Consumer Safety Complaints
Search 2,192,899 safety complaints filed by vehicle owners with NHTSA — including 137,559 crashes, 55,854 fires, and 8,555 deaths.
Showing 27,958 complaints for BUICK
Incident date: Oct 24, 2014
DRIVING TO WORK IN THE MORNINGS RECENTLY, I HAVE BEEN HAVING SOME ELECTRICAL ISSUES WITH MY CAR. IF I USE MY BLINKERS, ALL THE WARNING LIGHTS IN MY DASH CLUSTER WILL LIGHT UP FOR A FEW SECONDS, AND I COULD FEEL MY BRAKES PULSE. THIS MORNING MY CAR STALLED WHEN I MADE A RIGHT HAND TURN. I MANAGED TO PULL OVER AND RESTART THE CAR, BUT I DIDN'T USE THE BLINKERS AGAIN. THIS REALLY SCARED ME, AS I WAS ... Read more
Incident date: Oct 24, 2014
DRIVING TO WORK IN THE MORNINGS RECENTLY, I HAVE BEEN HAVING SOME ELECTRICAL ISSUES WITH MY CAR. IF I USE MY BLINKERS, ALL THE WARNING LIGHTS IN MY DASH CLUSTER WILL LIGHT UP FOR A FEW SECONDS, AND I COULD FEEL MY BRAKES PULSE. THIS MORNING MY CAR STALLED WHEN I MADE A RIGHT HAND TURN. I MANAGED TO PULL OVER AND RESTART THE CAR, BUT I DIDN'T USE THE BLINKERS AGAIN. THIS REALLY SCARED ME, AS I WAS ... Read more
BUICK
RENDEZVOUS
(2002) — AIR BAGS
Oct 27, 2014
Incident date: Oct 23, 2014
CAR STOPPED IN FRONT OF ME, WAS ROOM TO STOP IN TIME, HOWEVER ABS SYSTEM KICKED IN & PREVENTED VEHICLE FROM STOPPING - IT ONLY SLOWED IT DOWN. ROAD WAS CLEAR & DRY, NO NEED FOR ABS BRAKES. BRAKE PADS & REAR ROTORS WERE LESS THAN 3 WEEKS OLD & FRONT TIRES WERE ONLY 3 DAYS OLD AT TIME OF ACCIDENT. TESTED BRAKES BY REMOVING ABS FUSE & CAR STOPS GREAT - FAULT IN ABS SYSTEM. ALSO, AIR BAGS DID NOT DEPL... Read more
Crash
BUICK
RENDEZVOUS
(2002) — SERVICE BRAKES
Oct 27, 2014
Incident date: Oct 23, 2014
CAR STOPPED IN FRONT OF ME, WAS ROOM TO STOP IN TIME, HOWEVER ABS SYSTEM KICKED IN & PREVENTED VEHICLE FROM STOPPING - IT ONLY SLOWED IT DOWN. ROAD WAS CLEAR & DRY, NO NEED FOR ABS BRAKES. BRAKE PADS & REAR ROTORS WERE LESS THAN 3 WEEKS OLD & FRONT TIRES WERE ONLY 3 DAYS OLD AT TIME OF ACCIDENT. TESTED BRAKES BY REMOVING ABS FUSE & CAR STOPS GREAT - FAULT IN ABS SYSTEM. ALSO, AIR BAGS DID NOT DEPL... Read more
Crash
Incident date: Nov 28, 2008
TL* THE CONTACT OWNS A 2003 BUICK LESABRE. THE CONTACT STATED THAT THE DASHBOARD BEGAN SEPARATING AND EXPANDING DOWN TO THE PASSENGERS SIDE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS UNKNOWN.
