Showing 1,147 complaints for KEYSTONE
Incident date: Jun 28, 2017
TIRE #1 BLEW OUT IN OKLAHOMA ON JUNE 14TH AND WAS LEFT BEHIND. AT THE TIME, I THOUGHT IT WAS A RANDOM FAILURE AND JUST MOVED ON. TIRE #2 BLEW OUT IN TENNESSEE ON JUNE 28TH. THE TIRE TECHNICIAN AT DISCOUNT SHOWED ME HOW TIRE #3 WAS SEPARATED AND READY TO FAIL. THE SPARE NEXT TO IT WAS FLAT ACROSS THE TREAD, BUT #3 WAS NOTICEABLY DOMED. AFTER IT WAS REPLACED HE PUSHED DOWN ON THE TREAD AND YOU COU
... LD HEAR THE SOUND OF THE METAL PLIES IN THE TIRE MOVING AROUND. TBC BRANDS PASSED MY CLAIM ONTO UNICORN TIRE CORPORATION. THEY HAD THE TIRE INSPECTED AND AGREED IT SHOWED STEEL BELT SEPARATION. THEY OFFERED $375 FOR $2000 DAMAGE. IT IS SAD THESE TIRES ARE USED ON NEW KEYSTONE TRAILERS. TRAILER MODEL IS COUGAR, NOT AVAILABLE IN WEBSITE PULLDOWN BOX.Read more
Incident date: Jul 21, 2017
WHILE PULLING OUR FIFTH-WHEEL TRAILER, WE HAD A TREAD SEPARATION WITH ONE OF OUR POWER KING TOWMAX STR TIRES. THE RESULTING TIRE FAILURE, CAUSE BODY DAMAGE TO BOTH THE PLASTIC AND ALUMINUM SKIRTING ON THE RV. TRAVELING SPEED: 60 MPH. TIRE PRESSURE: 80 PSI. TREAD DEPTH: 6/32".
Incident date: Aug 26, 2017
FROM THE TIME I LEFT THE DEALER LOT, I NEVER HAD BRAKES THAT WORKED PROPERLY. INCREASING THE OUTPUT FROM THE BRAKE CONTROLLER DIDN'T HELP. THE BRAKES WOULD OVER HEAT AND NEVER FELT THAT I HAD ENOUGH BRAKE TO STOP THE TRAILER/TRUCK. HAD THE BRAKES CHECKED BY SEVERAL RV DEALERS WHICH LED TO AN ADJUST ONLY. RECENT TRIP CAUSED "HOT" BRAKES/WHEELS AND BRAKE SMELL. WENT TO A FACILITY THAT SPECIALIZES
... IN RV REPAIR AND TOLD THEM TO TEAR THE SYSTEM APART AND FIX THE PROBLEM. THEY FOUND NOT ENOUGH VOLTAGE AT BRAKES. FURTHER INVESTIGATION FOUND EXCESSIVE LENGTH AND SMALL GAGE WIRE INSTALLED BY MANUFACTURER. NOT ENOUGH CURRENT GOING TO BRAKES. KEYSTONE INSTALLED 14 GAGE WIRE AND IT SHOULD HAVE BEEN 12 GAGE.Read more
Incident date: Aug 26, 2017
FROM THE TIME I LEFT THE DEALER LOT, I NEVER HAD BRAKES THAT WORKED PROPERLY. INCREASING THE OUTPUT FROM THE BRAKE CONTROLLER DIDN'T HELP. THE BRAKES WOULD OVER HEAT AND NEVER FELT THAT I HAD ENOUGH BRAKE TO STOP THE TRAILER/TRUCK. HAD THE BRAKES CHECKED BY SEVERAL RV DEALERS WHICH LED TO AN ADJUST ONLY. RECENT TRIP CAUSED "HOT" BRAKES/WHEELS AND BRAKE SMELL. WENT TO A FACILITY THAT SPECIALIZES
... IN RV REPAIR AND TOLD THEM TO TEAR THE SYSTEM APART AND FIX THE PROBLEM. THEY FOUND NOT ENOUGH VOLTAGE AT BRAKES. FURTHER INVESTIGATION FOUND EXCESSIVE LENGTH AND SMALL GAGE WIRE INSTALLED BY MANUFACTURER. NOT ENOUGH CURRENT GOING TO BRAKES. KEYSTONE INSTALLED 14 GAGE WIRE AND IT SHOULD HAVE BEEN 12 GAGE.Read more
Incident date: Jun 29, 2017
TL* THE CONTACT OWNS A 2014 KEYSTONE BULLET. THE CONTACT STATED THAT WATER ENTERED THE REAR PANEL OF THE TRAILER. UPON INSPECTION, THE CONTACT FOUND THAT THE ALUMINUM MOLDING HEATED AND CAUSED THE REAR PANEL TO WARP. AN INDEPENDENT MECHANIC WAS CONTACTED AND CONFIRMED THAT INADEQUATE MATERIAL WAS USED, WHICH CAUSED THE FAILURE. THE DEALER AND MANUFACTURER WERE NOT CONTACTED. THE FAILURE MILEAGE WA
... S 1,500.Read more
Incident date: Aug 10, 2017
BACK BUMPER WELDS BREAKING WITH A SPARE WHEEL MOUNTED THERE.
