Showing 76,133 complaints for HYUNDAI
Incident date: Jul 11, 2025
The contact owns a 2020 Jeep Gladiator. The contact stated that upon starting the vehicle, the instrument panel was inoperable, and failed to display critical safety information. No warning lights were illuminated. The vehicle was taken to the dealer, who diagnosed a failure with the instrument panel. The contact was informed that instrument panel needed to be replaced. The vehicle was not repaire
... d. After investigating the failure, the contact related the failure to NHTSA Campaign Number: 24V652000 (Electrical System), but the VIN was not included. The manufacturer was notified of the failure and referred the contact to the NHTSA Hotline for assistance. The failure mileage was 87,000.Read more
Incident date: Feb 1, 2025
Scan Report done ! odometer 25266.Engine coolant bypass valve "A" control circuit failed test. Engine Control Module Code P2681-15. Message: factory service require !
Incident date: Jul 12, 2025
The issue involves the engine’s piston rings, which appear to be malfunctioning and causing excessive oil consumption. This has led to oil entering the combustion chamber and likely damaging the catalytic converter. The engine began consuming oil rapidly between oil changes — far more than normal — and has since developed engine knocking and performance issues. These symptoms are consistent
... with piston ring failure in other 2017 Kia Soul models that have been recalled, though my VIN is not currently included. • Component or system that failed: The likely failure is with the piston rings, which are allowing oil to burn inside the engine. This has begun to impact the catalytic converter as well. All parts remain installed and are available for inspection upon request. • Safety risks: This situation puts my safety and the safety of others at risk, as the engine could seize or stall unexpectedly due to low oil levels or catalytic converter failure. Excessive oil burning also increases the risk of internal engine fire and significantly affects emissions. • Has it been reproduced or confirmed? Yes. The issue has been confirmed by an independent mechanic, who documented abnormal oil loss, engine knocking, and suspected damage to the emissions system. • Has it been inspected by others? The vehicle has not been inspected by Kia, law enforcement, or insurance, but has been examined by a certified independent technician who suspects piston ring failure. • Warning lamps or symptoms: Yes. The check engine light came on, and engine performance began to decline. I also noticed knocking sounds and sluggish acceleration. These symptoms started a few months ago and progressively worsened. The oil was being consumed rapidly even though no visible leaks were found. • Assessment of incident and cause: Based on mechanic feedback and my experience, this appears to be a case of premature piston ring failure, which is causing oil to burn internally and is likely leading to catalytic damage.Read more
Incident date: Jul 5, 2025
The contact owns a 2015 Kia Optima. The contact stated while attempting to accelerate from a stop light, the vehicle stalled and failed to restart. The vehicle was later towed to the local dealer who diagnosed that the engine had failed and needed to be replaced. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was 126,000. The VIN was not availab
... le.Read more
Incident date: Jun 19, 2025
Windshield Camera overheats causing Crash Sensor Warnings, Lane Departure will not work. Cruise control will also not work.
Incident date: Jun 7, 2025
The contact owns a 2018 Ram 2500. The contact received notification of NHTSA Campaign Number: 24V896000 (SERVICE BRAKES, HYDRAULIC); however, the part to do the recall repair was unavailable. The local dealer and manufacturer were not yet contacted regarding the recall. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The contact had not expe
... rienced a failure. VIN tool confirms parts not available.Read more
Incident date: Jun 7, 2025
Steering would not return to center after a turn only for LEFT turns, even at higher speeds. Steering would be sticky at low speeds. Resulted in challenging to predict cornering particularly for left turns. Manufacturer replaced steering gear under warranty. OK now.
