIR ENGINEERS SELECTED, NOR DID THEY OFFER OTHER OPTIONS TO ASSIST WITH REPLACEMENT OF THE DASHBOARD.Read more
Incident date: Jan 1, 2015
POWER STEERING CAN HARDLY MOVE
Crash
Incident date: Aug 24, 2015
TL* THE CONTACT OWNS A 2004 LEXUS SC430. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V285000 (AIR BAGS) AND STATED THAT THE PARTS NEEDED FOR THE RECALL REPAIR WERE NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIRS. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Aug 21, 2015
RECEIVED SAFETY RECALL NOTICE FOR PASSENGER SIDE AIR BAG. SAFETY RECALL WARNED NOT TO USE THE PASSSENGER SIDE SEAT. CALLED DEALER. DEALER ADVISED THAT THE FIRST AVAILABLE TIME THAT THEY COULD FIX THE RECALL WAS JUNE 1ST, 2016. THIS RENDERS THIS VEHICLE UNLESS FOR ALMOST A YEAR. IN THE MEAN TIME WHAT ARE SUPPOSED TO DRIVE?
Incident date: Jul 31, 2015
TL* THE CONTACT OWNS A 2006 LEXUS SC430. WHILE DRIVING AT 70 MPH, THE VOLUME AND THE CRUISE CONTROL ON THE STEERING WHEEL WERE ACTIVATED AND THE RADIO AND NAVIGATION FAILED TO FUNCTION. THE FAILURE RECURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 33,000.
Incident date: Aug 18, 2015
TL* THE CONTACT OWNS A 2008 LEXUS LS460. WHILE DRIVING APPROXIMATELY 30 MPH, THE BRAKE PEDAL WAS DEPRESSED AND THERE WAS AN EXCESSIVE DELAYED RESPONSE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE ABS ACTUATOR WOULD NEED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 130,000.
Incident date: Oct 22, 2013
DOOR LOCKS ACTUATOR FAILURE ON PASSENGER FRONT, PASSENGER REAR. UNABLE TO OPEN DOORS MANUALLY OR REMOTELY VIA KEY FOB.
Incident date: Feb 11, 2015
EXHAUST SYSTEM LEAKING EXHAUST FUME INTO INTERIOR OF CAR. SYSTEM IS LEAKING FROM EXHAUST FLANGES FROM THE FRONT CATALYTIC CONVERTER TO REAR CATALYTIC CONVERTER AND MUFFLER.
Incident date: Aug 1, 2015
TL* THE CONTACT OWNS A 2008 LEXUS RX400H. WHILE DRIVING AT APPROXIMATELY 5 MPH AND ATTEMPTING TO PARK, THE BRAKE PEDAL WAS DEPRESSED BUT THE BRAKES FAILED TO RESPOND. AS A RESULT, THE VEHICLE DROVE OVER A CURB AND CRASHED INTO TREES AND BUSHES. THE AIR BAGS DID NOT DEPLOY. A POLICE REPORT WAS NOT FILED. THE VEHICLE WAS TOWED TO THE CONTACT'S RESIDENCE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE.
... THE APPROXIMATE FAILURE MILEAGE WAS 80,000.Read more
Crash
Incident date: Aug 1, 2015
TL* THE CONTACT OWNS A 2008 LEXUS RX400H. WHILE DRIVING AT APPROXIMATELY 5 MPH AND ATTEMPTING TO PARK, THE BRAKE PEDAL WAS DEPRESSED BUT THE BRAKES FAILED TO RESPOND. AS A RESULT, THE VEHICLE DROVE OVER A CURB AND CRASHED INTO TREES AND BUSHES. THE AIR BAGS DID NOT DEPLOY. A POLICE REPORT WAS NOT FILED. THE VEHICLE WAS TOWED TO THE CONTACT'S RESIDENCE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE.
... THE APPROXIMATE FAILURE MILEAGE WAS 80,000.Read more
Crash
Incident date: Aug 1, 2015
TL* THE CONTACT OWNS A 2008 LEXUS RX400H. WHILE DRIVING AT APPROXIMATELY 5 MPH AND ATTEMPTING TO PARK, THE BRAKE PEDAL WAS DEPRESSED BUT THE BRAKES FAILED TO RESPOND. AS A RESULT, THE VEHICLE DROVE OVER A CURB AND CRASHED INTO TREES AND BUSHES. THE AIR BAGS DID NOT DEPLOY. A POLICE REPORT WAS NOT FILED. THE VEHICLE WAS TOWED TO THE CONTACT'S RESIDENCE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE.
