Showing 27,958 complaints for BUICK
Incident date: Feb 24, 2015
AFTER RETURNING FROM A TWO HOUR TRIP I PARKED MY CAR AT HOME. THE NEXT DAY I TRIED TO START MY CAR AND IT WOULD ONLY TURN OVER.A MECHANIC FOUND THE FUEL PUMP DEFECTIVE, FUEL PUMP RELAY BURNT AND THE POWER PANEL BURNT AS WELL.
Fire
Incident date: Feb 2, 2015
2012 BUICK LACROSSE. CONSUMER RECEIVED RECALL FOR VEHICLE AND IS REQUESTING REPAIRS. *TA THE ENGINE LIGHT ILLUMINATED. *JB
Incident date: Feb 2, 2015
2012 BUICK LACROSSE. CONSUMER RECEIVED RECALL FOR VEHICLE AND IS REQUESTING REPAIRS. *TA THE ENGINE LIGHT ILLUMINATED. *JB
Incident date: Dec 5, 2014
2011 BUICK REGAL. CONSUMER WRITES IN REGARDS TO VEHICLE REPAIR ISSUES. *SMD THE CONSUMER STATED HE RECENTLY NOTICED SEVERAL FLUID SPOTS UNDER THE VEHICLE. AN INSPECTION REVEALED THE TRANSMISSION COOLER LINES DETERIORATED WHICH CAUSED THE LEAK. *JB
Incident date: Feb 24, 2015
TL* THE CONTACT OWNS A 2003 BUICK RENDEZVOUS. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 07V349000 (FUEL SYSTEM, GASOLINE); HOWEVER, THE VIN WAS NOT INCLUDED IN THE RECALL. AFTER REFUELING, THE CONTACT NOTICED A FUEL SMELL AND OBSERVED A FUEL LEAKAGE. THE CONTACT INSPECTED THE TANK AND FOUND THAT THE NECK OF THE TANK WAS LEAKING AND THE FUEL TANK WAS FRACTURED. THE VEHICLE WAS TAK
... EN TO A DEALER. THE TECHNICIAN DIAGNOSED THAT THE FUEL SYSTEM NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 161,000.Read more
Incident date: Dec 22, 2014
TL* THE CONTACT OWNED A 2006 BUICK LACROSSE. WHILE DRIVING 35 MPH, THE HEAD LAMP LIGHTS SHUT OFF INTERMITTENTLY. THE CONTACT LOST VISIBILITY AND CRASHED INTO THE REAR OF ANOTHER VEHICLE. THE CONTACT SUSTAINED A CONCUSSION AND ANOTHER PERSON SUSTAINED SEAT BELT BRUISING WHICH REQUIRED MEDICAL ATTENTION. A POLICE REPORT WAS FILED. THE VEHICLE WAS COMPLETELY DESTROYED AND TOWED TO AN IMPOUND LOT. THE
... MANUFACTURER STATED THAT THE VIN WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING) . THE FAILURE MILEAGE WAS 62,000. UPDATED 3/24/15*CN UPDATED (/26?2017*CNRead more
Crash
2 injured
Incident date: Feb 7, 2015
WHILE I WAS GETTING READY TO MERGE ONTO A HIGHWAY I HEARD A "PINGING NOISE" THEN A "THUD". I IMMEDIATELY PULLED OVER TO FIND THE THE DRIVE TRAIN OR DRIVE SHAFT HAD JUST FALLEN OUT OF MY CAR ONTO THE ROAD. *JS
Incident date: Feb 9, 2015
TL*THE CONTACT OWNS A 2007 BUICK LUCERNE. THE CONTACT T STATED THAT THE MOTOR MOUNT FRACTURED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC. THE TECHNICIAN DIAGNOSED THAT THE MOTOR MOUNT NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 68,000.