Incident date: Jun 7, 2025
Complaint ID: 11667442 Vehicle: 2024 Hyundai Sonata Mileage: 20,000 (approx.). Update Summary: This update concerns the persistent, severe Electronic Stability Control (ESC) steering malfunction previously reported. Current Status of Issue: The ESC steering defect remains unresolved. The vehicle was taken to an authorized Hyundai dealership on July 15, 2025, for re-diagnosis. The technician rep
... orted being unable to find any fault, despite the clear, dangerous, and recurring symptoms of steering control loss and near-collisions. The vehicle is still unsafe to operate due to this unaddressed safety hazard. Manufacturer's Response: During this recent service visit, Hyundai continued to refuse to provide a loaner vehicle for the diagnostic and repair period. This refusal places the driver at extreme risk due to the necessity of driving a vehicle with a known, uncorrected safety defect that has already failed a previous recall repair (performed June 6, 2025, RO 41686321 ). Impact: The vehicle's safety is severely compromised. The persistent ESC defect, combined with the manufacturer's inability to diagnose/repair it and refusal to provide safe alternative transportation, necessitates immediate intervention.Read more
Incident date: Jun 29, 2025
There is a feature to create a scheduled charge for the vehicle. This feature is stuck on, turning it off on the vehicle does not override the feature on the phone. The phone will not disable it. As a result, I am unable to charge my vehicle (until the scheduled time, presumably). Additionally, the feature to reset the TCAM system is non-responsive, which is one of the supposed fixes, how am I a
... ble to reset the system if the command to do so does not respond? Power cycling the infotainment did not work. Force closing the app did not work.Read more
Incident date: Jul 13, 2025
The car doesn't start after overnight, or after a period of no usage for a certain time. Push button doesn't start the engine, it takes 25-30 attempts to get it started. It keeps happening almost every day.
Incident date: Jul 10, 2025
Idle needle jumping when turning the car on. Delay in shifting gears and throttle response. Forward collision warning goes off at random times even when no cars are present.
Incident date: Jul 1, 2025
While driving my 2025 Kia Sportage on the highway with my [XXX] son in the back seat, we experienced a sudden and dangerous malfunction that prompted this report. I was operating the vehicle as intended driving at a safe speed in normal highway conditions when an unexpected alarm sounded and the vehicles automated braking system suddenly and forcefully activated without warning. This caused the c
... ar to come to a complete and abrupt stop in the middle of active highway traffic, despite there being no obstacle or reason to brake. The product involved is the 2025 Kia Sportage, specifically its driver assistance and braking systems. I was the driver, and my son was a passenger. We were using the vehicle for normal, everyday travel. As a direct result of the incident, both my son and I sustained injuries. We experienced significant whiplash from the abrupt stop. My son also suffered a twisted spine, and I sustained a torn ligament in my ankle. Beyond the physical injuries, the emotional trauma has been substantial. The fear and anxiety that followed especially for my son have had lasting effects. He remains anxious in vehicles, and Ive struggled with panic and stress when driving or even thinking about being on the road again. This incident was not only physically harmful, but deeply traumatic, and it has severely impacted our sense of safety and trust in a vehicle that was supposed to protect us. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)Read more
2 injured
Incident date: Jun 22, 2025
The car stalls randomly and does not enter fail-safe mode. The dealer says it is the transmission but the transmission has never shuddered or hesitated. I am reading that these vehicles have intelligent power modules in the hybrid inverter that fail and can cause stalling. I feel like the dealership is working with Toyota to avoid addressing the actual problem. In the meantime I was sent home in
... a vehicle that continues to stall randomly and does not enter fail-safe mode.Read more
Incident date: May 24, 2025
There is an issue with the transmission when i accelerate at a slow pace. The car shakes and vibrates. Theres a possibility of an issue with the transfer case 4x4. When i turn the steering wheel and drive, it feels like it locks. It feels like 4x4 is on and theres a odd sound as well. I took my car to Hamilton Chevrolet and paid for inspection. They told me that there was no issue, but the issues
... i mentioned earlier in this message was mentioned to them. Those issues are still occurring. This is a recall issue but when i put my VIN number in, my car shows that there is no recall on it. There was many people who mentioned this problem.Read more
Incident date: May 24, 2025
Windshield crack issues , had to change 2 windshield
Incident date: May 24, 2025
While driving, my entire dashboard lit up with every warning sound and symbol for the car. It would cycle through collision, airbags, braking, all of it. Luckily I was able to drive to a safe place. I let the car sit overnight and the alarms stopped. Took it to service and they could not recreate it and no codes showed up. Second time it happened, the warning sounds and lights didn’t stop. The c
... ar would jerk when I tried to put it in drive, so I had it towed to dealership. They have video and photos of it. After 2 weeks, they said it was fixed-a pin in a connector was bent. Had car for 3 days and it happened again. Had it towed again. They have had their ‘senior’ techs looking at it, and none can figure it out. There are Reddit posts with this same issue, as well as Hyundai group sites.Read more
Incident date: Jul 15, 2025
issue: Transmission safety complaint: immediate reduction in forward motion dealer: Dealer currently has the car, stuck transmission valve Solenoid's. Has the vehicle or component been inspected by the manufacturer: awaiting backorder part to see 30 days warning lights: Car had no current warning lights before car immediately down accelerated while on the highway.