Incident date: Jan 1, 2008
MY HORN STOPPED WORKING. THE PROBLEM WAS TRACED TO THE HORN SWITCH. MY MECHANIC COULD NOT REPLACE THE HORN SWITCH BECAUSE IT IS PART OF THE DRIVER'S SIDE AIR BAG ASSEMBLY, WHICH HAD BEEN DISCONTINUED. I HAD TO HAVE A BYPASS SWITCH INSTALLED ON THE DASHBOARD, WHICH IS INCONVENIENT AND AWKWARD TO USE. IN MY OPINION, THE HORN IS A MORE IMPORTANT SAFETY FEATURE THAN THE AIR BAG. I AM 71 YEARS OLD ... Read more
Incident date: Jan 1, 2008
MY HORN STOPPED WORKING. THE PROBLEM WAS TRACED TO THE HORN SWITCH. MY MECHANIC COULD NOT REPLACE THE HORN SWITCH BECAUSE IT IS PART OF THE DRIVER'S SIDE AIR BAG ASSEMBLY, WHICH HAD BEEN DISCONTINUED. I HAD TO HAVE A BYPASS SWITCH INSTALLED ON THE DASHBOARD, WHICH IS INCONVENIENT AND AWKWARD TO USE. IN MY OPINION, THE HORN IS A MORE IMPORTANT SAFETY FEATURE THAN THE AIR BAG. I AM 71 YEARS OLD ... Read more
Incident date: Oct 25, 2014
TL-THE CONTACT OWNS A 2007 BUICK LUCERNE. THE CONTACT RECEIVED A NOTIFICATION FOR NHTSA CAMPAIGN ID NUMBER: 14V355000 (ELECTRICAL SYSTEM) AND STATED THAT THE PART NEEDED WAS UNAVAILABLE TO SERVICE THE VEHICLE. THE DEALER WAS UNABLE TO ADVISE WHEN THE PART WOULD BECOME AVAILABLE. THE MANUFACTURER WAS NOT NOTIFIED OF THE DELAY. THE CONTACT HAD NOT EXPERIENCED A FAILURE. DJR
Incident date: Mar 29, 2013
WHILE DRIVING AT APPROX 40 MPH OR MORE THE ENGINE SUDDENLY CUTS OUT AND THE STEERING LOCKS UP AND THE CAR VIOLENTLY STOPS, WHICH COULD CAUSE A FATAL ACCIDENT. THIS IS VERY MUCH LIKE THE IGNITION SWITCH PROBLEM IN THE OTHER RECALLS. AFTER A FEW TRIES THE CAR DOES START AGAIN BUT THIS IS NOT ACCEPTABLE. ALSO THERE HAS BEEN SMOKE POURING FROM THE ENGINE ON MORE THAN ONE OCCASION WHEN THE VEHICLE WAS ... Read more
Incident date: Mar 29, 2013
WHILE DRIVING AT APPROX 40 MPH OR MORE THE ENGINE SUDDENLY CUTS OUT AND THE STEERING LOCKS UP AND THE CAR VIOLENTLY STOPS, WHICH COULD CAUSE A FATAL ACCIDENT. THIS IS VERY MUCH LIKE THE IGNITION SWITCH PROBLEM IN THE OTHER RECALLS. AFTER A FEW TRIES THE CAR DOES START AGAIN BUT THIS IS NOT ACCEPTABLE. ALSO THERE HAS BEEN SMOKE POURING FROM THE ENGINE ON MORE THAN ONE OCCASION WHEN THE VEHICLE WAS ... Read more
Incident date: Mar 29, 2013
WHILE DRIVING AT APPROX 40 MPH OR MORE THE ENGINE SUDDENLY CUTS OUT AND THE STEERING LOCKS UP AND THE CAR VIOLENTLY STOPS, WHICH COULD CAUSE A FATAL ACCIDENT. THIS IS VERY MUCH LIKE THE IGNITION SWITCH PROBLEM IN THE OTHER RECALLS. AFTER A FEW TRIES THE CAR DOES START AGAIN BUT THIS IS NOT ACCEPTABLE. ALSO THERE HAS BEEN SMOKE POURING FROM THE ENGINE ON MORE THAN ONE OCCASION WHEN THE VEHICLE WAS ... Read more