... THE APPROXIMATE FAILURE MILEAGE WAS 80,000.Read more
Crash
Incident date: Jun 16, 2015
TL* THE CONTACT OWNS A 2005 LEXUS SC430. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V285000 (AIR BAGS) AND STATED THAT THE PART WAS NOT AVAILABLE WITHIN A REASONABLE TIMEFRAME TO SCHEDULE THE RECALL REPAIR. THE DEALER DID NOT GIVE A SPECIFIC DATE FOR WHEN THE PART WOULD BECOME AVAILABLE. THE MANUFACTURER COULD NOT PROVIDE AN ESTIMATED DATE FOR WHEN THE CONTACT'S VEHICLE WOULD RE
... CEIVE THE RECALL REPAIR. THE CONTACT WAS NOT EXPERIENCING A FAILURE.Read more
Incident date: Aug 17, 2015
DEALER MENTIONED POWER STEERING LEAK IN 2014, AGAIN IN 2015 AND PREVIOUS OWNER OF VEHICLE TOOK IT IN TO HAVE IT LOOKED AT DUE TO COMPLAINT OF PROBLEMS WITH POWER STEERING IN 2012 WITH WATER PUMP AND TIMING BELT WERE CHANGED. MY LOCAL DEALER IS STATING THE REPAIR WILL COST AT LEAST $1000 TO REPAIR. DESPITE RECALLS ON THE INTERNET, IT SEEMS THAT THE INVESTIGATION OF THE 2005 LEXUS RX 330 NEEDS TO IN
... CLUDE VEHICLE MANUFACTURED IN CANADA (MINE STATES CANADA). PLEASE HELP I WANT TO BE SAFE DRIVING MY FAMILY IN THIS VEHICLE.Read more
Incident date: May 18, 2015
TL* THE CONTACT OWNS A 2007 LEXUS SC430. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V286000 (AIR BAGS) AND STATED THAT THE PART NEEDED WAS NOT AVAILABLE. THE DEALER DID NOT GIVE A SPECIFIC DATE FOR WHEN THE PART WOULD BECOME AVAILABLE. THE MANUFACTURER WAS CONTACTED AND COULD NOT PROVIDE AN ESTIMATED DATE FOR WHEN THE VEHICLE WOULD RECEIVE THE RECALL REPAIR. THE CONTACT HAD NOT
... EXPERIENCED A FAILURE.Read more
Incident date: Jun 10, 2014
I SUFFERED BACK AND NECK PAIN WHILE LOADING THE REAR TRUNK OF MY LEXUS SUV. THE REMOTE DOOR CONTINUED TO CLOSE AND COULDN'T BE LIFTED FROM MY BODY THAT WAS STUCK BETWEEN THE DOOR AND REAR TRUCK AREA. I HAD TO CRAWL FROM UNDER THE CLOSING DOOR THAT WAS CRUSHING MY BACK TO PREVENT ADDITIONAL INJURIES THAT COULD HAVE BEEN FATAL. THE LEXUS HQ OFFICE WAS CONTACTED AND THERE IS A CURRENT CASE REPORT. T
... HE LEXUS DEALERSHIP LOCATED IN DULUTH GA FIXED THE REAR DOOR FREE OF CHARGE BY PLACING A SENSOR TO OPEN WHEN AN OBJECT OR PERSON IS BLOCKING THE DOOR WHILE CLOSING. OTHERS LEXUS AND TOYOTA SUV OWNERS HAVE EXPERIENCED SIMILAR PROBLEMS WHEN TOLD WHAT HAPPENED TO ME. IM STILL TAKING MEDICATION FOR PAIN CAUSED BY THE INJURIES.Read more
1 injured
Incident date: Jun 10, 2014
I SUFFERED BACK AND NECK PAIN WHILE LOADING THE REAR TRUNK OF MY LEXUS SUV. THE REMOTE DOOR CONTINUED TO CLOSE AND COULDN'T BE LIFTED FROM MY BODY THAT WAS STUCK BETWEEN THE DOOR AND REAR TRUCK AREA. I HAD TO CRAWL FROM UNDER THE CLOSING DOOR THAT WAS CRUSHING MY BACK TO PREVENT ADDITIONAL INJURIES THAT COULD HAVE BEEN FATAL. THE LEXUS HQ OFFICE WAS CONTACTED AND THERE IS A CURRENT CASE REPORT. T
... HE LEXUS DEALERSHIP LOCATED IN DULUTH GA FIXED THE REAR DOOR FREE OF CHARGE BY PLACING A SENSOR TO OPEN WHEN AN OBJECT OR PERSON IS BLOCKING THE DOOR WHILE CLOSING. OTHERS LEXUS AND TOYOTA SUV OWNERS HAVE EXPERIENCED SIMILAR PROBLEMS WHEN TOLD WHAT HAPPENED TO ME. IM STILL TAKING MEDICATION FOR PAIN CAUSED BY THE INJURIES.Read more