Incident date: Jun 30, 2025
There is a recall (N182202780) for certain models of gm apparently, but my truck does not fall under the recall though it is the same exact problem with the brake vacuum. When pumping my brake pedal, my brakes become almost non responsive, causing me to back into my secondary vehicle.
Crash
Incident date: Jun 30, 2025
The contact owns a 2022 Chevrolet Silverado 1500. The contact received notification of NHTSA Campaign Number: 25V274000 (Engine and Engine Cooling); however, the part to do the recall repair was not yet available. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The contact stated that while driving at various speeds, there was an abnormal kn
... ocking sound coming from the engine compartment. The manufacturer was made aware of the issue and referred the contact to a dealer. The contact had taken the vehicle to a local dealer who performed a road test but had not diagnosed the vehicle. The dealer informed the contact that the VIN was under recall for the engine; however, the sound coming from the engine was normal. The vehicle was not repaired. The failure mileage was 24,414. VIN tool confirms parts not available.Read more
Incident date: Jul 14, 2025
The contact owns a 2023 Nissan Rogue. The contact stated while driving at an undisclosed speed, there was an abnormal sound coming from the vehicle and the engine was running rough. The contact stated that the transmission was slipping, and the vehicle hesitated while driving. No warning light was illuminated. The vehicle was not diagnosed or repaired by an independent mechanic or dealer. The cont
... act received notification of NHTSA Campaign Number: 25V437000 (Engine and Engine Cooling); however, the part to do the recall repair was not yet available. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The manufacturer was not made aware of the failure. The failure mileage was 61,000. VIN tool confirms parts not available.Read more
Incident date: Jul 13, 2025
The multipurpose camera has an internal failure at 105 thousand miles. This controls the automatic emergency braking, lane keep assist, adaptive cruise control, lane departure warning, and more. This safety features such as emergency braking, lane keep assist, and lane departure warning are important safety features. All of these features help drivers avoid collisions by acting to correct or avoi
... d collisions or accidents faster or earlier than drivers can react. The Honda dealership service department has confirmed that the multipurpose camera had an internal failure, but did not provide a reason and there was no inciting incident during driving or ownership that caused this. The Honda dealership service department has been inspected and diagnosed that the multipurpose camera had an internal failure. No, there were no warning lamps, messages, or other symptoms of the problem prior to the failure. They only appeared after the failure, and the failure happened without warning. The failure first appeared on July 7th, 2025.Read more
Incident date: Jul 7, 2025
My vehicle has the 10l80 transmission. It experienced shuddering as well as several rear wheel lock ups at highway speeds. The vehicle is now out of service, since May 19 2025. I have been told there is no answer to shipment of replacement parts.
Incident date: Jul 7, 2025
Wiring harness to rear window defogger melted causing the rear window to crack and shatter. Safe lite replaced the window and recommended the harness not be reconnected. Told me it was not uncommon. Vehicle was not being used at the time. It was in my driveway when the window blew outward. Inspected by Safe lite, Reported to Liberty Mutual. No warning light, rear defogger was not in use, car was
... off.Read more
Incident date: Jul 10, 2025
The contact owns a 2024 Ford F-150. The contact stated that while driving at an undisclosed speed, the oil change warning light illuminated. The service warning light was reset but the issue became a regular occurrence. The vehicle was taken to the dealer, and the contact was informed that the service light needed to be reset each time the light became illuminated. The vehicle was not repaired. Th
... e manufacturer was notified of the issue, a case was opened, and the contact was referred to the NHTSA Hotline for assistance. The failure mileage was 10,000.Read more
Incident date: Mar 26, 2025
windshield, I cracked my 3rd windshield in 18 months and approx 7 windshields in 10 years. I replace this vehicle annually with the identical make and model range rover. The smallest stone chips the windshield and the chip turns into long cracks across the windshield within hours to a couple of days. I have alerted Land Rover to this.