Incident date: Jul 29, 2017
SLIDES OPEN WHILE MOVING TRAILER- PASSIVE. EMERGENCY WINDOW IN BEDROOM FLEW OFF TRAILER ON HIGHWAY- FAULTY LATCH AS NEVER OPENED AND LATCH WAS IN CLOSED POSITION
Incident date: Jul 10, 2017
TL* THE CONTACT OWNS A 2017 KEYSTONE MONTANA EQUIPPED WITH TRAILER KING TIRES, TIRE LINE: XT RADIAL N/A, TIRE SIZE: ST235/80/R16 AND DOT NUMBER: ADD85HFST WITH A MAX LOAD RATING OF 3,080 LBS AT 80PSI. THE CONTACT STATED THAT THE GROSS RATING ON THE TIRES DID NOT MEET SPECIFICATIONS PER THE MANUFACTURER MANUAL. THE CONTACT STATED THAT EACH TIRE WAS OVERLOADED BY 230 LBS BASED ON THE MANUFACTURER F
... ORMULA. THE CONTACT STATED THAT WHILE INSPECTING THE TIRES DISCOVERED THAT THE TIRE RATINGS WERE INCORRECT. THE CONTACT STATED THAT THE MANUFACTURER WAS MADE AWARE OF THE ISSUE BUT DID NOT OFFER ANY FURTHER ASSISTANCE. VIN WAS NOT AVAILABLE. THE TRAILER AND TIRE FAILURE MILEAGES WERE NOT AVAILABLE.*DT*JBRead more
Incident date: Jul 21, 2017
TRAILER IS LESS THAN A YEAR OLD. CAME ORIGINAL WITH TRAILER KING TIRES. DATE CODE 1015. ON JULY 21ST, 2017. I CHECKED TIRE PSI BEFORE LEAVING OVERNIGHT STAY. ALL TIRES WERE BETWEEN 78-80PSI. AFTER 49-50 MILES INTO TRIP ON I 75 NORTH BOUND. THE RR TIRE BLEW OUT. ROAD SPEED AT WHICH TIRE WAS RUN WAS BETWEEN 64-66 MPH. WE WERE AT 65 MPH WHEN BLOW-OUT OCCURRED. NO DEBRIS IN ROADWAY. CHANGED TIRE & D
... ROVE TO NEAREST SERVICE FOR REPLACEMENT TIRE. AT THIS SERVICE I NOTICED RUST IN BELT PACKAGE. LIKE THIS TIRE WAS ASSEMBLED WITH RUSTED BELTS. ON RETURN TRIP HOME JULY 24TH. STOPPING AFTER 2 HOUR DRIVE AT REST AREA SOUTH OF OCALA,FL. I DID A WALK AROUND INSPECTION & NOTICED THE LF TIRE BELT SEPARATING. TIRE PSI WAS 78. NO DAMAGE TO TIRE. RELEASED AIR FROM TIRE TO AVOID INJURY & DROVE TO NEAREST SERVICE. HAD REMAINING TRAILER KING TIRES REPLACED.Read more
Incident date: Nov 1, 2016
TL* THE CONTACT OWNS A 2017 KEYSTONE BULLET TRAVEL TRAILER. WHILE DRIVING AT SPEEDS ABOVE 60 MPH, THE TRAILER BECAME EXTREMELY UNSTABLE AND SWAYED AND ROCKED BACK AND FORTH. THE TRAILER WAS TAKEN TO THE DEALER (CAMPING WORLD OF NEW PORT RICHIE IN HOLIDAY, FLORIDA). THE HITCH AND TIRES WERE REPLACED, BUT THE FAILURE CONTINUED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE, BUT NO ASSISTANCE WAS OFFE
... RED. THE FAILURE MILEAGE WAS 1,000.Read more
Incident date: Jul 6, 2017
TIRE BLEW OUT CAUSING 1,850.00 DAMAGE NOT COUNTING NEW TIRE. NOVEMBER 2016 . NEXT TRIP JULY 6 2017 HAD BLOW OUT 7 MILES DOWN THE HWY SECOND TIRE BLEW OUT CAUSING EXTENSIVE DAMAGE . TIRES ARE TOW MAX235/80/16 . I HAD 5 NEW ONES PUT ON THE ONES THAT DIDN'T BUST ARE ALL KNOTTED UP LIKE THE BELTS ARE BROKE I SAVED THE TIRES .*DT*JB
Incident date: Jul 14, 2017
AFTER ONLY 3000 MILES AND 5 YEARS OF AGE TWO OF THESE TIRES BLEW WITH SEPERATION FAILURES. 70 PSI AND NO DEBRIS ON THE ROAD. 65 MPH CRUISE FOR ABOUT AN HOUR. THE TIRES WERE NOT HOT. THE 2012 RAPTOR TRAILER SUSTAINED DAMAGE TO THE SIDING ABOVE THE WHEEL WELL.