Incident date: Sep 1, 2014
MY RAINER STARTED TO LOOSE AIR IN THE REAR SUSPENSION, AIR RIDE SYSTEM. AT THIS TIME THE COMPRESSOR WORKS AND DOES FILL THE AIR RIDE SUSPENSION BUT YOU CAN'T BE IN A HURRY TO GO ANYWHERE. YOU MUST LET THE CAR SIT WHILE RUNNING FOR SEVERAL MINUTES BEFORE YOU CAN LEAVE. IF YOU DON'T, YOU BOUNCE DOWN THE ROAD AND THAT COULD BE A DANGER TO YOU OR SOMEONE ELSE ON THE ROAD, I HAVE SPOKEN TO MY LOCAL
... DEALER ABOUT THE ISSUE AND THEY WOULD BE MORE THAN HAPPY TO CHARGE ME THOUSANDS OF DOLLARS TO FIX THE ISSUE. I THINK THIS IS SOMETHING THAT GM SHOULD TAKE CARE OF UNDER A SAFETY RECALL SINCE IT SEEMS TO BE A DESIGN FLAW. MY CAR ONLY HAS 70,500 MILES ON IT. *TRRead more
Incident date: Feb 19, 2015
I WAS DRIVING 70 MPH ON I-77 WHEN THE CAR SUDDENLY JERKED, FELT LIKE A DROP, AND THE CHECK ENGINE LIGHT WENT ON. I WAS ABLE TO PULL OFF THE ROAD AND FOR THE NEXT 4-5 MILES MY CAR WOULD NOT GET OUT OF FIRST GEAR. I HAD TO LEAVE IT IN A PARKING LOT AND TOW IT. *TR
Incident date: Jan 5, 2015
1. WHILE DRIVING, VEHICLE ENTERED "REDUCED POWER MODE" MAKING IT IMPOSSIBLE TO MAINTAIN SPEED. THIS IS A SAFETY ISSUE AS DRIVER LOSES ABILITY TO MAINTAIN SPEED WHILE TRAVELING WITH FLOW OF TRAFFIC AND WITH REDUCED ENGINE POWER, EVEN THE ABILITY TO PULL OUT OF THE LANE OF TRAVEL IS IMPAIRED. DEALER IDENTIFIED BAD THROTTLE BODY AS CAUSE AND REPLACED. 2. POWER STEERING PUMP FAILURE. IS
... SUE WAS IDENTIFIED DUE TO WHINING NOISE PRIOR TO COMPLETE FAILURE. HAD PUMP FAILED COMPLETELY, DRIVER COULD HAVE LOST CONTROL WITH POWER ASSIST NOT AVAILABLE WHILE DRIVING. PUMP WAS REPLACED AND NECESSARY ASSOCIATED REPAIRS MADE BY DEALER. *TRRead more
Incident date: Jan 5, 2015
1. WHILE DRIVING, VEHICLE ENTERED "REDUCED POWER MODE" MAKING IT IMPOSSIBLE TO MAINTAIN SPEED. THIS IS A SAFETY ISSUE AS DRIVER LOSES ABILITY TO MAINTAIN SPEED WHILE TRAVELING WITH FLOW OF TRAFFIC AND WITH REDUCED ENGINE POWER, EVEN THE ABILITY TO PULL OUT OF THE LANE OF TRAVEL IS IMPAIRED. DEALER IDENTIFIED BAD THROTTLE BODY AS CAUSE AND REPLACED. 2. POWER STEERING PUMP FAILURE. IS
... SUE WAS IDENTIFIED DUE TO WHINING NOISE PRIOR TO COMPLETE FAILURE. HAD PUMP FAILED COMPLETELY, DRIVER COULD HAVE LOST CONTROL WITH POWER ASSIST NOT AVAILABLE WHILE DRIVING. PUMP WAS REPLACED AND NECESSARY ASSOCIATED REPAIRS MADE BY DEALER. *TRRead more
Incident date: Feb 16, 2015
TL* THE CONTACT OWNS A 2002 BUICK LESABRE. THE CONTACT STATED THAT WHEN THE IGNITION WAS TURNED TO THE ON POSITION, THE VEHICLE BURST INTO FLAMES WITHOUT WARNING. A POLICE REPORT WAS NOT FILED AND THERE WERE NO INJURIES. THE VEHICLE WAS TOWED TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE INTAKE VALVE DID NOT CLOSE AND IGNITED THE FUEL GOING INTO THE ENGINE. THE VEHICLE WAS NOT REPAIRE
... D. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 136,000.Read more
Fire
Incident date: Jun 20, 2014
MY WIFE WAS TRAVELING SOUTH ON A 2 LANE ROADWAY,HEARD A LOUD BANG, LOST CONTROL OF STEERING AND CROSSED THE CENTERLINE , THEN SWERVED BACK ACROSS ROAD TO HER SIDE AND STRUCK A GUARDRAIL. LATER WE FOUND THAT THE RIGHT REAR BALL JOINT BROKE OFF CAUSING THE WHEEL TO COLLAPSE AND WHEN THE CAR SKIDDED OUT OF CONTROL THE LEFT REAR TIRE BLEW OFF THE RIM. THIS CAR HAD REGULAR MAINT. AND SERVICE. IF SHE WO
... ULD'VE HIT SOMEONE HEAD ON AND CAUSED A FATALITY NO ONE WOULD KNOW THE REAL CAUSE AND EVERYONE WOULD ASSUME SHE GOT DISTRACTED AND CAUSED THE ACCIDENT WHICH MAKES ME WONDER HOW MANY TIMES THIS OCCURRED AND NOBODY IS THE WISER. THE NTSB NEEDS TO MAKE BUICK ISSUE A SAFETY RECALL NOW! *TRRead more