1 injured
Incident date: Jun 10, 2014
I SUFFERED BACK AND NECK PAIN WHILE LOADING THE REAR TRUNK OF MY LEXUS SUV. THE REMOTE DOOR CONTINUED TO CLOSE AND COULDN'T BE LIFTED FROM MY BODY THAT WAS STUCK BETWEEN THE DOOR AND REAR TRUCK AREA. I HAD TO CRAWL FROM UNDER THE CLOSING DOOR THAT WAS CRUSHING MY BACK TO PREVENT ADDITIONAL INJURIES THAT COULD HAVE BEEN FATAL. THE LEXUS HQ OFFICE WAS CONTACTED AND THERE IS A CURRENT CASE REPORT. T
... HE LEXUS DEALERSHIP LOCATED IN DULUTH GA FIXED THE REAR DOOR FREE OF CHARGE BY PLACING A SENSOR TO OPEN WHEN AN OBJECT OR PERSON IS BLOCKING THE DOOR WHILE CLOSING. OTHERS LEXUS AND TOYOTA SUV OWNERS HAVE EXPERIENCED SIMILAR PROBLEMS WHEN TOLD WHAT HAPPENED TO ME. IM STILL TAKING MEDICATION FOR PAIN CAUSED BY THE INJURIES.Read more
1 injured
Incident date: Jul 27, 2015
TL* THE CONTACT OWNS A 2006 LEXUS IS 350. THE CONTACT STATED THAT WHILE DRIVING AT 40 MPH, THE VEHICLE STALLED AND THE CONTACT HEARD AN ABNORMAL NOISE COMING FROM THE ENGINE COMPARTMENT OF THE VEHICLE. ALL THE WARNING LIGHTS ON THE INSTRUMENT CLUSTER ILLUMINATED. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT VARIABLE TIMING GEAR, THE TIMING CHAIN, AND THE TIMING COVER NEEDED
... TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 77,000. THE VIN WAS UNAVAILABLE.Read more
Incident date: Jun 20, 2015
MY ACCIDENT WAS CAUSED BY UNINTENDED ACCELERATION. AS I WAS SLOWLY TURNING RIGHT INTO A PARKING PLACE, THE CAR SUDDENLY ACCELERATED AND CRASHED INTO A BRICK BUILDING. THE FORCE OF THE CRASH CAUSED THE AIR BAGS TO DEPLOY. THERE WAS SO MUCH DAMAGE TO THE CAR THAT IT WAS A TOTAL LOSS. AFTER THE CRASH I OBTAINED THE EVENT DATA RECORDER (EDR) READING FROM A CONTRACTOR HIRED BY TOYOTA. IT SHOWED THAT F
... OR THE LAST 5 SECONDS BEFORE THE CRASH, I WAS APPLYING VERY LIGHT PRESSURE TO THE GAS PEDAL UP UNTIL THE LAST .8 SECONDS. FOR THE LAST .8 SECONDS THE EDR SHOWS THAT MY FOOT WAS ON THE BREAK AND THE THROTTLE WAS AT NEARLY MAXIMUM VALUE. DURING THE LAST .8 SECONDS THE CAR WENT FROM 5 MPH TO 9.9 MPH AND THE ENGINE RPM WENT FROM 1200 TO 2800. I DID NOT APPLY PRESSURE TO THE GAS PEDAL AT THIS TIME. I WAS APPLYING PRESSURE TO THE BREAK PEDAL. THIS IS A CASE OF UNINTENDED ACCELERATION CAUSED BY FAULTY ELECTRONIC THROTTLE CONTROL (ETC) SOFTWARE. SINCE THE EDR GETS IT DATA FROM THE ETC SOFTWARE AND NOT THE GAS PEDAL ITSELF, IT IS MOST LIKELY THAT THE SOFTWARE WAS A FAULT, AS I WAS NOT APPLYING THE GAS DURING THE LAST SECOND BEFORE THE ACCIDENT. IT WOULD BE IMPOSSIBLE FOR ME TO APPLY FULL PRESSURE TO THE GAS PEDAL WHILE APPLYING THE BREAKS AT THE SAME TIME ON THIS CAR. FIRST OF ALL MY SHOE WIDTH IS SMALLER THAN THE SPACE BETWEEN BREAK AND GAS PEDALS. FURTHERMORE THE BREAK PEDAL IS ABOVE THE GAS PEDAL MAKING IT NEARLY IMPOSSIBLE FOR ANYONE TO APPLY THE BREAKS AND FLOOR THE GAS AT THE SAME TIME. THIS IS A CASE OF FAILED ELECTRONIC CONTROL SOFTWARE, WHICH HAS BEEN IDENTIFIED IN SEVERAL LAWSUITS THAT TOYOTA HAS LOST RECENTLY. IN SPITE OF ALL THESE LOST CASES, A LOST CLASS-ACTION LAWSUIT, AND NUMEROUS DOCUMENTED ACCIDENTS WITH NHTSA, TOYOTA HAS DONE NOTHING TO FIX THE PROBLEM, WHICH IS FAULTY ELECTRONIC THROTTLE CONTROL SOFTWARE.Read more
