Showing 48,526 complaints — component: POWER TRAIN:AUTOMATIC TRANSMISSION
Incident date: Feb 17, 2010
BOUGHT THIS CAR IN 2010 EVER SINCE I HAD IT NIGHTMARE, THE AUTOMATIC TRANSMISSION WOULD BANG BETWEEN 1ST AND 2ND GEAR AT JUST NORMAL SPEED, THE TIRES WOULD SPIN BECAUSE OF THIS. IT ALSO WOULD SLIP OUT OF GEAR IN 3RD WITH SHIFTING UP SOMETIMES. BUT JUST RECENTLY I FOUND OUT THAT THE INTAKE TUBE FOR THE CAR HAD A GIANT HOLE IN IT. SO FIXED THAT AND ITS NOT REALLY BANGING 1ST AND 2ND BUT SLIPS A LITT
... LE BIT. *TRRead more
Incident date: Oct 19, 2011
TL* THE CONTACT OWNS A 2006 NISSAN PATHFINDER. WHILE DRIVING APPROXIMATELY 40 MPH, THE VEHICLE BEGAN TO VIBRATE WITH HESITATION. THE VEHICLE WAS ABLE TO REMAIN IN OPERATION. THE CONTACT LATER INSPECTED THE VEHICLE AND DETECTED THE TRANSMISSION FLUID WAS A BROWN COLOR AND THE RADIATOR COOLANT LEAKED INTO THE TRANSMISSION. THE MANUFACTURER WAS MADE AWARE OF THE PROBLEM. THE APPROXIMATE FAILURE MILEA
... GE WAS 71,867. THE VIN WAS NOT AVAILABLE. UPDATED11/29/11 *BF UPDATED 12/14/11Read more
Incident date: Nov 5, 2011
TL*THE CONTACT OWNS A 2006 FORD FIVE HUNDRED AWD. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 60 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO COAST TO THE SIDE OF THE ROAD AND RESTART THE VEHICLE AFTER SEVERAL MINUTES. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THEY ADVISED HIM THAT THE VALVE BODY IN THE TRANSMISSION NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED FOR T
... HE VALVE BODY. THE FAILURE AND THE CURRENT MILEAGES WERE APPROXIMATELY 95,000. UPDATED 12/06/11*LJ UPDATED 02/29/12Read more
Incident date: Oct 12, 2011
TL* THE CONTACT OWNS A 2003 BUICK REGAL. THE CONTACT STATED THAT THE VEHICLE WAS OVERHEATING AND WOULD LOSE POWER WITHOUT WARNING. THE VEHICLE WAS TAKEN TO THE DEALER WHERE HE WAS INFORMED THAT THE CATALYTIC CONVERTER, IDLE AIR CONTROL VALVE AND THE MANIFOLD ABSOLUTE PRESSURE WERE DEFECTIVE AND NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE NOR WAS THE VEHICLE REPAIRED.
... UPDATED 12/12/11*LJ THE CONSUMER STATED THE EXHAUST MANIFOLD FRONT AND REAR GLOWED REED HOT. THE ENGINE TEMPERATURE GAUGE WAS IN THE RED. COOLANT LEAKED FROM A HOSE NEAR THE ENGINE AND THE ENGINE BEGAN TO EMIT BLUE SMOKE. THE VEHICLE BURNED ONE QUART OF OIL EXCESSIVELY. THE BATTERY, THERMOSTAT, FRONT BRAKES, TRANSMISSION OIL FILTER AND GASKET WERE ALL REPLACED. ALSO, THE DRIVER REAR WINDOW WAS INOPERATIVE, THE WINDSHIELD WASHER WAS SPRAYER DID NOT WORK, THE CATALYTIC CONVERTER NEEDED TO BE REPLACED AND THE HEAT/AC BLOWER DID NOT OPERATE IN ALL THE SETTINGS. UPDATED 12/23/11Read more
Incident date: Oct 13, 2011
2002 VOLKSWAGEN JETTA. CONSUMER WRITES TO EXPRESS DISCONTENT REGARDING REPAIRS AT LOCAL DEALER *TGW THE CONSUMER STATED THREE DAYS AFTER RETRIEVING THE VEHICLE FROM THE DEALER, FOR MAINTENANCE WORK, THE VEHICLE BROKE DOWN ON THE HIGHWAY. THE PROBLEM WAS DETERMINED TO BE THE ALTERNATOR. *JB THE CONSUMER STATED HE WAS INVOLVED IN A HIT-AND RUN ACCIDENT IN WHICH THE REAR END IMPACT CAUSED DAMAGE T