Incident date: May 26, 2017
CENTRAL A/C SYSTEM ALLOWS RAIN-WATER TO COME INTO THE COACH THRU THE EXTERIOR SHROUD HOUSING AND IT FLOWS/DRIPS INTO THE AIR RETURN IN THE CEILING (WHERE THERE IS ALSO ELECTRICAL/WIRING) AND THE RAIN WATER THEN RUNS TO THE AIR FILTER, SATURATES IT AND THEN DRIPS ONTO THE TOP OF THE KITCHEN CABINETS, DOWN THE WALL TO THE STOVE AND COUNTER IN THE KITCHEN. THIS MAY RESULT IN A SAFETY ISSUE SOON DUE
... TO THE ELECTRICAL WIRING AT THE ENTRY LOCATION (A RETRANGLE CUTOUT ON THE ROOF WHERE THE A/C MARRIES TO THE RUBBER ROOF. ALSO, THE EXPOSURE TO WATER WHERE I LIVE IN SW FLORIDA NOW MAY HAVE CAUSED "MOLD" TO BEGIN GROWING INSIDE MY WALL AND THE CEILING AND ROOF MATERIALS. UPON TAKING RV TO A CERTIFIED DEALER, THEY FOUND A 3" HOLD TORN AWAY UNDER THE A/C SYSTEM WITH A HOLE IN THE CENTER OF THE EXPOSED WOOD ROOF MATERIALS. AFTER THEY PATCHED THE HOLE THE COACH WAS FOUND TO STILL LEAK WATER INSIDE THE COACH DURING A RAIN STORM. 6 WEEKS LATER AT A DIFFERENT CERTIFIED DEALER, A WATER TEST WAS PERFORMED WITH THE TECH AND OWNER PRESENT WHERE AS THE COACH IS STILL LEAKING, NOW THRU THE EXTERIOR SHROUD ALLOWING THE WATER INTRUSION INTO THE COACH. AGAIN, THERE IS WIRING PRESENT AT THE PLACE OF ENTRY OF THE WATER. WATER & ELECTRICAL SYSTEMS ARE A HAZARD. COULD CAUSE A FIRE OR A ELECTRICAL SHORT TO HAPPEN AT ANY TIME THE COACH IS IN USE. THE COACH WAS INITIALLY PARKED IN A CAMPGROUND WHEN THE PROBLEM WAS DISCOVERED. THE WHOLE IN THE RUBBER ROOF WAS CAUSED BY A FACTORY WORKER OR PROCESS. THE "SHROUD" ISSUE SEEMS TO BE A DESIGN FLAW. I AM UNABLE TO SNAP A PICTURE OF THE SHROUD PROBLEM DUE TO TIGHT CONFINED AREA (1" SPACE IN THE AIR RETURNS ABOVE THE CABINETS). ATTACHED PHOTO OF THE HOLE IN RUBBER MATERIALS. HOWEVER THE RECTANGLE CUTOUT FOR THE A/C SHOWS THE WIRING THAT IS IN CLOSE RANGE OF THE WATER COMING INTO THE COACH THRU THIS CUTOUT.Read more
Incident date: Jul 1, 2017
TL* THE CONTACT OWNS A 2017 KEYSTONE MONTANA. THE CONTACT STATED THAT THE SIDE CURTAINS INSTALLED HAD SHARP, PROTRUDING STEEL PIECES COMING OUT OF THEM. THE DEALER AND MANUFACTURER WERE NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS APPROXIMATELY 30.
Incident date: Jun 24, 2017
TL* THE CONTACT OWNS A 2006 KEYSTONE COUGAR 314 EFS RV. THE CONTACT STATED THAT THE FRONT END COLLAPSED WHILE DRIVING 60 MPH. THE VEHICLE WAS TAKEN TO SOUTH COUNTRY RV REPAIR (541-863-3826) WHERE IT WAS DIAGNOSED THAT THE FRONT FRAME AND KINGPIN SEPARATED DUE TO POOR METAL AND WELDING. THE RV WAS REPAIRED AND THE FRAME AND KINGPIN WERE REPLACED. THE MANUFACTURER WAS NOTIFIED. THE FAILURE MILEAGE W
... AS UNKNOWN.Read more
Incident date: May 15, 2017
TL* THE CONTACT OWNS A 2014 KEYSTONE BULLET 284RLS TRAVEL TRAILER 28FT. THE CONTACT STATED THAT THE VEHICLE'S LIGHT SWITCHES BECAME INOPERABLE. UPON EXPECTING THE CEILING LIGHTS, THE CONTACT NOTICED THAT THE LIGHT SWITCHES HAD MELTED AND BURNED. THE CONTACT ALSO STATED THAT THE SOCKETS WERE BURNED. THE CONTACT STATED THAT THE SWITCHES WERE MOUNTED TO THE EXTERIOR OF THE WOODEN CABINETS AND WAS CON
... CERNED OF GREATER HEAT DISSIPATION. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE VEHICLE WAS NOT TAKEN TO A DEALER. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE, BUT DID NOT OFFER ANY ASSISTANCE. THE FAILURE MILEAGE WAS UNAVAILABLE.Read more
Fire
Incident date: Oct 1, 2016
2016 KEYSTONE COUGAR RV. CONSUMER WRITES IN REGARDS TO THREADED ROD THAT CLAMPS DOWN THE PROPANE TANKS BECAME UNSCREWED FROM TRAILER TONGUE WITH GAS REGULATOR STILL ATTACHED. *SMD UPDATED 06/26/2017*JS UPDATED 08/09/17*LJ *CN
Incident date: Apr 25, 2017