Crash
1 injured
Incident date: Sep 19, 2014
DRIVING DOWN THE ROAD LOST LOW BEAM HEADLIGHTS AS WELL AS DAY TIME LIGHTS , SMELLED SMALL BURNING ODOR AND DISCOVERED THE HEADLIGHT CONTROL IN THE FUSE PANEL TO BE OVER HEATING AND BEGINNING TO BURN A HOLE IN THE FUSE PANEL UNDER THE HOOD. HAVE READ OF THIS HAPPENING TO SEVERAL OF THESE CARS WITH THE FUSE PANEL BEING THE DIRECT SOURCE DUE TO WIRES SHORTING OUT INTERNALLY, WHY IS THIS CAR NOT INCLU
... DED IN THE RECENT RECALL? *TRRead more
Fire
Incident date: Sep 19, 2014
DRIVING DOWN THE ROAD LOST LOW BEAM HEADLIGHTS AS WELL AS DAY TIME LIGHTS , SMELLED SMALL BURNING ODOR AND DISCOVERED THE HEADLIGHT CONTROL IN THE FUSE PANEL TO BE OVER HEATING AND BEGINNING TO BURN A HOLE IN THE FUSE PANEL UNDER THE HOOD. HAVE READ OF THIS HAPPENING TO SEVERAL OF THESE CARS WITH THE FUSE PANEL BEING THE DIRECT SOURCE DUE TO WIRES SHORTING OUT INTERNALLY, WHY IS THIS CAR NOT INCLU
... DED IN THE RECENT RECALL? *TRRead more
Fire
Incident date: Feb 2, 2015
I WAS DRIVING ON THE FREEWAY WHEN I PUT MY RIGHT BLINKER ON TO CHANGE LANES AND MY VEHICLE JUST COMPLETELY SHUT OFF ON ME. I PULLED TO THE SIDE OF THE ROAD MY CAR STARTED BACK UP AND CONTINUES TO DO SO BUT EVERY TIME I HIT MY BLINKER RIGHT OR LEFT MY VEHICLE SHUTS OFF. *TR
Incident date: Jan 1, 2015
TL* THE CONTACT OWNS A 2009 BUICK LACROSSE. THE CONTACT STATED THAT NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING) EXCEEDED A REASONABLE AMOUNT OF TIME FOR REPAIR. THE DEALER STATED THAT THE PARTS WERE NOT AVAILABLE FOR REPAIR. THE MANUFACTURER STATED THAT A SOLUTION FOR THE FAILURE HAD NOT YET BEEN DEVELOPED. THE VEHICLE WAS NOT REPAIRED. THE CONTACT HAD NOT EXPERIENCED THE FAILURE.
Incident date: Jul 17, 2014
TL* THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM); HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Jun 10, 2014
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. WHILE DRIVING 30 MPH, THE LOW BEAM HEADLIGHTS WERE ENGAGED AND BECAME INOPERABLE. THE FAILURE DISTORTED THE CONTACT'S VISIBILITY AND THE HIGH BEAM HEADLIGHTS WERE ACTIVATED IN ORDER TO CONTINUE DRIVING. THE VIN WAS INCLUDED IN NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING); HOWEVER, THE REMEDY WAS UNAVAILABLE TO PERFORM THE REPAIR. THE VEHICLE WAS
... NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE APPROXIMATE FAILURE MILEAGE WAS 48,000. UPDATED 4/6/15*CN...UPDATED 04/08/15 *BF UPDATED 04/14/15*JB UPDATED 9/22/2017*CNRead more
Incident date: Feb 12, 2015
TL* THE CONTACT OWNS A 2009 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER:14V755000 (EXTERIOR LIGHTING); HOWEVER, THE CONTACT STATED THAT THE RECALL REMEDY WAS NOT EFFECTIVE. WHEN THE CONTACT OPENED UP THE PANEL WHERE THE MODULE WAS REPLACED, HE DISCOVERED THAT THE FUSE PANEL WAS BURNING. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE FUSE PANEL N
... EEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 94,000. UPDATED 04/13/15*LJ UPDATED 9/21/2017*CNRead more
Fire
Incident date: Feb 12, 2015
TL* THE CONTACT OWNS A 2009 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER:14V755000 (EXTERIOR LIGHTING); HOWEVER, THE CONTACT STATED THAT THE RECALL REMEDY WAS NOT EFFECTIVE. WHEN THE CONTACT OPENED UP THE PANEL WHERE THE MODULE WAS REPLACED, HE DISCOVERED THAT THE FUSE PANEL WAS BURNING. THE VEHICLE WAS TAKEN TO THE DEALER WHERE IT WAS DIAGNOSED THAT THE FUSE PANEL N
... EEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 94,000. UPDATED 04/13/15*LJ UPDATED 9/21/2017*CNRead more
Fire
Incident date: Mar 5, 2014
TL* THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT STATED THAT THE HEADLIGHTS SHORTED INTERMITTENTLY FOR THE LOW BEAMS AND THE CONTACT HAD TO APPLY THE HIGH BEAMS AS AN INTERIM REPAIR. AS THE FAILURE PROGRESSED, THE LOW BEAMS WOULD ILLUMINATE AND THEN SHORTED WITH NO WARNING. MONTHS LATER, THE LOW BEAMS FAILED TO WORK ENTIRELY. THE VEHICLE WAS TAKEN TO THE AUTHORIZED DEALER WHO STATED THAT TH
... E PART WAS NOT AVAILABLE TO REPAIR ACCORDING TO NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING). THE CONTACT WAS ALSO WAITING FOR THE PART TO BECOME AVAILABLE TO PERFORM THE REPAIR FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM). THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND WAS UNABLE TO PROVIDE A REASONABLE TIMEFRAME TO SCHEDULE THE TWO RECALL REPAIRS. THE FAILURE MILEAGE WAS UNAVAILABLE.Read more
Incident date: Mar 5, 2014
TL* THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT STATED THAT THE HEADLIGHTS SHORTED INTERMITTENTLY FOR THE LOW BEAMS AND THE CONTACT HAD TO APPLY THE HIGH BEAMS AS AN INTERIM REPAIR. AS THE FAILURE PROGRESSED, THE LOW BEAMS WOULD ILLUMINATE AND THEN SHORTED WITH NO WARNING. MONTHS LATER, THE LOW BEAMS FAILED TO WORK ENTIRELY. THE VEHICLE WAS TAKEN TO THE AUTHORIZED DEALER WHO STATED THAT TH
... E PART WAS NOT AVAILABLE TO REPAIR ACCORDING TO NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING). THE CONTACT WAS ALSO WAITING FOR THE PART TO BECOME AVAILABLE TO PERFORM THE REPAIR FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM). THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND WAS UNABLE TO PROVIDE A REASONABLE TIMEFRAME TO SCHEDULE THE TWO RECALL REPAIRS. THE FAILURE MILEAGE WAS UNAVAILABLE.Read more
Incident date: Jan 12, 2015
TL* THE CONTACT OWNS A 2007 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING); HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Jan 7, 2013
LOW BEAM HEADLIGHTS GO OUT, SOMETIMES THEY WILL NOT COME BACK ON UNTIL CAR IGNITION IS TURNED OFF AND BACK ON SOMETIMES THEY DON'T COME BACK ON AT ALL, VERY DANGEROUS, GM HAS A RECALL BUT THEY SAY MY VIN NUMBER IS NOT COVERED, I HAVE TALKED TO LOCAL DEALER AS WELL AS GENERAL MOTORS CONCERNING THIS ISSUE WITH NO POSITIVE RESPONSE. IT APPEARS THIS ISSUE WILL BE JUST LIKE THE KEY SWITCH ISSUE, PEOPLE
... WILL HAVE TO DIE BEFORE ANYTHING IS DONE. *TRRead more
Incident date: Jan 7, 2013
LOW BEAM HEADLIGHTS GO OUT, SOMETIMES THEY WILL NOT COME BACK ON UNTIL CAR IGNITION IS TURNED OFF AND BACK ON SOMETIMES THEY DON'T COME BACK ON AT ALL, VERY DANGEROUS, GM HAS A RECALL BUT THEY SAY MY VIN NUMBER IS NOT COVERED, I HAVE TALKED TO LOCAL DEALER AS WELL AS GENERAL MOTORS CONCERNING THIS ISSUE WITH NO POSITIVE RESPONSE. IT APPEARS THIS ISSUE WILL BE JUST LIKE THE KEY SWITCH ISSUE, PEOPLE
... WILL HAVE TO DIE BEFORE ANYTHING IS DONE. *TRRead more
Incident date: Feb 6, 2015
TL*THE CONTACT OWNS A 2011 BUICK ENCLAVE. THE CONTACT STATED THAT THE REAR DRIVER'S SIDE COIL SPRING FRACTURED. THE VEHICLE WAS TAKEN TO A DEALER FOR DIAGNOSTIC TESTING. THE REAR DRIVER'S SIDE COIL SPRING WAS REPLACED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 55,000.