Crash
Incident date: Jun 20, 2015
MY ACCIDENT WAS CAUSED BY UNINTENDED ACCELERATION. AS I WAS SLOWLY TURNING RIGHT INTO A PARKING PLACE, THE CAR SUDDENLY ACCELERATED AND CRASHED INTO A BRICK BUILDING. THE FORCE OF THE CRASH CAUSED THE AIR BAGS TO DEPLOY. THERE WAS SO MUCH DAMAGE TO THE CAR THAT IT WAS A TOTAL LOSS. AFTER THE CRASH I OBTAINED THE EVENT DATA RECORDER (EDR) READING FROM A CONTRACTOR HIRED BY TOYOTA. IT SHOWED THAT F
... OR THE LAST 5 SECONDS BEFORE THE CRASH, I WAS APPLYING VERY LIGHT PRESSURE TO THE GAS PEDAL UP UNTIL THE LAST .8 SECONDS. FOR THE LAST .8 SECONDS THE EDR SHOWS THAT MY FOOT WAS ON THE BREAK AND THE THROTTLE WAS AT NEARLY MAXIMUM VALUE. DURING THE LAST .8 SECONDS THE CAR WENT FROM 5 MPH TO 9.9 MPH AND THE ENGINE RPM WENT FROM 1200 TO 2800. I DID NOT APPLY PRESSURE TO THE GAS PEDAL AT THIS TIME. I WAS APPLYING PRESSURE TO THE BREAK PEDAL. THIS IS A CASE OF UNINTENDED ACCELERATION CAUSED BY FAULTY ELECTRONIC THROTTLE CONTROL (ETC) SOFTWARE. SINCE THE EDR GETS IT DATA FROM THE ETC SOFTWARE AND NOT THE GAS PEDAL ITSELF, IT IS MOST LIKELY THAT THE SOFTWARE WAS A FAULT, AS I WAS NOT APPLYING THE GAS DURING THE LAST SECOND BEFORE THE ACCIDENT. IT WOULD BE IMPOSSIBLE FOR ME TO APPLY FULL PRESSURE TO THE GAS PEDAL WHILE APPLYING THE BREAKS AT THE SAME TIME ON THIS CAR. FIRST OF ALL MY SHOE WIDTH IS SMALLER THAN THE SPACE BETWEEN BREAK AND GAS PEDALS. FURTHERMORE THE BREAK PEDAL IS ABOVE THE GAS PEDAL MAKING IT NEARLY IMPOSSIBLE FOR ANYONE TO APPLY THE BREAKS AND FLOOR THE GAS AT THE SAME TIME. THIS IS A CASE OF FAILED ELECTRONIC CONTROL SOFTWARE, WHICH HAS BEEN IDENTIFIED IN SEVERAL LAWSUITS THAT TOYOTA HAS LOST RECENTLY. IN SPITE OF ALL THESE LOST CASES, A LOST CLASS-ACTION LAWSUIT, AND NUMEROUS DOCUMENTED ACCIDENTS WITH NHTSA, TOYOTA HAS DONE NOTHING TO FIX THE PROBLEM, WHICH IS FAULTY ELECTRONIC THROTTLE CONTROL SOFTWARE.Read more
Crash
Incident date: Jun 20, 2015
MY ACCIDENT WAS CAUSED BY UNINTENDED ACCELERATION. AS I WAS SLOWLY TURNING RIGHT INTO A PARKING PLACE, THE CAR SUDDENLY ACCELERATED AND CRASHED INTO A BRICK BUILDING. THE FORCE OF THE CRASH CAUSED THE AIR BAGS TO DEPLOY. THERE WAS SO MUCH DAMAGE TO THE CAR THAT IT WAS A TOTAL LOSS. AFTER THE CRASH I OBTAINED THE EVENT DATA RECORDER (EDR) READING FROM A CONTRACTOR HIRED BY TOYOTA. IT SHOWED THAT F