UPSTATE TRUCK & RV SOLD ME A USED CAMPER THAT HAS VERY BOLD,CRACKED ROTTED 4 TIRES, ALL ELECTRICAL ISSUES THROUGHOUT ENTIRE CAMPER AND HARNESS HITCH TOO MORE. THEY PROMISED ME IT WAS IN GREAT CONDITION & DELIVERED IT TOOK MY CHECK & LEFT. ALSO IT PASSED NYS INSPECTION THIS WAY? I AM CONCERNED BECAUSE THEY HAVE A USED VEHICLE LOT. HOWEVER I CAN'T ENJOY CAMPING UNTIL ALL THE REPAIRS ARE DONE.THIS H
... AS BEEN AN ONGOING SINCE DAY ONE & I AM BEING IGNORED BY THEM.I AM TAKING LEGAL ACTION AGAINST THEM UPSTATE TRUCK & RV 93US RT 20, SENECAFALLS NY 13148 JOHN OBRIEN & MICHAEL HUMPHREY OWNERSRead more
Incident date: Apr 25, 2017
UPSTATE TRUCK & RV SOLD ME A USED CAMPER THAT HAS VERY BOLD,CRACKED ROTTED 4 TIRES, ALL ELECTRICAL ISSUES THROUGHOUT ENTIRE CAMPER AND HARNESS HITCH TOO MORE. THEY PROMISED ME IT WAS IN GREAT CONDITION & DELIVERED IT TOOK MY CHECK & LEFT. ALSO IT PASSED NYS INSPECTION THIS WAY? I AM CONCERNED BECAUSE THEY HAVE A USED VEHICLE LOT. HOWEVER I CAN'T ENJOY CAMPING UNTIL ALL THE REPAIRS ARE DONE.THIS H
... AS BEEN AN ONGOING SINCE DAY ONE & I AM BEING IGNORED BY THEM.I AM TAKING LEGAL ACTION AGAINST THEM UPSTATE TRUCK & RV 93US RT 20, SENECAFALLS NY 13148 JOHN OBRIEN & MICHAEL HUMPHREY OWNERSRead more
Incident date: Apr 25, 2017
UPSTATE TRUCK & RV SOLD ME A USED CAMPER THAT HAS VERY BOLD,CRACKED ROTTED 4 TIRES, ALL ELECTRICAL ISSUES THROUGHOUT ENTIRE CAMPER AND HARNESS HITCH TOO MORE. THEY PROMISED ME IT WAS IN GREAT CONDITION & DELIVERED IT TOOK MY CHECK & LEFT. ALSO IT PASSED NYS INSPECTION THIS WAY? I AM CONCERNED BECAUSE THEY HAVE A USED VEHICLE LOT. HOWEVER I CAN'T ENJOY CAMPING UNTIL ALL THE REPAIRS ARE DONE.THIS H
... AS BEEN AN ONGOING SINCE DAY ONE & I AM BEING IGNORED BY THEM.I AM TAKING LEGAL ACTION AGAINST THEM UPSTATE TRUCK & RV 93US RT 20, SENECAFALLS NY 13148 JOHN OBRIEN & MICHAEL HUMPHREY OWNERSRead more
Incident date: Apr 10, 2017
I PURCHASED A 2017 COLEMAN TRAVEL TRAILER AND ON OUR VERY 1ST TRIP THE ELECTRONIC AWNING OPENED WHILE WE WERE DRIVING. THE OPERATION OF THE AWNING HAS TO HAVE SOMEONE STAND BY THE POWER CENTER AND HOLD THE BUTTON DOWN. NO ONE WAS IN THE TRAVEL TRAILER AND THE BUTTON WAS NOT HELD DOWN. NOW DUTCHMAN SAYS IT'S NOT THEIR PROBLEM BUT OURS. THEY ARE LABELING THIS AN ACCIDENT. HOW THE HECK CAN THIS BE AN
... ACCIDENT... IT IS A MANUFACTURER/MECHANICAL ISSUE AND SHOULD BE HELD TO THE COMPANY WHO MANUFACTURER THIS PRODUCT.... DO YOU NOT STAND BY YOUR PRODUCT????Read more
Incident date: Apr 21, 2017
WHEN STOPPING FOR FUEL WHILE PULLING THE RV ON APRIL 21 I NOTICED THE UNIT TILTING TOWARDS THE RIGHT SIDE. WHEN INSPECTED FURTHER I COULD SEE THERE THE FRAME HAD SPLIT NEAR THE SPRING MIDDLE MOUNTING AREA. THE SPRING BRACKET ON THE FRAME WAS BENT IN GIVING NO SUPPORT TO THE LEAF SPRINGS CAUSING THE UNIT TO SAG TO THE RIGHT SIDE. RV WAS TAKEN TO A REPAIR FACILITY WHERE IT IS CURRENTLY LOCATED AW
... AITING REPAIR.Read more
Incident date: Jan 31, 2017
THE BRAKE WIRING WAS INSTALLED FROM THE FACTORY IN SUCH A MANNER THAT RESULTED IN DAMAGED INSULATION, DISCONNECTED WIRES AND DAMAGED PARTS. THIS CREATED INTERMITTENT SHORTING, RESULTING IN LOSS OF ALL BRAKING ON THE TRAILER.
Incident date: Apr 15, 2017
FLOOR IS BUCKLING, COULD LEAD TO FOOT GOING THROUGH FLOOR.
Incident date: Sep 8, 2014
WINDOWS WERE MANUFACTURED IN MEXICO. WINDOWS DO NOT FIT AND IMPROPERLY INSTALLED.CLAIM WAS MADE AND AND DENIED WITHIN WARRANTY PERIOD. KEYSTONE AFTER WARRANTY WAS OUT CHANGED COMPLAINT TO ANOTHER CAUSE WITHOUT INSPECTION AND DENIED AGAIN AS OUT OF WARRANTY. THE WORST CUSTOMER SERVICE I HAVE EVER EXPERIENCED.