Incident date: Feb 10, 2015
IN 2012, MY 2008 BUICK ENCLAVE WAS RECALLED DUE TO A MALFUNCTION OF THE AIRBAG. THE RECALL NUMBER WAS #10085. THE VEHICLE WAS REPAIRED BY COLEMAN BUICK IN LAWRENCEVILLE, NJ IN 2012 AND THE COST OF THE REPAIRS WAS COVERED UNDER THE RECALL. ON FEB 10, 2015, I TOOK THE VEHICLE TO COLEMAN BUICK BECAUSE THE PASSENGER SIDE AIRBAG WAS NOT PERFORMING PROPERLY AGAIN. THE DEALER INDICATED THE "PASSENGER PRE
... SENCE MODULE" WAS NOT FUNCTIONING CORRECTLY AND THAT IT WOULD NEED TO BE REPLACED AT THE COST OF OVER $875. I DO NOT FEEL THIS IS FAIR OR PROPER SINCE THE VEHICLE HAS PREVIOUSLY BEEN RECALLED FOR AIR BAG ISSUES AND BECAUSE GM IS CURRENTLY RECALLING THOUSANDS OF VEHICLES FOR KNOWN AIRBAG DEFECTS. *TRRead more
Incident date: Jan 1, 2015
TL*THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT STATED WHILE DRIVING 72 MPH, THE LOW BEAM HEADLAMPS LOSS POWER WITHOUT WARNING. THE CONTACT STATED THE VEHICLE RESTARTED AND THE HEADLAMPS ILLUMINATED. THE FAILURE RECURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED NEITHER REPAIRED. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER: 14V755000 (EXTERIOR LIGHTING). THE VIN WAS NOT LISTED U
... NDER THE RECALL. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 89,000.Read more
Incident date: Jan 30, 2015
I TURNED THE KEY IN THE IGNITION TO START THE CAR. IMMEDIATELY, A VERY LARGE ROAR ( LIKE AN AIRPLANE) OCCURRED JUST AS THE ENGINE STARTED. I TURNED OFF THE IGNITION FEARFUL OF DAMAGE TO THE ENGINE, NOT KNOWING WHAT MIGHT HAPPEN. IT WOULD NOT RESTART. IT WAS TOWED TO THE DEALERSHIP TO HAVE IT REPAIRED. THE IGNITION COIL HAD RUPTURED, IGNITION MODULE WAS KNOCKED OUT. THE COST FOR REPAIR: $
... 800+. TWO WEEKS LATER, THE ENGINE LIGHT LIT UP ON THE DASH BOARD DISPLAY. I RETURNED TO THE DEALERSHIP FOR INVESTIGATION. THE SECOND REPAIR DIAGNOSIS REPAIR REQUIRED THE REPLACEMENT OF THE FUEL PUMP, THE OIL PRESSURE SENDER PUMP AND THE AIR INJECTOR PUMP ( NO CHARGE FOR THIS). COST: $1004.81. WHEN I TRIED TO DRIVE IT HOME, THE ENGINE LIGHT LIT UP AGAIN SO I RETURNED TO THE DEALERSHIP. THIS TIME THERE WAS A NEED TO REPLACE A EMISSION VALVE.( NO CHARGE). FIVE DAYS LATER, THE ENGINE LIGHT LIT UP AGAIN. DIAGNOSIS: CODE PO411, AIR INJECTOR PUMP MALFUNCTION. WILL SCHEDULE REPAIR NEXT WEEK ( FEBRUARY 14-21) THIS IGNITION COIL MALFUNCTION CAUSED ELECTRICAL FAILURES TO ELECTRONIC MODULE, THE FUEL PUMP, THE AIR INJECTOR PUMP, THE OIL PRESSURE PUMP AND THE EMISSION VALVE SO FAR, AT GREAT COST TO THE CONSUMER. MORE IMPORTANTLY, THE FEAR IS THAT THE IGNITION COIL RUPTURE AND RESULTING FAILURE COULD HAVE CAUSED AN ENGINE FIRE. THE SOUND WAS DEAFENING AND FELT LIKE AN EXPLOSION. I HAVE NEVER EXPERIENCED THIS KIND OF PROBLEM WITH ANY OTHER OF MY AUTOMOBILES. IT WAS A FRIGHTENING EXPERIENCE. *TRRead more
Incident date: Sep 8, 2014
TL*THE CONTACT OWNS A 2011 BUICK LUCERNE. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 40 MPH, THE VEHICLE ACCELERATED INDEPENDENTLY WITHOUT WARNING. THE FAILURE RECURRED TWO TIMES. THE VEHICLE WAS TAKEN TO A DEALER. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 19,400. THE VIN WAS UNAVAILABLE.