... OR THE LAST 5 SECONDS BEFORE THE CRASH, I WAS APPLYING VERY LIGHT PRESSURE TO THE GAS PEDAL UP UNTIL THE LAST .8 SECONDS. FOR THE LAST .8 SECONDS THE EDR SHOWS THAT MY FOOT WAS ON THE BREAK AND THE THROTTLE WAS AT NEARLY MAXIMUM VALUE. DURING THE LAST .8 SECONDS THE CAR WENT FROM 5 MPH TO 9.9 MPH AND THE ENGINE RPM WENT FROM 1200 TO 2800. I DID NOT APPLY PRESSURE TO THE GAS PEDAL AT THIS TIME. I WAS APPLYING PRESSURE TO THE BREAK PEDAL. THIS IS A CASE OF UNINTENDED ACCELERATION CAUSED BY FAULTY ELECTRONIC THROTTLE CONTROL (ETC) SOFTWARE. SINCE THE EDR GETS IT DATA FROM THE ETC SOFTWARE AND NOT THE GAS PEDAL ITSELF, IT IS MOST LIKELY THAT THE SOFTWARE WAS A FAULT, AS I WAS NOT APPLYING THE GAS DURING THE LAST SECOND BEFORE THE ACCIDENT. IT WOULD BE IMPOSSIBLE FOR ME TO APPLY FULL PRESSURE TO THE GAS PEDAL WHILE APPLYING THE BREAKS AT THE SAME TIME ON THIS CAR. FIRST OF ALL MY SHOE WIDTH IS SMALLER THAN THE SPACE BETWEEN BREAK AND GAS PEDALS. FURTHERMORE THE BREAK PEDAL IS ABOVE THE GAS PEDAL MAKING IT NEARLY IMPOSSIBLE FOR ANYONE TO APPLY THE BREAKS AND FLOOR THE GAS AT THE SAME TIME. THIS IS A CASE OF FAILED ELECTRONIC CONTROL SOFTWARE, WHICH HAS BEEN IDENTIFIED IN SEVERAL LAWSUITS THAT TOYOTA HAS LOST RECENTLY. IN SPITE OF ALL THESE LOST CASES, A LOST CLASS-ACTION LAWSUIT, AND NUMEROUS DOCUMENTED ACCIDENTS WITH NHTSA, TOYOTA HAS DONE NOTHING TO FIX THE PROBLEM, WHICH IS FAULTY ELECTRONIC THROTTLE CONTROL SOFTWARE.Read more
Crash
Incident date: Jan 1, 2009
HELLO, FIRST THE HEADLIGHTS AUTO ADJUST LOW. THEY STATE ITS NORMAL AND I TOOK THE CAR TO DEALER A LEAST 13 TIMES FOR HEADLIGHTS POINTING LOW AND ONLY GIVES ABOUT 3 OR 4 FT ON LIGHT BEYOND GOOD. NOW WARRANTY EXPIRED. THEY DIDN'T NOTHING. REAR VIEW MIRROR FADED IT'S NOT SAFE TO USE IT. DEALER KNOWS ABOUT THE PROBLEM BUT WANTS ME TO 1300$ FOR NEW MIRROR. FRONT BUSHING SYSTEM FAILED COMPLETELY. I TO
... OK IT TO 3 REPAIR SHOPS AND ALL STATED AS KNOW PROBLEM, THEY QUOTED 2000$ FOR REPAIR BECAUSE LEXUS WILL NOT AND DON'T SELL ONLY BUSHINGS. YOU HAVE TO BUY ALL NEW COMPLETE ARM CONTROLS. LAST ITEM, THE HOOD STARTED TO RUST FROM UNDER THE PAINT WITHOUT ANY CHIPS. THE RUST STARTS A BUBBLE THEN CHIPS OPEN. ALL THESE COMPLAINTS ARE LISTED LEXUS FORUMS ALL OVER GOOGLE. VERY EASY TO FIND AND VERIFY. I HAVE CARS OVER 25YEARS OLD NEVER HAD A REAR VIEW MIRROR FADE TO THE POINT IT'S UNSAFE TO USE. BACKING OUT OF DRIVES. OUR KIDS AND NEIGHBORS MUST BE SAFE. HEAD LIGHTS THAT ARE UNSAFE , SCARY STUFF AND NO ONES FORCES LEXUS TO FIX THESE. GOD BLESS AND THANK YOU!Read more
Incident date: Jan 1, 2009
HELLO, FIRST THE HEADLIGHTS AUTO ADJUST LOW. THEY STATE ITS NORMAL AND I TOOK THE CAR TO DEALER A LEAST 13 TIMES FOR HEADLIGHTS POINTING LOW AND ONLY GIVES ABOUT 3 OR 4 FT ON LIGHT BEYOND GOOD. NOW WARRANTY EXPIRED. THEY DIDN'T NOTHING. REAR VIEW MIRROR FADED IT'S NOT SAFE TO USE IT. DEALER KNOWS ABOUT THE PROBLEM BUT WANTS ME TO 1300$ FOR NEW MIRROR. FRONT BUSHING SYSTEM FAILED COMPLETELY. I TO
... OK IT TO 3 REPAIR SHOPS AND ALL STATED AS KNOW PROBLEM, THEY QUOTED 2000$ FOR REPAIR BECAUSE LEXUS WILL NOT AND DON'T SELL ONLY BUSHINGS. YOU HAVE TO BUY ALL NEW COMPLETE ARM CONTROLS. LAST ITEM, THE HOOD STARTED TO RUST FROM UNDER THE PAINT WITHOUT ANY CHIPS. THE RUST STARTS A BUBBLE THEN CHIPS OPEN. ALL THESE COMPLAINTS ARE LISTED LEXUS FORUMS ALL OVER GOOGLE. VERY EASY TO FIND AND VERIFY. I HAVE CARS OVER 25YEARS OLD NEVER HAD A REAR VIEW MIRROR FADE TO THE POINT IT'S UNSAFE TO USE. BACKING OUT OF DRIVES. OUR KIDS AND NEIGHBORS MUST BE SAFE. HEAD LIGHTS THAT ARE UNSAFE , SCARY STUFF AND NO ONES FORCES LEXUS TO FIX THESE. GOD BLESS AND THANK YOU!Read more