Incident date: Mar 4, 2014
I WAS DRIVING ON A ROAD AT ABOUT 35 MPH, I SIGNALED TO TURNED RIGHT AND MY VEHICLE WENT DEAD(THE ENGINE STOPPED-NO STEERING OR BRAKES.) FORTUNATELY,NO ONE WAS DRIVING BEHIND ME. I CAME TO A HALT AND TRIED STARTING THE ENGINE MULTIPLE TIMES, BUT ALL THAT HAPPENED WAS THE DASHBOARD LIGHTS WOULD FLASH. FINALLY, I TRIED MOVING THE TURN SIGNAL UP AND DOWN AND IT STARTED! SINCE THEN THIS HAS HAPPENE... Read more
Incident date: Mar 4, 2014
I WAS DRIVING ON A ROAD AT ABOUT 35 MPH, I SIGNALED TO TURNED RIGHT AND MY VEHICLE WENT DEAD(THE ENGINE STOPPED-NO STEERING OR BRAKES.) FORTUNATELY,NO ONE WAS DRIVING BEHIND ME. I CAME TO A HALT AND TRIED STARTING THE ENGINE MULTIPLE TIMES, BUT ALL THAT HAPPENED WAS THE DASHBOARD LIGHTS WOULD FLASH. FINALLY, I TRIED MOVING THE TURN SIGNAL UP AND DOWN AND IT STARTED! SINCE THEN THIS HAS HAPPENE... Read more
Incident date: Mar 4, 2014
I WAS DRIVING ON A ROAD AT ABOUT 35 MPH, I SIGNALED TO TURNED RIGHT AND MY VEHICLE WENT DEAD(THE ENGINE STOPPED-NO STEERING OR BRAKES.) FORTUNATELY,NO ONE WAS DRIVING BEHIND ME. I CAME TO A HALT AND TRIED STARTING THE ENGINE MULTIPLE TIMES, BUT ALL THAT HAPPENED WAS THE DASHBOARD LIGHTS WOULD FLASH. FINALLY, I TRIED MOVING THE TURN SIGNAL UP AND DOWN AND IT STARTED! SINCE THEN THIS HAS HAPPENE... Read more
Incident date: Nov 29, 2011
RETURNING FROM A MI TRIP ON PA RT 80, NOTICED PASSENGER AIR BAG WARNING LIGHT WAS OFF. SINCE THAT TIME, THE AIR BAG LIGHT HAS BEEN INTERMITTENTLY EFFECTIVE (SEE DIAGNOSTIC CHECK ON DEALER BILLING). RECENTLY, DEPUTY ADMINISTRATOR [XXX] HAS TESTIFIED A DEFECT WAS THE RESULT OF INACCURATE SUPPRESSION READ BY THE AIR BAG MODULE WHICH ACTIVATES THE SEAT BAG. WE HAVE BEEN TRAVELING SINCE, UNSURE... Read more
Incident date: Nov 29, 2011
RETURNING FROM A MI TRIP ON PA RT 80, NOTICED PASSENGER AIR BAG WARNING LIGHT WAS OFF. SINCE THAT TIME, THE AIR BAG LIGHT HAS BEEN INTERMITTENTLY EFFECTIVE (SEE DIAGNOSTIC CHECK ON DEALER BILLING). RECENTLY, DEPUTY ADMINISTRATOR [XXX] HAS TESTIFIED A DEFECT WAS THE RESULT OF INACCURATE SUPPRESSION READ BY THE AIR BAG MODULE WHICH ACTIVATES THE SEAT BAG. WE HAVE BEEN TRAVELING SINCE, UNSURE... Read more
Incident date: Apr 1, 2009
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. THE CONTACT STATED THAT WHILE OPERATING THE VEHICLE, THE PASSENGER SIDE AIR BAG LIGHT ILLUMINATED INDICATING THAT THE AIR BAGS SYSTEM WAS OFF. THE VEHICLE WAS TAKEN TO A DEALER WHO WAS UNABLE TO DIAGNOSE THE CAUSE OF THE PROBLEM. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE VIN WAS NOT AVAILABLE. THE FAILURE MILEAGE WAS 5,000.