... O THE TRANSMISSION. THE CONSUMER STATED EVEN THOUGH THE VEHICLE WAS REPAIRED, HE CONTINUED TO EXPERIENCE PROBLEMS WITH THE TRANSMISSION. UPDATED 12/08/11Read more
Crash
1 injured
Incident date: Nov 1, 2011
LETTER TO FROM RE A DANGEROUS AUTOMATIC TRANSMISSION FAILURE IN VOLKSWAGEN JETTAS *TGW
Incident date: Nov 1, 2011
2001 HONDA ODYSSEY. CONSUMER WRITES IN REGARDS TO TRANSMISSION PROBLEMS *TGW THE CONSUMER STATED THE VEHICLE WOULD SLAM INTO GEAR AND SLIP OUT OF GEAR. HONDA REPAIRED IT IN LATE 2009 UNDER WARRANTY. HOWEVER, LESS THAN TWO YEARS LATER, THE PROBLEM HAS RETURNED. THE CONSUMER STATED THE REPLACEMENT TRANSMISSION WAS ALSO DEFECTIVE. *JB
Incident date: Sep 28, 2011
TRANSMISSION DOES NOT SHIFT SMOOTHLY ANYMORE. IT SEEMS THAT 2ND GEAR IS GONE. THE CHECK ENGINE LIGHT COMES ON TOO. IT HAS THE RPM GO HIGH BEFORE SHIFTING. *TT
Incident date: Oct 22, 2011
TL* THE CONTACT OWNS A 2007 CADILLAC DTS. THE CONTACT STATED THAT WHILE DRIVING 50 MPH HE ATTEMPTED TO ACCELERATE FURTHER, BUT THE VEHICLE WOULD NOT RESPOND TO THE ACCELERATOR PEDAL. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER AND THE CONTACT WAS INFORMED THAT THE VEHICLE WOULD NOT DOWNSHIFT WHEN THE ENGINE RPMS REACHED 1500. THE CONTACT WAS ALSO INFORMED THAT THE VEHICLE WAS ENGINEERED TO OPERA
... TE IN THAT MANNER. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND THE CONTACT WAS AWAITING A RESPONSE. THE FAILURE MILEAGE WAS 15,300. THE CONSUMER STATED HE CAME TO A PASSING LANE ABOUT 1/4 MILE LONG AND PULLED OUT TO PASS. THE SHIFTER LEVER WAS IN "3" ON THE STEEP HILL. HE DEPRESSED THE ACCELERATOR TO ADVANCE INTO 2ND GEAR, BUT THE VEHICLE WOULD NOT DOWN SHIFT OR ACCELERATE. HE PULLED THE SHIFTER LEVER INTO 2ND . BUT THE TRANSMISSION STILL DID NOT DOWN SHIFT OR ACCELERATE. THE VEHICLE WAS TAKEN TO THE DEALER. AFTER AN EXAMINATION, THE CONSUMER WAS INFORMED THE TRANSMISSION WAS DESIGNED TO NOT SHIFT DOWN ABOVE 1500 RPM. IN CONTRAST, THE OWNER'S MANUAL WARNED NOT TO DOWN SHIFT INTO 2ND ABOVE 65 MPH BECAUSE IT MAY DAMAGE THE TRANSMISSION. UPDATED 11/17/11Read more
Incident date: Aug 19, 2011
WHILE BEING PARKED ON AN INCLINED HILL, MY EXPLORER WOULD NOT GET INTO GEAR. HAD TO CALL AAA TO TOW TO TRANSMISSION SPECIALIST WHO ADJUSTED THE GEAR BUT STATED YOU MIGHT HAVE MORE TRANSMISSION PROBLEMS. SINCE THEN MY CAR HAS HAD PROBLEMS WHERE THE GEARS HAVE BEEN GRINDING AS I'M DRIVING. I'M AFRAID I MIGHT HAVE MORE SERIOUS PROBLEMS IN THE FUTURE SINCE I'VE BEEN READING REPORTS FROM FORD OWNERS TH
... AT THIS IS BECOMING A MAJOR PROBLEM WITH FORD VEHICLES. *TTRead more
Incident date: Oct 25, 2011