Incident date: Jul 13, 2025
The contact owns a 2025 Hyundai Tucson. The contact stated that while driving approximately 5 - 35 MPH, the Forward Collision Avoidance Automatic Emergency Braking system activated and applied the brakes unintendedly. The contact stated that the Forward Collision Avoidance message was displayed. The contact stated that several unknown warning lights were illuminated. The vehicle was taken to a loc
... al dealer where the vehicle was diagnosed and the contact was informed that no fault was found with the vehicle. The vehicle was not repaired. The manufacturer was notified of the failure. The approximate failure mileage was 5,380.Read more
Incident date: Jul 7, 2025
Incident 1 - Dashboard Electrical Failure Date: June 11, 2025 Mileage: approx. 10,000 Problem: Multiple dashboard error lights activated simultaneously, including false "dead battery" warnings despite the vehicle starting normally. The vehicle could not be shifted into gear and could not be shut off through normal ignition procedures, requiring manual battery disconnection to resolve. Incident 2
... - Power Steering System Failure Date: June 12-13, 2025 Problem: Complete power steering failure. Temporary resolution achieved by battery disconnection and reconnection, indicating systemic electrical issues. Incident 3 - CAN Bus Communication System Failure Date: July 6 and 9, 2025 Problem: Check engine light with diagnostic code U0073, indicating Controller Area Network (CAN) bus communication failure - a critical vehicle system malfunction. On July 11, 2025 my wife had the oil changed and the mechanic assured her, “It’s just a glitch ma'am, like a computer. Just restart the car 2 or 3 times.” Incident 4 - Recurring Power Steering Failure Date: July 12, 2025 Problem: “Service ESC and Power Steering”. Power steering system failed again, demonstrating that previous "fixes" were ineffective and the underlying defect persists.Read more
Incident date: Nov 24, 2024
Date of Incident or Diagnosis: 7/15/2025 I am writing to formally report a serious issue with my 2018 Ford Focus, which has required a full engine replacement due to a known and widespread defect — coolant intrusion into the engine cylinders, specifically cylinders 1 and 3. This is a manufacturing defect and not the result of normal wear and tear or improper vehicle maintenance. Coolant intrus
... ion leads to engine misfiring, overheating, stalling, and ultimately complete engine failure — posing both safety risks and a significant financial burden to owners. This issue is especially concerning as there is no check engine light or prior warning before the damage becomes irreparable. In my case, the damage was discovered only after experiencing performance issues and having the vehicle professionally diagnosed. This problem has been widely reported by other owners of 2018 Ford Focus and Escape vehicles with similar 1.5L EcoBoost engines. Ford has previously issued technical service bulletins (TSBs) and recalls for similar issues in other model years and engine variants, but this specific year and model have not yet been included — despite exhibiting the exact same symptoms and root cause. I strongly believe that this failure is a design and manufacturing defect, not an isolated incident. It is unfair to hold consumers responsible for the cost of an engine replacement due to a flaw that Ford is already aware of in similar vehicles. Requested Action: I urge the NHTSA to investigate this issue further and push for an official safety recall of 2018 Ford Focus vehicles affected by coolant intrusion. Engine failure while driving could pose a serious hazard to the driver and other motorists. Ford should be held accountable and required to cover the cost of repairs for all affected vehicles, not just those included in previous recall campaigns.Read more
Incident date: Jul 14, 2025
The contact owns a 2016 Ford Edge. The contact stated that while driving at an undisclosed speed, the temperature gauge indicated that the engine was overheating, prompting the contact to discontinue driving the vehicle. The check engine warning light was illuminated. The vehicle was towed to the dealer, who determined that coolant intrusion into cylinder #3 had resulted in damages to the engine.