Incident date: Mar 8, 2014
REAR VIEW CAMERA SYSTEM: WHEN BACKING OUT OF MY GARAGE DURING LIGHT HOURS THE DISPLAY IS USELESS. THE LIGHT SENSOR TAKES FROM ONE MINUTE TO FIFTEEN MINUTES BEFORE THE DISPLAY GOES BRIGHT. SINCE MY DRIVEWAY CROSSES A SIDEWALK THE DISPLAY IS USELESS IN THAT SITUATION AND A SAFETY HAZZARD. THE DEALER ADVISED ME THERE WAS NOTHING THEY COULD DO ABOUT IT. THE LIGHT SENSOR IS MOUNTED ON TOP OF THE DASHB... Read more
Incident date: Mar 8, 2014
REAR VIEW CAMERA SYSTEM: WHEN BACKING OUT OF MY GARAGE DURING LIGHT HOURS THE DISPLAY IS USELESS. THE LIGHT SENSOR TAKES FROM ONE MINUTE TO FIFTEEN MINUTES BEFORE THE DISPLAY GOES BRIGHT. SINCE MY DRIVEWAY CROSSES A SIDEWALK THE DISPLAY IS USELESS IN THAT SITUATION AND A SAFETY HAZZARD. THE DEALER ADVISED ME THERE WAS NOTHING THEY COULD DO ABOUT IT. THE LIGHT SENSOR IS MOUNTED ON TOP OF THE DASHB... Read more
Incident date: Aug 8, 2014
THE SERVICE VEHICLE SOON/ABS WARNING LIGHT/AND TRAC OFF LIGHT LIT AND THE CAR LURCHED AS IF THE BRAKES WERE APPLIED AT THE LEFT FRONT WHEEL. THE ERROR CODE WAS C1225, WHICH IS TOO MUCH SPEED AT THE LEFT FRONT WHEEL. THE BEARING AND SENSOR WAS REPLACED 3 TIMES AND THE PROBLEM STILL OCCURRED. THE MECHANIC ALSO REPLACED THE ABS PUMP MODULE (THE ELECTRONIC PART OF THE ABS UNIT) AND THEN HAD TO UPGR... Read more
Incident date: Aug 8, 2014
THE SERVICE VEHICLE SOON/ABS WARNING LIGHT/AND TRAC OFF LIGHT LIT AND THE CAR LURCHED AS IF THE BRAKES WERE APPLIED AT THE LEFT FRONT WHEEL. THE ERROR CODE WAS C1225, WHICH IS TOO MUCH SPEED AT THE LEFT FRONT WHEEL. THE BEARING AND SENSOR WAS REPLACED 3 TIMES AND THE PROBLEM STILL OCCURRED. THE MECHANIC ALSO REPLACED THE ABS PUMP MODULE (THE ELECTRONIC PART OF THE ABS UNIT) AND THEN HAD TO UPGR... Read more
Incident date: Aug 8, 2014
THE SERVICE VEHICLE SOON/ABS WARNING LIGHT/AND TRAC OFF LIGHT LIT AND THE CAR LURCHED AS IF THE BRAKES WERE APPLIED AT THE LEFT FRONT WHEEL. THE ERROR CODE WAS C1225, WHICH IS TOO MUCH SPEED AT THE LEFT FRONT WHEEL. THE BEARING AND SENSOR WAS REPLACED 3 TIMES AND THE PROBLEM STILL OCCURRED. THE MECHANIC ALSO REPLACED THE ABS PUMP MODULE (THE ELECTRONIC PART OF THE ABS UNIT) AND THEN HAD TO UPGR... Read more
Incident date: Jul 10, 2008
HAD TRANSMISSION REPLACED AT AUTHORIZED GMC DEALERSHIP MAY 2006 .THIS CAME WITH A WARRANTY. SEVERAL TIMES OVER SEVERAL SUMMERS SINCE THEN HAVE TAKEN VEHICLE INTO DEALERSHIP WITH CONCERNS THAT HAPPENED AFTER VEHICLE WOULD BE DRIVEN IN HIGH HUMIDITY HIGH TEMPERATURE DAYS AFTER TRAVELING A MINIMUM OF 60 MILES MOSTLY ON STATE HIGHWAYS THAT ARE QUITE ROUGH AND CURVY, I.E. IT WOULD TAKE ABOUT 90 MINUTE... Read more