TL* THE CONTACT OWNS A 2006 JEEP COMMANDER. THE CONTACT STATED THAT THE VEHICLE STALLED WHILE DRIVING 30 MPH. THE VEHICLE OPERATED AS NORMAL UPON RESTART. THE VEHICLE WAS TAKEN TO AN INDEPENDENT REPAIR SHOP AND THE CONTACT WAS INFORMED THAT THE TRANSMISSION CONTROL MODULE AND POWER TRAIN CONTROL MODULE FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND THE CON
... TACT WAS INFORMED THAT THE VEHICLE WAS NOT INCLUDED IN THE RECALL ASSOCIATED WITH NHTSA CAMPAIGN ID NUMBER 08V203000 (POWER TRAIN:AUTOMATIC TRANSMISSION:CONTROL MODULE (TCM, PCM)). THE FAILURE AND CURRENT MILEAGES WERE 50,000. UPDATED 11/10/11 *BFRead more
Incident date: Oct 10, 2011
TL* THE CONTACT OWNS A 2004 INFINITY QX56. THE CONTACT WAS DRIVING 50 MPH WHEN THE FRONT END OF THE VEHICLE BEGAN TO SHAKE. THE VEHICLE WAS TAKEN TO THE DEALER WHO PERFORMED A DIAGNOSTIC THAT LOCATED THE FAILURE AT THE FRONT SUSPENSION LOWER CONTROL ARMS. THE VEHICLE WAS TAKEN TO THE LOCAL MECHANIC TO HAVE THE FRONT LOWER CONTROL ARMS REPLACED. THE VEHICLE WAS REPAIRED. THE FAILURE MILEAGE WAS 110
... ,000 AND THE CURRENT MILEAGE WAS 119,000. THE CONSUMER AT HIS OWN EXPENSE, HE HAD TO REPLACE THE LEFT AND RIGHT CONTROL LOWER ARMS. THE CONSUMER STATED A RECALL WAS ISSUED IN MAY 2010. HOWEVER, HE WAS INFORMED THAT FOR HIS MODEL THE PARTS WERE NOT DEFECTIVE, AND THEREFORE DID NOT FALL UNDER THE RECALL. ALSO, ALL FOUR BELT PRE-TENSIONS HAD TO BE REPLACED ON BOTH SIDE. THE CONSUMER STATED ON FOUR SEPARATE OCCASIONS THE PRE-TENSIONS FAILED. EACH TIME THEY FAILED, IT RENDERED THE AIR BAGS NON-FUNCTIONAL. THE TRANSMISSION FAILED HAD TO BE REPLACED AT A COST OF $8000 DUE TO THE FAILURE OF A $10 SWITCH INSIDE THE TRANSMISSION, WHICH WAS RESPONSIBLE FOR THE REVERSE COMPONENT. THE WIPER FLUID MOTOR WAS DIAGNOSED AS BEING INOPERABLE. THE CONSUMER WAS INFORMED IT WOULD REQUIRE REPLACEMENT AT A COST OF A FEW HUNDRED DOLLARS. THE CONSUMER RECEIVED A SECOND OPINION AND WAS TOLD A HOSE HAD COME OFF AND RE-ATTACHED IT FREE OF CHARGE THE ENTIRE BRAKE ASSEMBLY, DRIVER SIDE WINDOW MOTOR, LIFT GATE MOTOR, TACHOMETER, DRIVER SIDE DOOR LOCK, HVAC CONTROL, BLOWER RESISTOR AND EXHAUST HEAT SHIELD ALL HAD TO BE REPLACED. . UPDATED 04/27/12Read more
Incident date: Aug 3, 2011
TL* THE CONTACT OWNS A 2011 TIFFIN ALLEGRO RV. WHILE DRIVING APPROXIMATELY BETWEEN 20-40 MPH THE BRAKES OVERHEATED AND SMOKE EMITTED INSIDE OF THE VEHICLE. THE CONTACT MANEUVERED TO THE SIDE OF THE ROAD TO INSPECT THE VEHICLE AND THEN CONTINUED TO DRIVE WITH CAUTION. THE VEHICLE WAS TAKEN TO AN AUTHORIZED DEALER WHERE THE FRONT AND REAR BRAKES WERE REPLACED. THE MANUFACTURER WAS MADE AWARE OF THE
... FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 3,500. UPDATED 10/26/11 *BF UPDATED 11/03/11 *BF UPDATED 12/15/11 *BF THE CONSUMER ALSO STATED THE TRANSMISSION WAS NOT SUFFICIENT ENOUGH TO SLOW THE RV DOWN ON STEEP GRADES. UPDATED 06/08/12 THE CONSUMER SUBMITTED AN ENGINEERING TESTING REPORT. UPDATED 06/22/12Read more