Incident date: Apr 6, 2017
THE SPARE TIRE HAS A COVER AND THE TRAILER HAS ALWAYS BEEN STORED IN A TEMPERATURE-CONTROLLED GARAGE. THE TIRE WAS INSTALLED ON THE TRAILER (IN THE RIGHT REAR POSITION) FOR THE FIRST TIME, PRESSURE CHECKED (65 PSI), AND DRIVEN 25-30 MILES ON I-25 AT 60-62 MPH BEFORE SUFFERING A CATASTROPHIC BLOW-OUT (ACCOMPANIED BY A VERY LARGE "BANG"). THE ENTIRE TREAD AREA PEELED OFF THE TIRE AND A LARGE HOLE
... REMAINED IN THE TREAD AREA OF THE CARCASS WITH JAGGED STEEL BELT CORDS PROTRUDING. WHILE GETTING THE TRAILER STOPPED, THE FLAILING TIRE (VISIBLE IN THE REARVIEW MIRROR) REPEATEDLY STRUCK THE SIDE OF THE TRAILER. THE WHEEL MOLDING ON THE SIDE OF THE TRAILER ABOVE THE WHEELS WAS TORN OFF AND DISINTEGRATED. THE ALUMINUM PANEL ABOVE THE WHEELS WAS BADLY DAMAGED AND COMPACTED INTO THE AREA BEHIND THE WHEEL AND IN FRONT OF THE ACCESS STEPS. THE STEPS AND MAIN ACCESS DOOR WERE ALSO DAMAGED. THE UNDERBODY AREA WAS DAMAGED IN THAT THE BELLY COVERING AND INSULATION WERE SHREDDED. THIS TIRE WAS A POWER KING TOWMAX STR SIZE ST225/75R15 IDENTIFIED BY DOT 83B4GPB1010.Read more
Incident date: Oct 22, 2016
CARBON 387: REAR ELECTRIC BED WITH INTEGRATED COUCH WAS REPLACED DUE TO DEFECTS IN OUTER SEATING MATERIAL. SAFETY RELEASE LATCHES (1 EACH SIDE OF BACK REST) THAT WERE PRESENT IN THE ORIGINAL DESIGN TO PREVENT UNINTENDED PINCH AND/OR INJURY FROM COUCH SEAT BACK ARTICULATION ARE COMMUNICATED BY DEALER TO BE DISCONTINUED BY THE MANUFACTURER. ARTICULATING SEAT BACK MOVES FROM A HORIZONTAL TO A VERTICA
... L POSITION ON LINKAGE BARS THAT ACT IN A "SCISSOR-LIKE" MOTION. WITHOUT DUAL RELEASE LATCHES (AS ARE INSTALLED ON REMAINING 7 SEAT BACKS) THE RISK OF INJURY TO FINGERS, UNINTENDED PINCH, IS GREATLY INCREASED.Read more
Incident date: Jul 18, 2016
ALUMINUM FRAMEWORK CONSTRUCTING THE MAIN LIVING AREA SLIDE-OUT PROTRUDES INTO THE TIRE AREA AND CONTACTS THE REAR TIRE DURING JOUNCE CONDITIONS. [PICTURE SHOWN IS FRAMEWORK PULLED AWAY FROM BODY SIDE - AS SHOWN BY MOLDING MISMATCH]
Incident date: Jul 18, 2016
CARBON 387: REAR ELECTRIC BED WITH INTEGRATED COUCH HAS MANUALLY ARTICULATING AND LOCKING SUPPORT LEGS ATTACHED. SUPPORT LEG LOCKS LOOSEN AND DO NOT STAY ENGAGED AFTER USE. UNEXPECTED FAILURE TO STAY IN THE STOWED POSITION CREATES A HIGH RISK FOR INJURY DURING LOADING AND UNLOADING OF THE GARAGE AREA.
Incident date: Oct 22, 2016
CARBON 387: ARTICULATING ROOF ACCESS LADDER FASTENERS (MULTIPLE) LOOSEN AND BACK OUT OF THE SIDE WALL DURING ROAD MOTION/ USE. LADDER BRACKETS BEGIN TO SEPARATE FROM SIDE WALL CREATING AN UNSAFE CLIMBING CONDITION.
Incident date: Oct 28, 2016
ATWOOD FURNACE MODEL AFMD35131A CONTROL CARD FAILURE DUE TO DESIGN ERROR THAT PLACES THE CONTROL CARD IN AN AREA WHERE CONDENSATION FROM THE MOTOR COLLECTS. CARD FAILURE CAN RESULT IN POTENTIAL LOSS OF CONTROL OF THE PROPANE SUPPLIED FURNACE AND OVERHEATING AND FIRE. ATWOOD HAS A RELOCATION KIT FOR THE CARD BUT IT HAS NOT BEEN ANNOUNCED AS A RECALL.
Incident date: Feb 17, 2017
BOLT FAILED ON THE AXLE HANGER WHILE TRAVELING DOWN THE ROAD .
Incident date: Jul 28, 2016
WHILE ON I 290 NORTH IN MA. OUR TIRE BLEW OUT AND HIT THE CURB AND DID DAMAGE TO BOTH SIDES OF FIFTH WHEEL . THEN UPON ARRIVAL AT DESTINATION, THE OTHER 3 TIRES HAD BUBBLES . A TOW TRUCK CAME AND PUT ON OUR SPARE.
Crash
Incident date: Jul 28, 2016
WHILE ON I 290 NORTH IN MA. OUR TIRE BLEW OUT AND HIT THE CURB AND DID DAMAGE TO BOTH SIDES OF FIFTH WHEEL . THEN UPON ARRIVAL AT DESTINATION, THE OTHER 3 TIRES HAD BUBBLES . A TOW TRUCK CAME AND PUT ON OUR SPARE.
Crash
Incident date: Jul 28, 2016
WHILE ON I 290 NORTH IN MA. OUR TIRE BLEW OUT AND HIT THE CURB AND DID DAMAGE TO BOTH SIDES OF FIFTH WHEEL . THEN UPON ARRIVAL AT DESTINATION, THE OTHER 3 TIRES HAD BUBBLES . A TOW TRUCK CAME AND PUT ON OUR SPARE.
Crash
Incident date: Jun 24, 2015
TL* THE CONTACT OWNS A 2015 KEYSTONE RAPTOR. THE CONTACT STATED THAT TOP DRIVER SIDE STEP FRACTURED WHILE ENTERING THE VEHICLE. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED WITH A FAULTY PIN THAT NEEDED REPLACEMENT. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER STATED THAT VIN WAS NOT INCLUDED IN NHTSA CAMPAIGN NUMBER: 16V825000 (EQUIPMENT). THE FAILURE MILEAGE WAS UNKNOWN.