Incident date: Jun 14, 2014
DAMAGE ON DRIVE SIDE OF REAR BUMPER AND TRUNK LIGHT, INCLUDING TRUNK DAMAGE TO THE VEHICLE. *TR
Crash
Incident date: Oct 13, 2014
TL*THE CONTACT OWNS A 2007 BUICK LACROSSE. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 35 MPH, THE HEAD LOW BEAM LIGHTS SEIZED CAUSING THE CONTACT TO CRASH INTO THE DUMPSTER. AS A RESULT OF THE FAILURE, THE DRIVER SIDE HEAD LIGHT BECAME DAMAGED. THE VEHICLE WAS TAKEN TO THE DEALER. THE VEHICLE WAS REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE MILEAGE FAILURE WAS 2
... 03,000. ..UPDATED 02/24/15*BF UPDATED 9/21/2017*CNRead more
Incident date: Feb 9, 2015
TL* THE CONTACT OWNS A 2000 BUICK REGAL. WHILE DRIVING AT AN UNKNOWN SPEED, THERE WAS A LOUD ABNORMAL NOISE COMING FROM THE FRONT PASSENGER SIDE OF THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 150,000.
Incident date: Mar 4, 2013
TL*THE CONTACT OWNS A 2004 BUICK RAINIER. THE CONTACT STATED THAT THE LOW BEAM HEADLIGHT SOCKET MELTED CAUSING THE LIGHT TO SHAKE. THE FAILURE RECURRED NUMEROUS TIMES. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE HEAD LAMP MODULE NEEDED TO BE REPLACED, ALONG WITH REPLACEMENT OF THE LIGHT. THE VEHICLE WAS NOT REPAIRED. THE CONTACT REFERENCED NHTSA CAMPAIGN NUMBER
... : 14V755000 (EXTERIOR LIGHTING). THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 80,000.Read more
Incident date: Feb 2, 2015
LETTER FROM SENATOR RUBIO ON BEHALF OF CONSTITUENT RE 2005 BUICK LESABRE DEFECTS (ATTN: DAVID HUFF). *SMD THE CONSUMER STATED THE IGNITION SWITCH BROKE, AND WHEN HE EXITED THE VEHICLE THE INSTRUMENT PANEL STATED THE KEY WAS STILL IN THE IGNITION. ALSO, THE AIR BAG WAS PROTRUDING OUT OF THE DASHBOARD. THE CONSUMER WAS INFORMED THE RECALLS DID NOT APPLY TO HIS VEHICLE. *JB
Incident date: Feb 2, 2015
LETTER FROM SENATOR RUBIO ON BEHALF OF CONSTITUENT RE 2005 BUICK LESABRE DEFECTS (ATTN: DAVID HUFF). *SMD THE CONSUMER STATED THE IGNITION SWITCH BROKE, AND WHEN HE EXITED THE VEHICLE THE INSTRUMENT PANEL STATED THE KEY WAS STILL IN THE IGNITION. ALSO, THE AIR BAG WAS PROTRUDING OUT OF THE DASHBOARD. THE CONSUMER WAS INFORMED THE RECALLS DID NOT APPLY TO HIS VEHICLE. *JB
Incident date: Feb 2, 2015
LETTER FROM SENATOR RUBIO ON BEHALF OF CONSTITUENT RE 2005 BUICK LESABRE DEFECTS (ATTN: DAVID HUFF). *SMD THE CONSUMER STATED THE IGNITION SWITCH BROKE, AND WHEN HE EXITED THE VEHICLE THE INSTRUMENT PANEL STATED THE KEY WAS STILL IN THE IGNITION. ALSO, THE AIR BAG WAS PROTRUDING OUT OF THE DASHBOARD. THE CONSUMER WAS INFORMED THE RECALLS DID NOT APPLY TO HIS VEHICLE. *JB
Incident date: Jun 15, 2014
TL*THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT STATED THAT THE HEADLIGHTS FAILED. AS A RESULT, THE CONTACT HAD TO ACTIVATE THE HIGH BEAMS. THE VEHICLE WAS INCLUDED IN NHTSA CAMPAIGN ID NUMBER: 14V755000 (EXTERIOR LIGHTING) HOWEVER, THE PART WAS AVAILABLE. THE VEHICLE WAS TAKEN TO A DEALER WHERE SHE WAS INFORMED THAT ADDITIONAL REPAIRS WERE REQUIRED PRIOR TO THE RECALL REMEDY BEING PERFORME