Incident date: Jun 6, 2011
TL* THE CONTACT OWNS A 2009 FORD F-150. THE CONTACT STATED THAT THE TRANSMISSION EXHIBITED A DELAY IN SHIFTING. THE CONTACT TOOK THE VEHICLE TO THE DEALER AND HAD THE TRANSMISSION CALIBRATED, BUT THE REPAIR ONLY LASTED FOUR TO FIVE DAYS BEFORE THE FAILURE RECURRED. THE DEALER THEN TOLD THE CONTACT THAT THE VEHICLE WAS DESIGNED TO SHIFT IN THE MANNER THAT IS WAS AND THAT THERE WAS NOTHING THAT COUL
... D BE DONE TO CORRECT THE FAILURE. THE CONTACT BELIEVED THE FAILURE WAS A SAFETY ISSUE BECAUSE THERE WAS A DELAY IN ACCELERATION GOING FROM SECOND TO THIRD GEARS. THE FAILURE MILEAGE WAS 18,500 AND THE CURRENT MILEAGE WAS 24,152. UPDATED 11/18/11*LJ THE CONSUMER ALSO STATED THERE WAS A DELAY GOING FROM FIRST TO SECOND GEAR. THE DEALER REPROGRAMMED THE TCM/PCM AND RESET THE ADAPTIVE SHIFT STRATEGIES. UPDATED 03/05/12Read more
Incident date: Oct 15, 2011
TL* THE CONTACT OWNS A 2010 FORD F-150. THE CONTACT STATED THE UNOCCUPIED VEHICLE BEGAN TO ROLL WHILE PARKED ON A LEVEL SURFACE AND CRASHED INTO A WOODEN FENCE. A POLICE REPORT WAS FILED. THE VEHICLE SUSTAINED MINOR DAMAGE TO THE FRONT END AND WAS TOWED TO AN AUTHORIZED DEALER WHERE IT WAS CURRENTLY BEING DIAGNOSED AND REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 20,000. UPDATED 11/04/11*LJ UP
... DATED 11/14/11 *BF UPDATED 11/21/11 UPDATED 12/16/11Read more
Crash
Incident date: Nov 25, 2009
2005 HONDA ACCORD. CONSUMER REQUEST FULL REIMBURSEMENT IN REGARDS TO RECALL REPAIRS *TGW THE CONSUMER STATED THE TRANSMISSION WAS MAKING A BAD WHINING SOUND. THE DEALER REPLACED THE TRANSMISSION AND TORQUE CONVERTER. *JB
Incident date: Oct 17, 2011
TL* THE CONTACT OWNS A 2006 CHRYSLER 300. THE CONTACT STATED THAT THE GEAR SHIFTER COULD NOT BE RELEASED FROM PARK. THE MANUFACTURER STATED THAT THE VEHICLE WAS NOT INCLUDED IN NHTSA CAMPAIGN ID NUMBER: 05V460000 (POWER TRAIN: AUTOMATIC TRANSMISSION) AND DENIED ASSISTANCE WITH THE REPAIR. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND THE CURRENT MILEAGE WAS 38,000. UPDATED 11/16/11*LJ UPDATED 11
... /18/11. *JBRead more
Incident date: Oct 11, 2011
TL* THE CONTACT OWNS A 2005 CHRYSLER 300 C. THE CONTACT STATED THAT VEHICLE FAILED TO SHIFT OUT OF PARK. THE VEHICLE WAS TAKEN TO A PRIVATE MECHANIC WHERE THE MECHANIC CONFIRMED THAT THE TRANSMISSION SHIFTER INTERLOCK LEVER NEEDED TO BE REPLACED. THE MANUFACTURER WAS CONTACTED AND THEY CONFIRMED THE VIN DID NOT QUALIFY FOR REPAIRS UNDER NHTSA CAMPAIGN ID NUMBER: 05V460000(POWER TRAIN:AUTOMATIC TRA
... NSMISSION). THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND CURRENT MILEAGES WERE 51,088. UPDATED 11/07/11 *BFRead more
Incident date: Oct 7, 2011
CAS ASKS THIS LETTER AND THE 92 COMPLAINTS ATTACHED HERETO BE PLACED IN THE DOCKET OF EA09-016 AND THAT FORD BE ORDERED TO RECALL ALL 2004-05 FORD FREESTAR, AND MERCURY MONTEREY VANS FOR DEFECTIVE TRANSMISSIONS.