Incident date: Oct 21, 2016
I WAS TAKING MY FIFTH WHEEL FROM MY HOUSE AND PUTTING IT IN TO STORAGE, ABOUT 4 MILES AWAY. I NOTICED WHEN ARRIVING, MY FIFTH WHEEL CAMPER WAS LEANING TO THE RIGHT. I CHECKED UNDER THE CAMPER AND NOTICED THE RIGHT REAR LEAF SPRING WAS NOT IN THE REAR HANGER BRACKET AND WAS LODGED UP INSIDE THE FRAME. I ALSO NOTICED RUBBING TO THE RIGHT REAR TIRE DUE TO THE SUSPENSION SYSTEM / LEAF SPRING. I USED
... THE HYDRAULIC LEVELING SYSTEM AND A PRY BAR AND HAMMER TO GET THE LEAF SPRING BACK IN TO THE REAR HANGER BRACKET. I THEN INSTALLED A HIGH TENSION BOLT I PURCHASED FROM FASTENAL TO GET IT TO A RV DEALERSHIP ABOUT 15 MILES AWAY. THE RV DEALER SERVICE DEPT. INSTALLED A NEW LIPPERT BOLT. THE ROADS FROM MY HOUSE TO THE STORAGE UNIT ARE OF VERY GOOD CONDITION AND A FEW TURNS FROM STREET TO STREET. I WAS DRIVING NO MORE THAN 45 MPH. I AM WONDERING WHAT DAMAGE MIGHT HAVE OCCURRED IF I WERE ON THE INTERSTATE TRAVELING AT A HIGHER RATE OF SPEED AND THIS LIPPERT BOLT OR ANOTHER OF THE ELEVEN HAPPENS TO SHEAR.Read more
Incident date: Aug 26, 2016
THE TIGHT REAR SHACKLE BOLTS FAILED ON THE LIPPERT AUTO ALIGNMENT SUSPENSION, CAUSING THE TRAILER WHEELS TO BECOME MISALIGNED FORCING THE TRAILER TO FORCE THE SUSPENSION TO TRACK TO THE LEFT. THE SHACKLE BOLTS FAILED TO THE NUTS BECAME LOOSE CAUSING THE SHACKLE PLATES TO FALL OFF THE TRAILER. THE CONDITION WAS DANGEROUS BECAUSE THE TRAILER COULD HAVE FLIPPED WHEN TOWED. I HAD TO HAVE THE TRAILER
... SUSPENSION REPAIRED. THE SHACKLE BOLTS WERE DETERMINED TO BE UNDERSIZED FOR THE TRAILER AND THE CORES HAD BEEN BORED TO ALLOW GREASE FITTING TO BE INSTALLED IN THE HEADS OF THE BOLTS WEAKENING THE STRUCTURAL STRNGTH. THE BOLTS WERE REPLACED WITH SOLID BOLTS AT ALL POINTS OF THE SUSPENSION TO PREVENT FURTHER FAILURE. I HAVE BEEN INFORMED BY MY DEALER THAT FOREST RIVER HAS RECALLED TRAILERS USING THE LIPPERT SELF-ALIGNING SUSPENSION BECAUSE THE SHACKLE BOLTS SHEAR OFF. THIS ISSUE WOULD BE EXACTLY THE SAME ISSUE AS MINE. MORE IMAGES AVAILABLE!Read more
Incident date: Dec 4, 2016
CARBON MONOXIDE AND FIRE HAZARD. ON DECEMBER 4, 2016 WHILE CAMPING IN MESA, AZ WE ENCOUNTERED A HEAVY RAIN. AFTER TURNING ON THE FURNACE WE SMELLED SOMETHING OUT OF THE ORDINARY AND THE FURNACE WAS HARD TO IGNITE. FURNACE WAS SHUT DOWN AND AFTER EXTENSIVE INVESTIGATION IT WAS DISCOVERED THAT SMELL CAME FROM THE FURNACE COMBUSTION CHAMBER. IT WAS FOUND THAT A METAL VENT COVER THAT COMBINES INTAK
... E COMBUSTION AIR AND AN EXHAUST OPENING BELOW IT HAD LOUVERED HORIZONTAL OPENINGS POINTED UP, THAT ALLOWED RAINWATER AND OTHER WATER FLOWING DOWN THE SIDE OF THE TRAVEL TRAILER TO ENTER THE ENCLOSED COMBUSTION CHAMBER. INVESTIGATION OF THAT PROBLEM LED TO VARIOUS WEB-SITES WHERE OTHER PEOPLE HAD ENCOUNTERED SIMILAR PROBLEMS. THE WATER INFILTRATION INTO THE COMBUSTION CHAMBER PRESENTS A HAZARD TO THE OCCUPANTS OF THE TRAILER, IN THAT IT CAN SHORT OUT THE ELECTRONIC BOARD THAT RUNS THE FURNACE AND IT CORRODE THE CHAMBER AND CREATE HOLES IN THE CHAMBER THEREBY ALLOWING THE COMBUSTION FROM INSIDE THE COACH DEPRIVING THE OCCUPANTS OF OXYGEN. A SILENT KILLER! THE MANUFACTURER OF THE LAREDO MK240 WERE NOTIFIED BY HAS FAILED TO ACT OTHER THAN TO LET ME KNOW THAT I SHOULD TAKE TO TRAILER TO THE DEALER, (A 40 MILE TREK) AND THAN KEYSTONE WOULD DECIDE IF THEY WANTED TO 'PARTICIPATE IN THE REPAIR'. THE MANUFACTURER OF THE FURNACE MAY ALSO BE AWARE OF THE PROBLEM, SINCE THE PROBLEM HAS BEEN DISCUSSED ON WEB-SITES. THIS CONDITION ON MANY RV'S, AND TRAVEL TRAILERS PRESENTS A DANGER OF NOT ONLY A FIRE BUT ALSO OF POSSIBLE SUFFOCATION OF THE OCCUPANTS OF ANY AFFECTED RV'S AND TRAVEL TRAILERS. WEB LINKS AND PHOTOS ENCLOSED. HTTP://WWW.FORESTRIVERFORUMS.COM/FORUMS/F113/NEW-ATWOOD-FURNACES-AFMD-SERIES-79088.HTML HTTP://WWW.ARFC.ORG/RVS/KEYSTONE/LAREDO/RECALLS.ASPX *TRRead more