... D. THE DEALER MENTIONED THAT THE WIRES WERE BURNED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS NOT AVAILABLE. UPDATED 04/06/15*LJRead more
Fire
Incident date: Jun 15, 2014
TL*THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT STATED THAT THE HEADLIGHTS FAILED. AS A RESULT, THE CONTACT HAD TO ACTIVATE THE HIGH BEAMS. THE VEHICLE WAS INCLUDED IN NHTSA CAMPAIGN ID NUMBER: 14V755000 (EXTERIOR LIGHTING) HOWEVER, THE PART WAS AVAILABLE. THE VEHICLE WAS TAKEN TO A DEALER WHERE SHE WAS INFORMED THAT ADDITIONAL REPAIRS WERE REQUIRED PRIOR TO THE RECALL REMEDY BEING PERFORME
... D. THE DEALER MENTIONED THAT THE WIRES WERE BURNED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS NOT AVAILABLE. UPDATED 04/06/15*LJRead more
Fire
Incident date: Jul 14, 2014
WHILE THE VEHICLE WAS PARKED IN OUR DRIVEWAY THE AIR SUSPENSION FAILED CAUSING THE REAR OF VEHICLE TO DROP TO AND UNSAFE LEVEL. UPON STARTING THE VEHICLE THE COMPRESSOR REFILLED THE SUSPENSION BAGS BUT WHEN PARKED AND NOT DRIVEN FOR ANY PERIOD OF TIME THE AIR BAGS LEAK DOWN CAUSING THE REAR SUSPENSION TO DROP DOWN AGAIN. THIS HAS BEEN HAPPENING FOR SEVERAL MONTHS NOW AND I UNDERSTAND THAT THIS IS
... NOT AND UNCOMMON PROBLEM WITH THIS MAKE AND MODEL VEHICLE. THE VEHICLE NOW HAS ONLY 50,000 ACTUAL MILES AND HAS NEVER BEEN USED FOR TOWING. *TRRead more
Incident date: Dec 1, 2014
TL*THE CONTACT OWNS A 2003 BUICK RENDEZVOUS. THE CONTACT STATED THE VEHICLE FAILED TO ACCELERATE UP AN INCLINE. THE CONTACT MENTIONED THAT WHEN TRAVELLING AT A STEADY SPEED, THE VEHICLE JERKED VIOLENTLY. THE FAILURE RECURRED ON NUMEROUS OCCASIONS. THE VEHICLE HAD NOT BEEN DIAGNOSED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 117,000.
Incident date: Feb 5, 2015
DIC SAID RIGHT FRONT HEADLIGHT OUT,TOOK TO DEALER,SAID BALLAST BURNED UP INSIDE HEADLIGHT ASSEMBLY PUT ON ORDER, WAITING FOR REPAIR AT THIS TIME. *JS
Incident date: Oct 12, 2013
10/2012 - (APROX 115,000 MILES ON VEHICLE) VEHICLE WAS TURNING LEFT ONTO A CITY STREET WHEN WITHOUT NOTICE THE RIGHT REAR BALL JOINT BROKE OFF AND FORCED ME TO THE SIDE OF THE STREET. LUCKILY THERE WERE NO CARS DIRECTLY BEHIND ME. THE VEHICLE HAD TO BE TOWED AND REPAIRED. THE LEFT BALL JOINT WAS DEEMED GOOD AT THAT TIME. ONCE IN REPAIR, FRONT TIE RODS WHERE ALSO REPLACED IN PREVENTION OF ANY FAILU
... RE BECAUSE OF THERE POOR CONDITION. 2/2015 - (135,000 MILES ON VEHICLE) DRIVING VEHICLE DOWN MAJOR HIGHWAY AT 65 MPH THE LEFT REAR BALL JOINT BROKE WITHOUT NOTICE CAUSING ME TO SLIDE OUT OF CONTROL AND CRASH INTO A DITCH. ONLY BECAUSE THERE WAS NOT HEAVY TRAFFIC AND THE BLESSINGS OF THE LOCATION AND SNOW, DID I NOT SUFFER INJURIES TO MYSELF OR VEHICLE. 100 FT IN ANY OTHER DIRECTION WOULD OF RESULTED IN A DIFFERENT ENDING. THIS VEHICLE HAD BEEN SERVICED WITH TIRE REPLACEMENT AND ALIGNMENT WITHOUT ANY INDICATION OF BALL JOINT DISTRESS. I DO NOT FEEL SAFE IN THIS VEHICLE AND FEAR ANY OTHER MAJOR FAULT IN THE VEHICLE PARTS/DESIGN THAT MIGHT OCCUR WITHOUT NOTIFICATION. *TR UPDATED 3/31/16 *JSRead more
Crash
Incident date: Oct 12, 2013