Incident date: Oct 10, 2011
ON MONDAY NIGHT (AROUND MIDNIGHT) OCTOBER 10, 2011 I WAS TAKING MY HUSBAND FOR A ROUTINE VISIT TO THE HOSPITAL FOR STROKE RELATED PROBLEMS AND IN NORMAL FASHION, I STARTED MY CAR, PUT MY FOOT ON THE BRAKE (NOT THE ACCELERATOR) AND SHIFTED INTO REVERSE. IMMEDIATELY, THE CAR ACCELERATED OUT OF CONTROL AT A HIGH RATE OF SPEED AND DIDN'T STOP UNTIL WE WERE INSIDE MY NEIGHBORS HOUSE, STOPPED ONLY BY T
... HE INTERIOR WALL OF HIS HOME. WE WENT BACKWARDS THROUGH HIS FRONT GATE, HIS EXTERIOR WALL AND ENDED UP COMPLETELY INSIDE HIS DEN/GAME ROOM. I WAS NOT ABLE TO STOP IT WITH THE BRAKES AND THERE WAS NO EXPLAINABLE REASON FOR THE MALFUNCTION, BUT IT WAS BIZARRE TO SAY THE LEAST. THERE WAS EXTENSIVE DAMAGE TO HIS HOME AND MY CAR, BUT LUCKILY NO ONE WAS KILLED. MY HUSBAND WAS TRANSPORTED TO THE HOSPITAL FOR NECK INJURIES SUSTAINED IN THE ACCIDENT AND THE CAR IS NOW IN A WRECKING YARD. WE BOUGHT THIS PARTICULAR VEHICLE BECAUSE OF IT'S SAFETY RATING AND WELL DOCUMENTED MAINTENANCE RECORDS, BUT AFTER THIS PROBLEM, I WILL NEVER OWN ANOTHER VOLVO. UPON RESEARCH (AFTER THE ACCIDENT) , I DISCOVERED NUMEROUS COMPLAINTS OF THIS EXACT SCENARIO...ENGAGING IN REVERSE AND UNCONTROLLABLE ACCELERATION OCCURRING. THIS IS A MAJOR SAFETY ISSUE, REGARDLESS OF THE AGE OF A VEHICLE, ESPECIALLY IF IT HAS BEEN WELL MAINTAINED. *KBRead more
Crash
1 injured
Incident date: Oct 5, 2011
2004 FORD FREESTAR LOST ALL ACCELERATION AND STOPPED ON MAJOR ROADWAY. NO PREVIOUS SIGNS OF TROUBLE FROM TRANSMISSION. CLASS ACTION FILED IN US DISTRICT COURT AUGUST 2010 DECLARING FAULTY MANUFACTURING. FORD REFUSING TO REPAIR WITHOUT FULL PAYMENT OF $3200. CURRENT MILEAGE 94,000. HOW MANY MUST GET ROBBED BEFORE THIS IS ADDRESSED? *KB
Incident date: Oct 12, 2011
2002 HONDA ODYSSEY WITH 147,000 MILES ON IT. TRANSMISSION NEEDS TO BE REPLACED. *KB
Incident date: Oct 5, 2011
I AM CURRENTLY THE ORIGINAL OWNER OF A 2005 NISSAN MAXIMA. MUCH TO MY TOTAL SHOCK AND DISMAY, I RECENTLY HAD TO REPLACE THE AUTOMATIC TRANSMISSION AT ONLY 98,700 MILES. SEVERAL WEEKS AGO, THE VEHICLE BEGAN TO SPORADICALLY JERK HARSHLY WHEN ADVANCING TO FIRST GEAR BETWEEN 20-25 MPH. THIS STARTED TO HAPPEN MORE AND MORE FREQUENTLY AND AT TIMES THE VEHICLE WOULD HESITATE RIGHT BEFORE JERKING INTO FI