Incident date: Oct 26, 2016
I BOUGHT THIS KEYSTONE LAREDO 295RK IN 2012. THE CAMPER CAME WITH POWER KING TOWMAX STR ST235/80R/16E TIRES. THEN IN OCT 2015 THE RIGHT REAR SEPARATED INTERNALLY, BUT DID NOT GO FLAT, DATE CODE 4910 CALLED MANUFACTURER AND THEY ADJUSTED TIRE. THEN IN OCT. 2016 ANOTHER TIRE SEPARATED RIGHT FRONT POWER KING TOWMAX STR ST235/80R/16E DATE CODE 4910 CAUSING DAMAGE TO CAMPER, CALLED WRECKER AND HAD
... SPARE INSTALLED. AT THE TIME THE TIRE BLEW I WAS DRIVING ON 2 LANE STATE HIGHWAY WITH SPEED LIMIT OF 45. GOT TO CAMP GROUND 1/4 MILE AWAY AN INSPECTED OTHER TIRES AND THE FOUND THAT THE LEFT FRONT HAD AND INTERNAL SEPARATION, BUT STILL HOLDING AIR, POWER KING TOWMAX STR ST235/80R/16E DATE CODE 4910. I STILL HAVE THE TIRE THAT BLEW ON THE RIGHT FRONT AND THE INTERNAL SEPARATION ON THE LEFT FRONT. THE OTHER 2 TIRES OUT OF THE 5 ORIGINAL TIRES HAVE THE SAME DATE CODE 4910. THE MARKINGS ON THE TIRE ARE DOT 83B5 GPB 4910. CONTACTED MANUFACTURER AND THEY WILL GIVE ME A CREDIT FOR 3 TIRES AND WILL PICKUP 3 TIRES, AFTER I HAVE TIRES REPLACED AND THEY INSPECT TO SEE IF IT IS THE FAULT OF THE TIRE. THEY ALSO HAVE OPENED A DAMAGE CLAIM. MY PROBLEM, THESE TIRES ARE NOT READILY AVAILABLE IN MY AREA, HAD TO BUY A HERCULES TIRE TO REPLACE THE LEFT FRONT. I WOULD LIKE TO SEE IF YOU CAN CHECK THESE TIRES AND MAKE THE DETERMINATION SINCE I FEEL THE MANUFACTURER WILL NOT BE TOTALLY HONEST ABOUT THE RESULTS.Read more
Incident date: Nov 8, 2016
I HAVE A 2014 MONTANA FIFTH WHEEL TRAILER NOT YET THREE YEARS OLD. I HAD A MASSIVE BLOW OUT ON THE FRONT DRIVERS SIDE TIRE ON 11/08/2016 ON THE INTERSTATE GOING 58MPH. AFTER GOING TO THE NEAREST LES SCHWAB DEALER IN NAPA IDAHO ONLY TO BE TOLD THAT ALL FOUR TIRES WERE SEPARATING AND NEEDED TO BE REPLACED. THIS RIG IS LESS THAN THREE YEARS OLD WITH ABOUT FOUR THOUSAND MILES ON THE TIRES. I FEEL THAT
... THEIR IS A DEFECT IN GOODYEAR MARATHON ST TIRES AND SHOULD BE RECALLED AND OWNERS COMPEDRead more
Incident date: Nov 15, 2016
SUSPENSION SHACKLE BUSHINGS WEARING IN LESS THAN 3000 MILES MOUNTING BOLTS TO SHACKLES LOOSE LOCK NUT. NO MANUAL THAT STATES OPERATOR HAS TO HAVE SUSPENSION SERVICED . HAVE HAD WHEEL BEARING REPLACED IN SAME FRONT AXLE TWICE BECAUSE OF WHEEL OVERHEATING CAUSING BRAKE DUST.
Incident date: Oct 17, 2016
TL* THE CONTACT OWNS A 2013 KEYSTONE LAREDO EQUIPPED WITH SUTONG, TIRE LINE: SUPERCARGO, TIRE SIZE: ST 235/80R16 TIRES (N/A). THE CONTACT STATED THAT WHILE DRIVING AT AN UNKNOWN SPEED, AN ABNORMAL VIBRATING AND RUMBLING SOUND EMITTED FROM THE VEHICLE. THE CONTACT PULLED OVER AND DISCOVERED THAT THE FRONT PASSENGER SIDE TIRE HAD BLOWN OUT. THE VEHICLE WAS NOT DIAGNOSED HOWEVER, THE CONTACT REPLACED
... THE TIRE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE TIRE FAILURE MILEAGE WAS 500. THE DOT NUMBER AND VIN WERE UNAVAILABLE.Read more
Incident date: Mar 19, 2016
TL* THE CONTACT OWNS A 2004 KEYSTONE COUGAR FIFTH WHEEL EQUIPPED WITH A DOMETIC REFRIGERATOR. THE CONTACT STATED THAT THE REFRIGERATOR CAUGHT FIRE. THE FIRE EXTINGUISHED INDEPENDENTLY. THERE WERE NO INJURIES AND A POLICE REPORT WAS NOT FILED. A TECHNICIAN DIAGNOSED THAT THE REFRIGERATOR NEEDED TO BE REPLACED AND SERVICED PER NHTSA CAMPAIGN NUMBERS: 08V325000 (EQUIPMENT) AND 08E032000 (EQUIPMENT).