Incident date: Jul 10, 2008
HAD TRANSMISSION REPLACED AT AUTHORIZED GMC DEALERSHIP MAY 2006 .THIS CAME WITH A WARRANTY. SEVERAL TIMES OVER SEVERAL SUMMERS SINCE THEN HAVE TAKEN VEHICLE INTO DEALERSHIP WITH CONCERNS THAT HAPPENED AFTER VEHICLE WOULD BE DRIVEN IN HIGH HUMIDITY HIGH TEMPERATURE DAYS AFTER TRAVELING A MINIMUM OF 60 MILES MOSTLY ON STATE HIGHWAYS THAT ARE QUITE ROUGH AND CURVY, I.E. IT WOULD TAKE ABOUT 90 MINUTE... Read more
Incident date: Oct 21, 2014
THE ENGINE DIED WITHOUT WARNING AND WOULD NOT RESTART. IT HAPPENED SHORTLY AFTER I PULLED OUT OF A PARKING AREA. THE MECHANIC SAID IT WAS A CRACKED IGNITION COIL THAT 'FRIED' THE IGNITION MODULE AND CORRESPONDING WIRES. HE ALSO SAID IN THIRTY YEARS HE HAS NEVER SEEN ANYTHING LIKE IT. IT WAS A VERY EXPENSIVE REPAIR FOR A VEHICLE WITH SO FEW MILES ON IT. HAD IT HAPPENED ON A HIGHWAY, IT WOULD HAVE B... Read more
Incident date: Oct 19, 2014
LOST POWER STEERING AT LOW SPEED. *TR
Incident date: Mar 20, 2012
AIRBAG DISPLAY SHOWS AIRBAG OFF INTERMITTENTLY WITH SEATBELT ON WITH AN ADULT IN PASSENGER SEAT WHILE MOVING ON HIGHWAY. *TR
Incident date: Sep 27, 2011
CONTROL MODULE FAILED AS I ENTERED THE DRIVEWAY, INTO MY GARAGE. THE KEY COULD NOT BE REMOVED. DIRECTIONAL CONTROL WAS LOST AND THE ENGINE WOULD NOT TURN OFF. THE BATTERY HAD TO BE DISCONNECTED TO TURN OFF THE ENGINE. THE KEY SWITCH FAILED ONCE BEFORE, WHEN THE TUMBLER WITHIN THE IGNITION SWITCH STUCK OPEN WHEN THE KEY WAS REMOVED; BUT THE IGNITION CIRCUIT REMAINED OPEN. CONSEQUENTLY, THE BATTERY... Read more
Incident date: Oct 18, 2014
IN FATHER'S CAR. DOORS LOCKED, BUT REAR DOOR WAS AJAR. CLOSED THE DOOR AND THEN IT WOULDN'T UNLOCK FOR SEVERAL DAYS DESPITE MANUAL, ELECTRONIC, AND OTHER ATTEMPTS. *TR
Incident date: Sep 29, 2014
THE CAR IMPACTED THE OTHER CAR BY TURNING LEFT INTO THE PATH OF THE ONCOMING CAR. THE FRONT END OF THE BUICK WAS SERIOUSLY DAMAGED AND CAR SUBSEQUENTLY "TOTALED" BY THE INSURANCE COMPANY. THE AIRBAGS DID NOT DEPLOY WHICH RESULTED IN BROKEN BONES AND BRUISES TO THE DRIVER. *TR
Crash
Incident date: Sep 29, 2014
THE CAR IMPACTED THE OTHER CAR BY TURNING LEFT INTO THE PATH OF THE ONCOMING CAR. THE FRONT END OF THE BUICK WAS SERIOUSLY DAMAGED AND CAR SUBSEQUENTLY "TOTALED" BY THE INSURANCE COMPANY. THE AIRBAGS DID NOT DEPLOY WHICH RESULTED IN BROKEN BONES AND BRUISES TO THE DRIVER. *TR
Crash
Incident date: Sep 29, 2014