... RST GEAR AND THEN QUICKLY THRUST FORWARD WITH REVVED UP RPMS. NEEDLESS TO SAY, I FELT EXTREMELY UNSAFE DRIVING THE VEHICLE. I TOOK MY CAR TO THE SERVICE DEPARTMENT OF THE NISSAN DEALERSHIP WHERE I PURCHASED THE VEHICLE. THE SERVICE MANAGER INFORMED ME THAT THIS WAS AN INCREASINGLY COMMON PROBLEM WITH 2004 & 2005 MODEL YEAR MAXIMAS. HE SAID THAT THE ONLY REMEDY WAS TO REPLACE THE TRANSMISSION AT A COST OF APPROXIMATELY $4,000! I TOOK MY CAR TO A TRANSMISSION REPAIR SHOP FOR A SECOND OPINION AND WAS TOLD THE SAME THING. THE MECHANIC CONFIRMED THAT THIS IS A MAJOR ISSUE WITH MAXIMAS MANUFACTURED IN THOSE MODEL YEARS. I ENDED UP TAKING MY CAR BACK TO THE DEALERSHIP AND HAD THEM REPLACE THE TRANSMISSION. I HAVE RESEARCHED THIS ISSUE AND HAVE FOUND THAT THERE ARE NUMEROUS COMPLAINTS ON VARIOUS INTERNET SITES BY OWNERS OF 2004 & 2005 MAXIMAS WHO HAVE EXPERIENCED THE EXACT SAME PROBLEM WITH THEIR TRANSMISSION. IT'S CLEARLY APPARENT THAT THERE IS A MAJOR DEFECT WITH THE TRANSMISSIONS THAT WERE INSTALLED IN 2004 & 2005 MAXIMAS. I HAVE TAKEN VERY GOOD CARE OF MY VEHICLE AND HAVE KEPT UP WITH REGULAR SCHEDULED MAINTENANCE INTERVALS. THERE IS NO WAY THAT I SHOULD HAVE HAD TO REPLACE THE TRANSMISSION AT THAT MILEAGE IF IT WAS NOT DEFECTIVE. I BESEECH YOU TO RECALL ALL 2004 & 2005 MAXIMAS AND FIX THIS DANGEROUS PROBLEM BEFORE IT CAUSES SEVERE ACCIDENTS IF THERE HAVE NOT ALREADY BEEN. *KBRead more
Incident date: Oct 5, 2011
PREMATURE TRANSMISSION FAILURE. PURCHASED USED WITH 85,000 MILES. TRANSMISSION FLUID CHANGED AT SUGGESTED INTERVALS. CAR WILL NOT MOVE IN ANY TRANSMISSION SELECTOR POSITION. AFTER RESEARCH, FOUND THAT THIS IS A COMMON PROBLEM WITH THIS YEAR AND MODEL LEXUS. *KB
Incident date: May 21, 2011
I WAS DRIVING DOWN THE ROAD AND THE VEHICLE DROPPED OUT OF GEAR AND LOSS ACCELERATION. IT WOULD NOT GO BACK INTO GEAR. *KB
Incident date: Oct 2, 2011
TL* THE CONTACT OWNS A 2005 NISSAN MAXIMA. THE CONTACT WAS DRIVING APPROXIMATELY 25 MPH WHEN THERE WAS AN ABNORMAL INCREASE IN ENGINE RPMS AND THE VEHICLE BEGAN TO DECELERATE AND ACCELERATE INDEPENDENTLY. THE FAILURE RECURRED INTERMITTENTLY. THE VEHICLE WAS NOT TAKEN TO THE DEALER FOR DIAGNOSTICS BUT WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 88,000. UPDATED 12/12/11*LJ UPDATED 12
... /13/11Read more
Incident date: Sep 26, 2011
HONDA DEALERSHIP (HOEN HONDA/ POWAY HONDA) KNOWINGLY INSTALLED DEFECTIVE REBUILT TRANSMISSIONS (3 TIMES) ON MY HONDA ODYSSEY 2001. THE TRANSMISSION FAILED ALL THREE TIMES!! THESE TRANSMISSIONS ARE DEFECTIVE AND IT IS NOT A MATTER OF IF IT IS A MATTER OF WHEN THEY FAIL. RECENTLY, MY WIFE WAS STRANDED IN RUSH HOUR TRAFFIC WITH HER ELDERLY PARENTS. LUCKILY, SHE GOT OUT OF CAR AND REDIRECTED TRAFFIC.