10/2012 - (APROX 115,000 MILES ON VEHICLE) VEHICLE WAS TURNING LEFT ONTO A CITY STREET WHEN WITHOUT NOTICE THE RIGHT REAR BALL JOINT BROKE OFF AND FORCED ME TO THE SIDE OF THE STREET. LUCKILY THERE WERE NO CARS DIRECTLY BEHIND ME. THE VEHICLE HAD TO BE TOWED AND REPAIRED. THE LEFT BALL JOINT WAS DEEMED GOOD AT THAT TIME. ONCE IN REPAIR, FRONT TIE RODS WHERE ALSO REPLACED IN PREVENTION OF ANY FAILU
... RE BECAUSE OF THERE POOR CONDITION. 2/2015 - (135,000 MILES ON VEHICLE) DRIVING VEHICLE DOWN MAJOR HIGHWAY AT 65 MPH THE LEFT REAR BALL JOINT BROKE WITHOUT NOTICE CAUSING ME TO SLIDE OUT OF CONTROL AND CRASH INTO A DITCH. ONLY BECAUSE THERE WAS NOT HEAVY TRAFFIC AND THE BLESSINGS OF THE LOCATION AND SNOW, DID I NOT SUFFER INJURIES TO MYSELF OR VEHICLE. 100 FT IN ANY OTHER DIRECTION WOULD OF RESULTED IN A DIFFERENT ENDING. THIS VEHICLE HAD BEEN SERVICED WITH TIRE REPLACEMENT AND ALIGNMENT WITHOUT ANY INDICATION OF BALL JOINT DISTRESS. I DO NOT FEEL SAFE IN THIS VEHICLE AND FEAR ANY OTHER MAJOR FAULT IN THE VEHICLE PARTS/DESIGN THAT MIGHT OCCUR WITHOUT NOTIFICATION. *TR UPDATED 3/31/16 *JSRead more
Crash
Incident date: Jan 30, 2015
TL*THE CONTACT OWNS A 2011 BUICK REGAL. THE CONTACT STATED THAT THE VEHICLE STARTED TO SHAKE AND STALLED INTERMITTENTLY. THE CONTACT STATED THAT THE FAILURE OCCURRED DURING COLD WEATHER CONDITIONS. IN ADDITION, THE CONTACT STATED THAT THE VEHICLE FAILED TO ACCELERATE OVER 36 MPH. THE CONTACT ALSO STATED THAT THE VEHICLE WOULD ACCELERATE INDEPENDENTLY INTERMITTENTLY. THE CONTACT MENTIONED THAT THE
... ELECTRONIC STABILITY CONTROL, THE ENGINE AND THE OIL WARNING LIGHTS ILLUMINATED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 44,000.Read more
Incident date: Jan 30, 2015
TL*THE CONTACT OWNS A 2011 BUICK REGAL. THE CONTACT STATED THAT THE VEHICLE STARTED TO SHAKE AND STALLED INTERMITTENTLY. THE CONTACT STATED THAT THE FAILURE OCCURRED DURING COLD WEATHER CONDITIONS. IN ADDITION, THE CONTACT STATED THAT THE VEHICLE FAILED TO ACCELERATE OVER 36 MPH. THE CONTACT ALSO STATED THAT THE VEHICLE WOULD ACCELERATE INDEPENDENTLY INTERMITTENTLY. THE CONTACT MENTIONED THAT THE
... ELECTRONIC STABILITY CONTROL, THE ENGINE AND THE OIL WARNING LIGHTS ILLUMINATED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 44,000.Read more
Incident date: Jan 31, 2015
TL*THE CONTACT OWNS A 2008 BUICK ENCLAVE. THE CONTACT STATED THAT THE STEERING WHEEL WAS EXTREMELY DIFFICULT TO TURN. IN ADDITION, THE STEERING WHEEL WAS SHAKING AND VIBRATING ALONG WITH AN ABNORMAL NOISE UPON TURNING. THE VEHICLE WAS TAKEN TO THE DEALER, WHO REPLACED THE POWER STEERING PUMP BUT THE FAILURE RECURRED. THE VEHICLE WAS TAKEN BACK TO THE DEALER WHERE THE FAILURE WAS UNABLE TO BE REPLI
... CATED. THE VEHICLE WAS THEN TAKEN TO AN INDEPENDENT MECHANIC, WHO DIAGNOSED THAT THE RACK AND PINION NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 46,000.Read more
Incident date: Feb 5, 2015
THIS IS A REOCCURRING ISSUE WITH THE CAR SHUTTING OFF COMPLETLY WHILE DRIVING OR LOSS OF ENGINE POWER. *TR