... The contact was informed that the engine needed to be replaced. The vehicle was not repaired. After investigating the failure, the contact related the failure to Customer Satisfaction Program: 21N12. The manufacturer was notified of the failure, a case was opened, and the contact was referred to the NHTSA Hotline for assistance. The failure mileage was 56,000.Read more
Incident date: Jul 12, 2025
I had a flat tire while driving on 7/8/25 and THE TPMS error did not show up in the car screen. I informed the dealer Hoen Honda motors of Carlsbad, CA, and he mentioned that TPMS will not work for flat tire.
Incident date: Jul 12, 2025
The contact owns a 2019 Infiniti QX50. The contact stated while driving 40 MPH, the vehicle experienced a temporary reduction in engine power. The contact was able to pull over to the side of the road. The contact stated that the check engine warning light was illuminated. The failure became persistent with significant reduction in engine power while attempting to accelerate. The vehicle was taken
... to the dealer, who diagnosed that the variable compression actuator had failed and needed to be replaced. The vehicle was not repaired. The manufacturer was informed of the failure and offered a partial payment for the repair. The failure mileage was approximately 49,000.Read more
Incident date: Jul 12, 2025
When starting car warning lights came on for ABS, AEB, Cruise Control. Cruise control is locked out and not working due to these warnings.
Incident date: Dec 1, 2024
The contact owned a 2010 Ford Fusion. The contact stated that while her son was driving 35 MPH, the steering wheel locked, became difficult to maneuver, causing the contact son vehicle to encounter a tree. No warning light was illuminated. The air bag did not deploy. The contacts son called 911 after the failure. The contact son sustained injuries to the chest, face, back of his neck, and his knee
... s. A police report was filed. Medical attention was required. The vehicle was towed to Larry Campbell's Towing Garage. The insurance company deemed the vehicle a total loss. The vehicle's steering wheel was repaired once. The manufacturer was notified of the failure and closed contact case due to not being able to obtain the vehicle to remove a part of the vehicle. The failure mileage was 189,000.Read more
Crash
1 injured
Incident date: Dec 1, 2024
The contact owns a 2022 Ford Escape. The contact stated that while depressing the brake pedal there was an excessive amount of brake dust coming from the front brake pads. Additionally, there was an abnormal banging sound coming from the vehicle. There were no warning lights illuminated. The vehicle was taken to the local dealer, where it was diagnosed and determined that the brake pads and rotors
... needed to be replaced. The vehicle was repaired; however, the failure recurred. The manufacturer was contacted and filed a claim and referred the contact to the NHTSA Hotline to report the failure. The failure mileage was approximately 35,000.Read more
Incident date: Dec 1, 2024
The turbocharger failed on my 2017 Hyundai Santa Fe Sport 2.0T. It is still on the vehicle and available for inspection upon request. The turbo failure caused a severe loss of engine power, making acceleration dangerously slow and unpredictable, especially when merging onto highways or passing vehicles. This sudden reduction in power could have caused a rear-end collision or made it impossible to
... avoid faster-moving traffic. Yes. The failure was confirmed by two independent service centers: Mavis Tires and Brakes, and Tires and Trust in Pensacola, FL. Both observed loss of turbo boost and excessive oil consumption consistent with turbocharger failure. Yes. The vehicle was also inspected by Allen Turner Hyundai in Pensacola, FL. They did not detect the failure during their inspection, but the issue persisted and was documented by the other two shops. The check engine light came on around 118,000–119,000 miles. After that, the turbocharger lost significant power, making the vehicle unable to accelerate normally. At the same time, the engine began consuming oil at an abnormally high rate, requiring frequent top-offs between oil changes. This suggests internal oil seal failure in the turbo or related component issues. These symptoms are consistent with failed turbocharger bearings or seals, oil starvation, or blocked oil lines causing overheating and damage. Such failures can release oil and metal debris into the intake and exhaust systems, risking further engine damage or even fire. Hyundai previously issued a software update (KSDS) to detect early bearing wear in these engines, which my vehicle received in 2019 (Service Campaign 953). Despite this, the turbo failure still occurred, suggesting the underlying design or manufacturing issue may not have been fully resolved. I am requesting that NHTSA investigate this pattern of failures, given the safety risks of sudden power loss and potential fire hazard from oil leaks.Read more