... HONDA CHARGED ME $4700 TO REPLACE THEIR DEFECTIVE REBUILT TRANSMISSION. HONDA AND THEIR DEALERSHIPS ARE VERY AWARE OF THE DEFECTIVE TRANSMISSIONS THEY INSTALL AND ARE NOT WILLING TO STAND-BY THEIR PRODUCTS. I WOULD LIKE NHTSA TO KINDLY INVESTIGATE THE SAFETY OF THE THE DEFECTIVE REBUILT TRANSMISSION THAT ARE BEING INSTALLED BY HONDA. *KBRead more
Incident date: Sep 1, 2011
MY 2006 NISSAN XTERRA (PURCHASED NEW IN FEB 2007) BEGAN OCCASIONAL SHUDDERING, AS IF DRIVING OVER RUMBLE STRIPS, WHILE DRIVING AT ABOUT 131,000 MILES. IF I LET OFF THE GAS OR ACCELERATED, IT WOULD STOP, BUT NO CONSTANT TRIGGER. THIS INCREASED OVER A COUPLE WEEKS SO I DECIDED TO RESEARCH ONLINE AND FOUND MANY USERS WITH THE SAME ISSUE. I TOOK IT TO A MECHANIC AND THEY COULDN'T GET IT TO REPLICAT
... E. I LEFT THERE AND DROVE TO TROPHY NISSAN IN MESQUITE AND THEY WOULDN'T LOOK AT IT FOR ANOTHER 1.5 DAYS AND ONLY AFTER I PAID THEM AN $85 DIAGNOSTIC FEE (TO LOOK AT SOMETHING THAT IS THERE FAULT!) I DECIDED TO BE PROACTIVE AND REPLACE THE RADIATOR AND HOSES, HOPING TO CATCH IT EARLY ENOUGH. I TOOK IT TO A MECHANIC 2 DAYS LATER. THEY SAID THE RUMBLING WAS FROM A TORQUE CONVERTER LOCK-UP AND WE COULD DO A FLUSH BUT THAT MAY NOT FIX IT. SO, WE FLUSHED IT WITH 12 QTS NEW NISSAN TRANSMISSION OIL. THE PROBLEM SEEMED TO STAY THE SAME OVER THE NEXT COUPLE WEEKS AND THEN THE TRANSMISSIONS WENT OUT ON MY WAY HOME FROM WORK. SO, NOW WE GET TO REPLACE THE TRANSMISSION. I CALLED A TRANSMISSION SHOP, (AT THIS POINT I DON'T TRUST NISSAN OR ANYTHING THEY SAY - SINCE THEY CAN'T EVEN ADMIT FAULT ON THIS!) AND THEY SAID THIS TRANSMISSION IS AN EXPENSIVE TRANSMISSION (WITH IT'S COMPUTER ETC.) SO JUST TO REBUILD IT IS GOING TO RUN $2500. NISSAN WANTS $4400+ JUST FOR A NEW PART. THIS IS RIDICULOUS. THIS WAS VERY DANGEROUS AS MINE COMPLETELY WENT OUT WHEN I WAS IN THE MIDDLE OF AN INTERSECTION. I AM SO DISGUSTED AT NISSAN AND THEIR LACK OF MORALS / VALUES. IF THEY WOULD JUST DO THE RIGHT THING AND FIX THE ISSUE THAT IS THEIR OWN FAULT, THEN I THINK EVERYONE WOULD FEEL COMPLETELY DIFFERENT. THEY NEED TO STAND BEHIND THE PRODUCT THEY SELL. AS OF RIGHT NOW, I WILL NEVER BUY A NISSAN AGAIN. WHY IS THERE NOT A DEFECT INVESTIGATION WITH AS MANY PEOPLE THAT ARE HAVING THESE ISSUES? *KBRead more
Incident date: Mar 29, 2010
I JUST CAME ACROSS NHTSA ACTION NUMBER : PE11025 AND WANTED TO MAKE YOU AWARE OF THE FOLLOWING: I PARKED MY CAR IN FRONT OF MY DAUGHTER'S DAY CARE CENTER (THE GODDARD SCHOOL, SUWANEE) ON THE MONDAY BEFORE EASTER IN 2010 (MARCH 29, 2010). WHEN I CAME OUT, I DISCOVERED THE CAR APPROXIMATELY 40 YARDS AWAY CRASHED INTO THE EMBANKMENT OF THE NEIGHBORING PARKING LOT, AT AN INCLINE OF APPROXIMATELY 45