Incident date: Jan 1, 2009
HELLO, FIRST THE HEADLIGHTS AUTO ADJUST LOW. THEY STATE ITS NORMAL AND I TOOK THE CAR TO DEALER A LEAST 13 TIMES FOR HEADLIGHTS POINTING LOW AND ONLY GIVES ABOUT 3 OR 4 FT ON LIGHT BEYOND GOOD. NOW WARRANTY EXPIRED. THEY DIDN'T NOTHING. REAR VIEW MIRROR FADED IT'S NOT SAFE TO USE IT. DEALER KNOWS ABOUT THE PROBLEM BUT WANTS ME TO 1300$ FOR NEW MIRROR. FRONT BUSHING SYSTEM FAILED COMPLETELY. I TO
... OK IT TO 3 REPAIR SHOPS AND ALL STATED AS KNOW PROBLEM, THEY QUOTED 2000$ FOR REPAIR BECAUSE LEXUS WILL NOT AND DON'T SELL ONLY BUSHINGS. YOU HAVE TO BUY ALL NEW COMPLETE ARM CONTROLS. LAST ITEM, THE HOOD STARTED TO RUST FROM UNDER THE PAINT WITHOUT ANY CHIPS. THE RUST STARTS A BUBBLE THEN CHIPS OPEN. ALL THESE COMPLAINTS ARE LISTED LEXUS FORUMS ALL OVER GOOGLE. VERY EASY TO FIND AND VERIFY. I HAVE CARS OVER 25YEARS OLD NEVER HAD A REAR VIEW MIRROR FADE TO THE POINT IT'S UNSAFE TO USE. BACKING OUT OF DRIVES. OUR KIDS AND NEIGHBORS MUST BE SAFE. HEAD LIGHTS THAT ARE UNSAFE , SCARY STUFF AND NO ONES FORCES LEXUS TO FIX THESE. GOD BLESS AND THANK YOU!Read more
Incident date: Aug 13, 2015
TL* THE CONTACT OWNS A 2011 LEXUS RX350 EQUIPPED WITH DUNLOP TIRES, SIZE: 235/55R19 (NA). WHILE DRIVING APPROXIMATELY 45 MPH, THERE WAS A LOUD SOUND COMING FROM OUTSIDE THE VEHICLE. IN ADDITION, THE VEHICLE STARTED WOBBLING AND WAS DIFFICULT TO STEER. THE CONTACT PULLED OVER AND DISCOVERED THAT THE REAR PASSENGER SIDE TIRE WAS BLOWN OUT. THE VEHICLE WAS TOWED TO THE DEALER WHERE IT WAS CONFIRMED T
... HAT THE TIRE NEEDED TO BE REPLACED. THE TIRE WAS REPLACED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VEHICLE FAILURE MILEAGE 66,000 AND THE TIRE FAILURE MILEAGE WAS 12,506. THE DOT NUMBER WAS NOT AVAILABLE.Read more
Incident date: Jul 25, 2015
I HAVE BEEN EXPERIENCING ISSUE WITH MY STEERING CONTROL, AND A UNIQUE NOISE ON SHARP TURNS, SO DURING MY NEXT OIL CHANGE AT THE LEXUS DEALERSHIP THEY EXAMINED AND INFORMED ME THAT MY STEERING RACK IS SEEPING OIL, AND WOULD NEED A REPLACEMENT TO A COST OF $1,800. I DRIVE MY CAR OVER THE WEEKENDS WITH MY KIDS ON OUTDOOR TRIPS OVER THE WEEKEND AND HAVE ONLY 70K MILES, SO WAS A COMPLETE SHOCK TO LEARN
... ABOUT THIS ISSUE. RESEARCH HAS SHOWN ME THAT THIS IS A KNOW ISSUE, AND MANY CONSUMERS HAVE SIMILAR COMPLAIN. ON CONTACTING LEXUS, I WAS INFORMED THAT SINCE MY CAR IS OUT OF WARRANTY PERIOD, THERE NOT MUCH THEY CAN DO ALTHOUGH THEY ARE WELL AWARE OF THE ISSUE, THERE WAS A CHANNEL 2 SAN DIEGO, CA CLIP ON TOYOTA MOTORS HAVING A RECALL, BUT I WAS INFORMED NO SUCH RECALL IS IN FORCE, SO I AM CONFUSED. LEXUS CONTACT ME AND READY TO PAY A PARTIAL SUM ON THE PART REPLACEMENT BUT I WOULD HAVE TO BEAR THE LABOR AND MUCH OF THE COST ASSOCIATED FOR THE PART. A SIMILAR STORY THAT ECHOED WITH OTHER USERS, LEXUS NEEDS TO ADDRESS THIS RECALL/SAFETY ISSUE AT ONCE, BEFORE A FATALITY OCCURS.Read more