Incident date: Jul 1, 2025
The problem is with the horn. Tesla instead of a regular horn has a SPEAKER under the car. So whenever it rains, the speaker gets wet and the horn gets muffled and barely audible, it’s a major concern. Not sure how anyone hasn’t done anything about it yet. Another thing is: the 2024 and 2025 tesla model 3 have blinkers on the steering wheel, the blinkers operate via capacitive buttons, which
... stop working for a few seconds if you accidentally rested your fingers on them, making you unable to use blinkers in a situation that quickly requires it.Read more
Incident date: May 22, 2025
Audi MMI (Muti Media Interface) constantly resets while driving the vehicle. The problem began about 4 months ago. The MMI would reboot very infrequently- about once every couple weeks. However, I took the vehicle in for a routine oil change yesterday and when I received the vehicle back, it now constantly resets as soon as it reboots. If I attempt to click a button (like accepting my user profile
... ) the screen immediately goes black. I believe this poses an extreme safety hazard given it can shut off while in reverse when the back up camera is engaged. It is also very distracting constantly seeing the MMI reboot and shut down as every time it reboots it asks for credentials/PINs/Users etc. Lastly, it's very dangerous because if I'm on a call it tries to constantly kick it over to the Bluetooth (but it doesn't work) so I have to manually put the phone back into speaker mode which is extremely distracting.Read more
Incident date: May 22, 2025
The contact owned a 2019 GMC Sierra 3500. The contact stated while driving at approximately 45 MPH, the vehicle went into “Engine Power Reduced Mode” and the contact attempted to pull over to the side of the road, but the contact stated that the battery went dead and the vehicle shutoff. The contact shifted to park(P) and attempted to restart the vehicle; however, the vehicle failed to restart
... , and smoke started coming from under the hood. The contact stopped attempting to restart the vehicle, and exited the vehicle and raised the hood, and the vehicle was on fire in the engine compartment on the left side of the firewall. The contact stated that there was gray and white smoke coming from the vehicle and an odor of electrical wires burning. The contact attempted to reach for a fire extinguisher but was informed by another driver who had stopped to see if the contact needed assistance, to step away from the vehicle. The other driver saw the flames coming from the engine compartment and told the contact to step away from the vehicle because it was unsafe to attempt to extinguish the flames, and the engine compartment became engulfed in flames. The Fire Department was contacted and arrived on scene and extinguished the fire. The contact stated that the front end of the vehicle and the front bumper, hood, engine, and engine components were damaged by the fire. Additionally, the front windshield was severely damaged. The vehicle was towed to an impound lot and declared a total loss by the Insurance provider. The contact stated that the Fire Department filed an incident report. The manufacturer was not informed of the failure. The contact related the failure and the fire to NHTSA Campaign Number: 21V496000 (Equipment) which was associated with the VIN. The failure mileage was approximately 242,000.Read more
Fire
Incident date: May 22, 2025
The "Auto Hold" feature on my Hyundai Ioniq malfunctioned, displaying a dashboard warning: "AUTO HOLD conditions not met. Press brake pedal." This message randomly appears while driving or stopping, and it deactivates the Auto Hold and Electronic Parking Brake (EPB) functions. In some cases, the car rolls after stopping because the system fails to hold the vehicle. This issue compromises vehicle
... safety, especially on inclines or during stop-and-go traffic. It puts me, passengers, and other drivers at risk. The problem has occurred multiple times and is unpredictable. It appears to be linked to a faulty brake switch or sensor, as noted in Hyundai’s TSB 23-BR-001H. I discovered this issue is affecting many other Hyundai Ioniq owners, as seen in this discussion: [XXX] The dealer has not yet inspected the vehicle, but the symptoms match the TSB. No accident has occurred, but the safety risk is serious due to brake failure behavior. There were no visible warning lights before the issue started, just the "Auto Hold" message when the failure happens. I bought the car from a used car dealer when it had 39,000 miles. Now it has around 74,000 miles. I’m not sure if it’s still under warranty. I haven’t taken it to the dealer yet, but the symptoms match exactly what other people are reporting online. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)Read more