THE CAR IMPACTED THE OTHER CAR BY TURNING LEFT INTO THE PATH OF THE ONCOMING CAR. THE FRONT END OF THE BUICK WAS SERIOUSLY DAMAGED AND CAR SUBSEQUENTLY "TOTALED" BY THE INSURANCE COMPANY. THE AIRBAGS DID NOT DEPLOY WHICH RESULTED IN BROKEN BONES AND BRUISES TO THE DRIVER. *TR
Crash
Incident date: Oct 16, 2014
WAS DRIVEN OFF THE ROAD BY ANOTHER VEHICLE I THEN HIT A POTHOLE AT THE SAME TIME MY PASSENGER DASH AIRBAG DEPLOYED. *TR
Incident date: Mar 12, 2014
WHILE DRIVING AT NIGHT LOW BEAMS STOP WORKING. HIGH BEAMS WORK. NUMEROUS COMPLAINTS ARE LOCATED ON VARIOUS WEBSITES OF SAME ISSUE. DEALERS CANT FIX. *TR
Incident date: Oct 20, 2014
TL* THE CONTACT OWNS A 2007 BUICK LACROSSE. THE CONTACT RECEIVED A NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM). HOWEVER, THE PART NEEDED TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
BUICK
RENDEZVOUS
(2003) — FUEL/PROPULSION SYSTEM
Oct 20, 2014
Incident date: Sep 24, 2014
GAS LEAKING OUT OF FUEL TANK. A RECALL ( NHTSA 0TV349000) HAD BEEN ISSUED WHICH THE OWNER NEVER RECEIVED DUE TO RECENT MOVES FROM ONE STATE TO ANOTHER STATE. REPAIR WAS COMPLETED AT A COST OF $988.65 WHICH THE OWNER HAD TO PAY. APPROXIMATELY 1 YEAR OUT OF THE 10 YEAR RECALL WARRANTY. *TR
BUICK
RENDEZVOUS
(2002) — AIR BAGS
Oct 20, 2014
Incident date: Aug 13, 2014
TL* THE CONTACT OWNS A 2002 BUICK RENDEZVOUS. THE CONTACT STATED WHILE DRIVING APPROXIMATELY 35 MPH, THE PASSENGER'S SIDE AIR BAG DEPLOYED INDEPENDENTLY. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC FOR DIAGNOSTIC TESTING. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE FAILURE RECURRED ON THE DRIVER'S SIDE. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS ... Read more
Incident date: Jul 4, 2011
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. THE CONTACT STATED WHILE DRIVING AT VARIOUS SPEEDS, THE STEERING COLUMN LATCH ADJUSTED INDEPENDENTLY. THE FAILURE OCCURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED. THE FAILURE HAD NOT BEEN REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 38,000. UPDATED 01/22/15*CN UPDATED 01/26/15*JB
Incident date: Apr 25, 2014
PASSENGER AIR BAG LIGHT ON THE DASHBOARD TURNED FROM "ON" TO "OFF" WITH 150 POUND PASSENGER SEATED IN THE FRONT PASSENGER SEAT. THE RED WARNING INDICATOR LIGHT ON INSTRUMENT PANEL ALSO CAME ON. IT STAYED ON FOR 2 OR 3 MILES THEN THE DASHBOARD LIGHT TURNED BACK TO "ON" AND THE RED WARNING INDICATOR LIGHT TURNED OFF. IT OCCURS INTERMITTENTLY ON MOST TRIPS, "ON" THEN "OFF" THEN BACK TO "ON". TYP... Read more
Incident date: Oct 20, 2014