Incident date: Jul 3, 2015
WHEN I'M USING MY VENTILATED SEATS THE BOTTOM OF THE SEAT IS NICE AND COOL BUT IT FEELS LIKE THE MY BACK IS BEING HEATED. I ALWAYS HAVE VENTILATION ON LOWEST SETTING. THE TOP OF THE SEAT BETWEEN SHOULDER BLADES... VERY HOT!??? SERIOUSLY. I FELT IT WITH MY HAND, AS IF THE VENTILATION WAS SHORTING THE HEATING ELEMENTS. IT STAYED HOT A WHILE AFTER I TURNED OFF VENTILATION. THEN IT COOLED. HAD THIS HA
... PPEN TO ME ON MY WAY HOME. THE BOTTOM OF THE SEAT WAS COOLING BUT MID BACK THE SEAT GOT VERY HOT. TURNING IT OFF DID CUT THE HEAT AND THEN IT WOULD COME RIGHT BACK WHEN I TURNED IT ON. AND IT SEEMED TO BE GONE. THIS HAPPENED TO ME. TO MAKE SURE I TURNED ON THE VENTILATION ON THE PASSENGER SIDE TOO, NO ONE SITTING IN IT. IT WARMS UP AT THE SAME SPOT AS THE DRIVER SIDE. JUST BELOW SHOULDER BLADE AREA. THE SEAT PORTION IS COOL AND YOU CAN FEEL THE AIR. THE BACK (WARMER PART) IS NOT EMITTING AIR, BUT JUST HOT. TURNED THE SWITCH ON AND OFF, BUT STILL GETS HOT IN THE THE BACK. FINALLY, TURNED THE CAR OFF FOR ABOUT 10 MINUTES. TURNED IT BACK ON, AND THE PROBLEM WENT AWAY. HOWEVER, I FEEL THAT THIS PROBLEM WILL RETURN. JUST USED VENTED SEATS I EXPERIENCED THE EXACT SAME THING. COOLING ON THE SEAT AND IT GOT VERY HOT ABOUT WHERE MY SHOULDER BLADES ARE. IT WAS UNCOMFORTABLE ENOUGH THAT I WAS COOLER LEAVING THEM OFF. I TAKE IT INTO THE DEALER FOR THE 5K CHECKUP SOON. THE BACK OF THE SEAT HEATING IS REALLY ANNOYING!! HOPE IT'S A QUICK FIX! THEY CAN'T REPLICATE THE PROBLEM, THUS UNABLE TO DIAGNOSE. ALTHOUGH I'M NOT HAPPY WITH THE FACT THIS PROBLEM IS NOT RESOLVED, I KNOW THAT THE PROBLEM IS OCCURS AT RANDOM. WE JUST HAVE TO KEEP THEM AWARE THAT THE PROBLEM EXIST BY REPORTING IT. THE SERVICE WRITER CREATED A CASE NUMBER (IT'S PRINTED IN THE PAPERWORK) AND SUBMITTED TO LEXUS CORP. HOPEFULLY WE GET A FIX FOR THIS SOON.Read more
Incident date: Jul 3, 2015
WHEN I'M USING MY VENTILATED SEATS THE BOTTOM OF THE SEAT IS NICE AND COOL BUT IT FEELS LIKE THE MY BACK IS BEING HEATED. I ALWAYS HAVE VENTILATION ON LOWEST SETTING. THE TOP OF THE SEAT BETWEEN SHOULDER BLADES... VERY HOT!??? SERIOUSLY. I FELT IT WITH MY HAND, AS IF THE VENTILATION WAS SHORTING THE HEATING ELEMENTS. IT STAYED HOT A WHILE AFTER I TURNED OFF VENTILATION. THEN IT COOLED. HAD THIS HA
... PPEN TO ME ON MY WAY HOME. THE BOTTOM OF THE SEAT WAS COOLING BUT MID BACK THE SEAT GOT VERY HOT. TURNING IT OFF DID CUT THE HEAT AND THEN IT WOULD COME RIGHT BACK WHEN I TURNED IT ON. AND IT SEEMED TO BE GONE. THIS HAPPENED TO ME. TO MAKE SURE I TURNED ON THE VENTILATION ON THE PASSENGER SIDE TOO, NO ONE SITTING IN IT. IT WARMS UP AT THE SAME SPOT AS THE DRIVER SIDE. JUST BELOW SHOULDER BLADE AREA. THE SEAT PORTION IS COOL AND YOU CAN FEEL THE AIR. THE BACK (WARMER PART) IS NOT EMITTING AIR, BUT JUST HOT. TURNED THE SWITCH ON AND OFF, BUT STILL GETS HOT IN THE THE BACK. FINALLY, TURNED THE CAR OFF FOR ABOUT 10 MINUTES. TURNED IT BACK ON, AND THE PROBLEM WENT AWAY. HOWEVER, I FEEL THAT