Incident date: May 5, 2025
This is the same thong that was recalled on the other 2020 vw jetta..I also had a 2016 jettabefore I was allowed to trade it in for the 2020 jetta and the air went out on the both of them before the car was 2 years old. Now the 2020 has rain water coming in holding in the doors. When you open it the water comes out. What's showing is: 1.front assist not available 2. Fault electronic parking br
... ake 3. Transmission in emergency mode you can continue driving 4.only exit vehicle in P position service engine soon Number 3 has shown before and I had another transmission put in. Also engine light was on for the longest. I'm not sure of the exact date. I do have repair bills but I will have to go in my storage unit. Would like to send laterRead more
Incident date: Jul 15, 2024
I have serval codes from varies companies, O'Reilly's, Luther Nissan Dearlership from April to June 2025, the code is P0012, camshaft. The vehicle intermittently does not have power and I could easily be rear ended. Even thought Luther Nissan has had code P0012, camshaft they have not fixed it. I brought it to Luther Nissan 3 times since 4/22/25 to 6/2/25. Luther said,"Valvoline put transmission f
... luid in oil, said they drove it for 100 miles and found nothing, said old and current code on the same day and finally said you need a new battery. I bought a new battery. It happened again and I brought to a different certified shop on 7/11/25. Waiting to hear back. I have VERY detailed paperwork and many family/neighbors know. If I have an accident they know to sue Luther and Nissan.Read more
Incident date: May 14, 2025
Subject: Formal Complaint – 2018 Ram 1500 EcoDiesel Engine Failure at 11,900 Miles To Whom It May Concern at National Highway Traffic Safety Administration (NHTSA), I am filing a formal complaint regarding a major mechanical failure in my 2018 Ram 1500 EcoDiesel. Despite all scheduled maintenance being performed and documented, the engine failed at just 11,900 miles — a clear indication of a s
... erious defect or flaw in manufacturing. Vehicle Information: - Year/Make/Model: 2018 Ram 1500 EcoDiesel - VIN: [XXX] - Dealer: Elk Grove Dodge - Mileage at Failure: 11,900 miles I have researched and documented similar cases involving this engine model, pointing to a larger, systemic issue that warrants investigation. This premature engine failure poses a significant safety risk, especially if it were to occur while driving at highway speeds or in traffic. I am requesting a formal safety defect investigation and consideration for recall. What I Am Requesting: - Investigation into systemic engine issues affecting 2018 Ram 1500 EcoDiesel vehicles - Manufacturer accountability for premature failures under warranty - Consumer assistance in repair, buyback, or replacement under applicable laws or enforcement programs I am providing this documentation in the interest of resolving this matter through the proper regulatory channels. I respectfully request follow-up contact regarding next steps or findings. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)Read more
Incident date: May 14, 2025
Subject: Formal Complaint – 2018 Ram 1500 EcoDiesel Engine Failure at 11,900 Miles To Whom It May Concern at National Highway Traffic Safety Administration (NHTSA), I am filing a formal complaint regarding a major mechanical failure in my 2018 Ram 1500 EcoDiesel. Despite all scheduled maintenance being performed and documented, the engine failed at just 11,900 miles — a clear indication of a s
... erious defect or flaw in manufacturing. Vehicle Information: - Year/Make/Model: 2018 Ram 1500 EcoDiesel - VIN: [XXX] - Dealer: Elk Grove Dodge - Mileage at Failure: 11,900 miles I have researched and documented similar cases involving this engine model, pointing to a larger, systemic issue that warrants investigation. This premature engine failure poses a significant safety risk, especially if it were to occur while driving at highway speeds or in traffic. I am requesting a formal safety defect investigation and consideration for recall. What I Am Requesting: - Investigation into systemic engine issues affecting 2018 Ram 1500 EcoDiesel vehicles - Manufacturer accountability for premature failures under warranty - Consumer assistance in repair, buyback, or replacement under applicable laws or enforcement programs I am providing this documentation in the interest of resolving this matter through the proper regulatory channels. I respectfully request follow-up contact regarding next steps or findings. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6)Read more