TL* THE CONTACT OWNS A 2013 BUICK ENCORE. THE CONTACT RECEIVED A NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 14V488000 (SEATS). HOWEVER, THE PART NEEDED TO DO THE REPAIR WAS UNABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOT AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Aug 15, 2011
CHROME PLATED WHEELS ARE CORRODING AND/OR PEELING CAUSING LOSS OF TIRE PRESSURE. *TR
Incident date: Aug 11, 2014
THE HEADLAMPS BLOW OUT AND UPON EXAMINING THE BULB HOUSING THE WIRING AND THE CASING THAT THE REPLACEMENT BULBS IS SUPPOSE TO BE INSERTED IN IS BURNED OFF. THE WIRING AND THE CASING IS GONE. THE RECALL IS 12V484 IS NOT ADDRESSING THE CONCERN THAT I HAVE OF THE HEADLAMPS CLEARLY FAILING TO CONFORM TO FEDERAL MOTOR VEHICLE SAFETY STANDARDS BY BURNING OUT AND NOT GIVING ANY INDICATORS ON THE INFORMA... Read more
1 injured
Incident date: Jan 16, 2013
BRAKE LINE WAS RUSTED & WAS REPLACED. *TR
Incident date: Sep 24, 2014
PASSENGER AIR BAGS LIGHT REMAINS ON WHILE SEAT BELT IS IN PLACE, HAD THE PROBLEM FIX ONCE AND THE LIGHT STAYED MAYBE TWO WEEKS BUT HAS BEEN ON SINCE. *TR
Incident date: Jan 21, 2013
MY CAR WAS PARKED. THE KEY WAS STUCK IN THE IGNITION. THE CAR CAUGHT FIRE. *TR
Fire
Incident date: Jan 21, 2013
MY CAR WAS PARKED. THE KEY WAS STUCK IN THE IGNITION. THE CAR CAUGHT FIRE. *TR
Fire
Incident date: Oct 17, 2014
SERVICE AIRBAG WARNING LIGHT WAS ON FOR 4 DAYS. TOOK CAR INTO BUICK DEALERSHIP, THEY SAID THE LIGHT WASN'T ON AND COULDN'T FIND A PROBLEM. THE LIGHT WAS ON WHEN I DROPPED THE CAR OFF THAT DAY. THEY HAD MY CAR FOR 2 DAYS. GOT THE CAR BACK ON FRIDAY EVENING, 2 DAYS LATER THE LIGHT IS BACK ON. THERE IS A RECALL FOR THIS ISSUE IN 2013 MODELS, BUT SINCE THIS IS A 2014 I WANTED TO MAKE THIS KNOWN T... Read more
Incident date: Oct 17, 2014
AFTER DRIVING THE CAR TO SCHOOL MY DAUGHTER WAS UNABLE TO SHIFT THE CAR INTO GEAR. MY HUSBAND WENT TO THE CAR AND WAS ALSO UNABLE TO SHIFT. WE HAD THE VEHICLE TOWED TO OUR LOCAL GARAGE AND RECEIVED A CALL THIS MORNING THAT THE SHIFTER CABLE BROKE. THE TOTAL PRICE FOR REPAIR IS 360.00 I NOTICED THERE WAS A RECALL FOR A SIMILAR GM VEHICLE FOR THE SHIFT CABLE BREAKING AND A RECALL ISSUED IN THE C... Read more
Incident date: Oct 17, 2014
MY DAUGHTER DROVE THE CAR TO SCHOOL AND WHEN SCHOOL WAS OUT THE CAR WOULD NOT GO INTO GEAR. MY HUSBAND CAME AND TRIED TO GET THE CAR INTO GEAR BUT ALSO HAD NO LUCK. WE HAD TO HAVE THE CAR TOWED TO THE GARAGE FOR WORK. I LOOKED UP RECALLS AND NOTICED THE CADILLAC HAS A RECALL FOR THE SAME PART. TOTAL COST FOR DEALER PARTS AND TOWING, INSTALLATION AND LABOR IS $ 360.00. *TR