... THE VEHICLE WAS NOT REPAIRED DUE TO THE MANUFACTURER'S REFUSAL. THE VIN WAS UNAVAILABLE.Read more
Fire
Incident date: Sep 14, 2016
TL* THE CONTACT OWNS A 2016 KEYSTONE COUGAR RECREATIONAL VEHICLE. WHILE DRIVING VARIOUS SPEEDS, ALL FOUR TIRES STRUCK AGAINST THE FLOOR OF THE RV. THERE WERE NO WARNING INDICATORS ILLUMINATED. THE DEALER DIAGNOSED THAT THE VEHICLE NEEDED HEAVIER SPRINGS AND AXLES. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED. THE VIN WAS INVALID. THE APPROXIMATE FAILURE MILEAGE WAS 650. UPDATED 01/
... 06/17*LJ UPDATED 6/29/18*JBRead more
Incident date: Sep 13, 2016
TL* THE CONTACT OWNS A 2016 KEYSTONE COUGAR. WHILE DRIVING APPROXIMATELY 63 MPH, THE REAR DRIVER SIDE WHEEL FRACTURED WITHOUT WARNING. DUE TO THE FAILURE, THE FRONT PASSENGER SIDE TIRE FLATTENED. THE VEHICLE WAS TOWED AND HAD TO BE DRIVEN LESS THAN 20 MPH. THE VEHICLE WAS TAKEN TO THE REPAIR SHOP FOR INSPECTION. THE MANUFACTURER WAS NOT NOTIFIED. THE VIN AND FAILURE MILEAGE WERE UNKNOWN.
Incident date: Sep 13, 2016
TL* THE CONTACT OWNS A 2016 KEYSTONE COUGAR. WHILE DRIVING APPROXIMATELY 63 MPH, THE REAR DRIVER SIDE WHEEL FRACTURED WITHOUT WARNING. DUE TO THE FAILURE, THE FRONT PASSENGER SIDE TIRE FLATTENED. THE VEHICLE WAS TOWED AND HAD TO BE DRIVEN LESS THAN 20 MPH. THE VEHICLE WAS TAKEN TO THE REPAIR SHOP FOR INSPECTION. THE MANUFACTURER WAS NOT NOTIFIED. THE VIN AND FAILURE MILEAGE WERE UNKNOWN.
Incident date: Aug 7, 2016
TL* THE CONTACT OWNS A 2015 KEYSTONE ALPINE TRAILER. WHILE DRIVING APPROXIMATELY 55 MPH, THE ROOF BEGAN TO DETACH. THE CONTACT TOOK THE VEHICLE TO THE DEALER WHERE IT WAS DETERMINED THAT THERE WAS A MANUFACTURER DEFECT DUE TO THE FACT THAT THERE WAS NOT ENOUGH ADHESIVE ON THE VEHICLE TO KEEP THE ROOF ATTACHED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FA
... ILURE MILEAGE WAS UNKNOWN. UPDATED 11/07/16*LJ THE CONSUMER STATED WHILE DRIVING DOWN THE HIGHWAY, THE ROOF STARTED FLAPPING . IT WAS DETERMINED IT WAS A MANUFACTURING DEFECT. KEYSTONE COVERED THE COSTS. UPDATED 11/30/16.*JBRead more
Incident date: Aug 7, 2016
TL* THE CONTACT OWNS A 2015 KEYSTONE ALPINE TRAILER. WHILE DRIVING APPROXIMATELY 55 MPH, THE ROOF BEGAN TO DETACH. THE CONTACT TOOK THE VEHICLE TO THE DEALER WHERE IT WAS DETERMINED THAT THERE WAS A MANUFACTURER DEFECT DUE TO THE FACT THAT THERE WAS NOT ENOUGH ADHESIVE ON THE VEHICLE TO KEEP THE ROOF ATTACHED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FA
... ILURE MILEAGE WAS UNKNOWN. UPDATED 11/07/16*LJ THE CONSUMER STATED WHILE DRIVING DOWN THE HIGHWAY, THE ROOF STARTED FLAPPING . IT WAS DETERMINED IT WAS A MANUFACTURING DEFECT. KEYSTONE COVERED THE COSTS. UPDATED 11/30/16.*JBRead more
Incident date: Sep 7, 2016
ON SEPTEMBER 7 2016 I WAS TRAVELING WEST ON I 64 AT APROX. 4:00 PM IN TRAFFIC JUST AFTER MILE 19 I HERD A LOUD BANG AND SAW DEBRIS FLYING OFF OF THE RIGHT SIDE OF MY RV. I PULLED ON TO THE SHOULDER AND DISCOVERED THAT THE ENTIRE TREAD ON MY RIGHT REAR TIRE HAD SEPARATED CAUSING DAMAGE TO THE RIGHT WHEEL WELL AND KNOCKED OFF THE VALVE STEM FROM THE RIGHT FRONT TIRE LEAVING ME WITH 2 FLAT TIRES. I
... ALWAYS USE A TPMS AND AT THE TIME OF FAILURE THAT TIRE WAS AT 85 PSI AND A TIRE TEMPERATURE OF 109 DEGREES. AFTER GETTING HOME I INSPECTED THE TIRE AND FOUND THE FOLLOWING 2 SPLITS ON THE SIDE WALL ABOUT 4 INCHES APART RUNNING FROM BEAD TO BEAD, AN AREA OF OLD RUST ON THE STEEL BELTS, AND A FARE AMOUNT OF UNBOND OF THE RUBBER FROM THE STEEL BELT ALSO THE STEEL BELT WAS BROKEN IN A STRAIGHT LINE 90 DEGREES TO THE TREAD. MY RV IS STORED INDOORS SO THERE IS NO UV DAMAGE AND WHEN NOT IN USE I KEEP IT OFF OF THE GROUND ON BLOCKS.Read more