Incident date: May 14, 2025
After a dealer-installed software update on my 2024 Hyundai Sonata sel awd, the car began jerking during acceleration and shifting. This happens at low and moderate speeds and creates an unsafe hesitation, especially in traffic. This issue did not exist before the update. I believe the software update affected the transmission or engine control calibration. The dealership has not resolved the iss
... ue, and it poses a safety concern. Please investigate whether this is linked to a faulty update affecting other Sonata vehicles.Read more
Incident date: Jul 14, 2025
I purchased a 2022 Forest River Clipper Model #272RLS on 10-28-2023. We put it in storage for the winter and took it out for the first time on May 19-2024. Driving down the freeway at 70 miles an hour the water tank fell out and was dragging on the road. We took it to the dealer the next day. We received a Recall NHTSA RECALL: 24V339 FOREST RIVER ID: 121-1777. The fix was to add another stra
... p. Myself and the dealership did not think this was adequate. We did not get our trailer back until 8-19-2024 and were unable to use it again. On June 26th we were taking it out for the first time and as we were filling it with water, the tank fell out of the brackets and ripped the hose. The tank was too small and the straps were not strong enough to hold the weight. I am very concerned about the safety hazard this could cause if someone else got the same fix. This could cause serious injury or death. Coachman put a bandage on it instead of being concerned about peoples safety and fixing it correctly. I am attaching some photos, the recall letter and the warranty invoice. If you need any further information please contact me. I believe these trailers should be recalled again and be fixed appropriately instead of allowing Coachman to save some money instead of saving a life.Read more
Incident date: Jul 8, 2025
I purchased a 2022 Forest River Clipper Model #272RLS on 10-28-2023. We put it in storage for the winter and took it out for the first time on May 19-2024. Driving down the freeway at 70 miles an hour the water tank fell out and was dragging on the road. We took it to the dealer the next day. We received a Recall NHTSA RECALL: 24V339 FOREST RIVER ID: 121-1777. The fix was to add another stra
... p. Myself and the dealership did not think this was adequate. We did not get our trailer back until 8-19-2024 and were unable to use it again. On June 26th we were taking it out for the first time and as we were filling it with water, the tank fell out of the brackets and ripped the hose. The tank was too small and the straps were not strong enough to hold the weight. I am very concerned about the safety hazard this could cause if someone else got the same fix. This could cause serious injury or death. Coachman put a bandage on it instead of being concerned about peoples safety and fixing it correctly. I am attaching some photos, the recall letter and the warranty invoice. If you need any further information please contact me. I believe these trailers should be recalled again and be fixed appropriately instead of allowing Coachman to save some money instead of saving a life.Read more
Incident date: Jul 14, 2025
While the car is parked and locked the rear driver side door opens in its own. The door handle does not present itself and is scheduled for repair. This is new and started happening today. Despite how many times I close it. It opens on it own. The door is locked when this happens. Door sitting still. Plugged in to charge and locked. The door opens on its own. It unlatches, Does not fully
... open.Read more
Incident date: May 6, 2025
Head gasket blown
Incident date: Jun 30, 2025
The contact owns a 2014 BMW 228I. The contact received notification of NHTSA Campaign Number: 24V608000 (Engine and Engine Cooling, Electrical System); however, the part to do the recall repair was not yet available. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The dealer was made aware of the issue and confirmed that parts were not yet a
... vailable. The manufacturer was made aware of the issue and confirmed that parts were not yet available. The contact had not experienced a failure. Parts distribution disconnect.Read more
Incident date: Jul 12, 2025
Lane keeping sensors periodically fault and Volvo's solution is to reboot the vehicle