THIS PROBLEM WILL RETURN. JUST USED VENTED SEATS I EXPERIENCED THE EXACT SAME THING. COOLING ON THE SEAT AND IT GOT VERY HOT ABOUT WHERE MY SHOULDER BLADES ARE. IT WAS UNCOMFORTABLE ENOUGH THAT I WAS COOLER LEAVING THEM OFF. I TAKE IT INTO THE DEALER FOR THE 5K CHECKUP SOON. THE BACK OF THE SEAT HEATING IS REALLY ANNOYING!! HOPE IT'S A QUICK FIX! THEY CAN'T REPLICATE THE PROBLEM, THUS UNABLE TO DIAGNOSE. ALTHOUGH I'M NOT HAPPY WITH THE FACT THIS PROBLEM IS NOT RESOLVED, I KNOW THAT THE PROBLEM IS OCCURS AT RANDOM. WE JUST HAVE TO KEEP THEM AWARE THAT THE PROBLEM EXIST BY REPORTING IT. THE SERVICE WRITER CREATED A CASE NUMBER (IT'S PRINTED IN THE PAPERWORK) AND SUBMITTED TO LEXUS CORP. HOPEFULLY WE GET A FIX FOR THIS SOON.Read more
Incident date: Aug 8, 2015
INITIALLY FELT THE VEHICLE SUDDENLY LURCH FOWARD ON SEVERAL OCCASIONS AFTER BACKING OUT OF PARKING SPACE AT WORK AND SHIFTING INTO DRIVE. HAD TO HIT BRAKES, BRING THE VEHICLE TO A COMPLETE STOP, AND THEN SLOWLY START FORWARD AGAIN. ACCIDENT OCCURRED IN THE DRIVEWAY OF A PRIVATE RESIDENCE. THE VEHICLE WAS PLACED IN PARK AND FULLY STOPPED.. DRIVER WAS ABOUT TO TURN OFF ENGINE AND, WITH PASSENGER
... , EXIT THE VEHICLE WHEN IT SUDDENLY ACCELERATED FOR NO REASON, PLOWING STRAIGHT INTO THE GARAGE DOOR OF RESIDENCE. GARAGE DOOR WAS COMPLETELY TORN OFF AND THE VEHICLE CAME TO A STOP AFTER SMASHING AN INTERIOR WALL AND DOORFRAME. THANKFULLY, NO INJURIES BUT COULD HAVE BEEN WORSE IF THE WINDSHIELD HAD BROKE. THE VEHICLE WAS DAMAGED ON 3 SIDES AND THE PROPERTY SUSTAINED DAMAGE TO THE GARAGE DOOR, INTERIOR DRYWALL, DOOR AND DOORFRAME. AGAIN, THE VEHICLE WAS COMPLETELY STOPPED AND IN PARK WHEN IT SUDDENLY ACCELERATED.Read more
Crash
Incident date: Aug 8, 2015
TL* THE CONTACT OWNS A 2012 LEXUS RX350. WHILE THE VEHICLE WAS PARKED AND ATTEMPTING TO TURN OFF THE ENGINE, THE VEHICLE SUDDENLY INDEPENDENTLY ACCELERATED AND CRASHED INTO A GARAGE DOOR AND INTO A WALL. THE VEHICLE HAD EXTENSIVE DAMAGES TO THE FRONT OF THE VEHICLE DUE TO THE FAILURE. THE DRIVER AND THE PASSENGER SUSTAINED WHIP LASH THAT DID NOT REQUIRE MEDICAL ATTENTION. THE VEHICLE WAS NOT DIAGN
... OSED AND THE DAMAGES WERE REPAIRED. A POLICE REPORT WAS NOT FILED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 14,878.Read more
Crash
2 injured
Incident date: Jul 1, 2014
I NOTICED THAT MY INFLATE TIRE LIGHT WAS ON. WHEN I LOOKED UNDER MY CAR TO INFLATE THE SPARE I NOTICED THAT THE SPARE WAS GONE AND THE CABLE HAD SNAPPED DUE TO RUSTING. THIS IS AN OBVIOUS DEFECT AND IS SURELY A SAFETY HAZARD IF THE TIRE WERE TO FALL OFF WHILE DRIVING. 2008 LEUS RX 350 AWD.
Incident date: Feb 1, 2010
DASH IS MELTING AND IS STICKING TO ANYTHING THAT IS RUB UP AGAINST IT. BODY PARTS, CAR WASH TOWEL, GROCERY. I SEEL RECALL ON ALL OTHER MODEL REGARDING THIS ISSUE. EXCEPT THIS PARTICULAR MODEL 2003 LEXUS IS300. I BELIEVE IT SHOULD EXTEND TO THIS YEAR AND MODEL AS WELL. NO DASH SHOULD BE MELTING AWAY WITH HEAT!
Incident date: Jul 7, 2015
NO DESCRIPTION
Incident date: Jul 7, 2015
NO DESCRIPTION