... DEGREES. MY CAR WAS DAMAGED, AS WAS THE LANDSCAPING AT THE CRASH SITE, HOWEVER, NO ONE WAS INJURED. IN RESPONSE TO MY INQUIRY, BMW INDICATED THAT THERE WERE NO RECALLS RELATED TO ISSUES SUCH AS THE ONE I EXPERIENCED. THE REPAIR SHOP WAS BAFFLED BY THE ISSUE AS WELL AND SAID IT MIGHT BE ATTRIBUTABLE TO A FAULTY PARKING BRAKE ACTUATOR. THE VEHICLE STILL GIVES OCCASIONAL TRANSMISSION FAULT ERROR MESSAGES AND INDICATORS. I HAD TO FILE AN INSURANCE CLAIM AND CAN CONTACT THE COMPANY FOR DETAILS. I ALSO STILL HAVE PICTURES SOMEWHERE IF SOMEONE WOULD LIKE TO VIEW THEM. THE REPAIRS (MECHANICAL AND BODY WORK) WERE COMPLETED AT GODWIN AUTOMOTIVE IN DULUTH/JOHNS CREEK, GEORGIA. THE MILEAGE STATED ABOVE IS BASED ON MEMORY AND MY NOT BE ACCURATE. *KBRead more
Crash
Incident date: Oct 12, 2011
WHILE DRIVING DOWN THE INTERSTATE IN RUSH HOUR TRAFFIC, MY 2010 FUSION (35,265 MI) LOST ACCELERATION. JERKED CAR INTO THE MEDIAN AND PUT INTO PARK, IT IMMEDIATELY BEGAN IDLING VERY ROUGH AND ALMOST SPUTTERING TO CUT OFF. THE WRENCH LIGHT DISPLAYED. I CUT THE CAR OFF AND LET IT SIT FOR A MOMENT AND THEN CUT THE CAR BACK ON. I PRESSED THE GAS AND THE CARS RPM SHOT UP TO OVER 5000 RPM. IT THEN I
... DLED NORMALLY AND I MERGED BACK IN TRAFFIC JUST HOPING TO GET IT TO MY OFFICE. I MADE IT ANOTHER 2-3 MILES AND IT DID IT AGAIN, THIS TIME BOTH THE ENGINE LIGHT AND WRENCH LIT UP. I IMMEDIATELY CUT IT OFF, RESTARTED IT AND IT SEEMED FINE. I DECIDED TO GET OFF AT THE EXIT I WAS CLOSE TOO AND PARK THE CAR AS I KNEW I WAS GOING TO CAUSE A MAJOR ACCIDENT IF I DID NOT GET IT OFF THE ROAD. I CAME TO THE TOP OF THE EXIT RAMP AND SAT IN TRAFFIC FOR A FEW MINUTES, THE CAR SEEMED OKAY, NO ROUGH IDLE NOTHING STRANGE EXCEPT THE ENGINE LIGHT WAS STILL DISPLAYED. I MERGED INTO TRAFFIC OFF THE RAMP AND IN THE MIDDLE OF THE ROAD SAME THING OCCURRED, NO ACCELERATION, I HAD MY FOOT TO THE FLOOR. I GOT IT INTO A PARKING LOT AND CALLED THE DEALERSHIP. I HAD THE CAR TOWED IN GOT A LOANER TO DRIVE INTO WORK. THE FORD DEALERSHIP CALLED ABOUT AN HOUR LATER AND SAID THE CAR IS FIXED AND I CAN COME GET IT. THEY SAID THEIR WAS AN ISSUE IN MY ELECTRONIC THROTTLE BODY AND THEY HAVE REPLACED THE THROTTLE BODY. I LOVE THIS CAR BUT AT 35,000 MILES I SHOULD NOT HAVE ALREADY HAD A BAD BATTERY AND NOW THIS ISSUE. I AM STARTING TO NOT TRUST THE CAR. I HOPE THE ISSUE IS FIXED, BUT I AM ALMOST SCARED TO GO PICK IT UP TONIGHT. I HAD NO IDEA OF THESE ISSUES UNTIL I LOOKED IT UP ONLINE AFTER THE THIS MORNING. *KBRead more
Incident date: Oct 9, 2009
FUEL GAUGE NOT WORKING,RADIATOR FLUID LEAKING INTO TRANSMISSION DAMAGING TRANSMISSION,FRONT PASSENGER SEATBELT GETTING STUCK. *KB
Incident date: Jul 21, 2011
NEVER HAD ANY PROBLEMS WITH TRANSMISSION IN THE PAST. I WAS DRIVING ON THE HIGHWAY AT 70 MPH WHEN, WITHOUT ANY WARNING, THE TRANSMISSION FAILED. THE CAR WAS UNDRIVABLE AND BEGAN TO OVERHEAT. THERE WAS TRANSMISSION FLUID ALL OVER. HAD THE VEHICLE TOWED AND HAD TRANSMISSION REBUILT FOR $1500. SINCE THE REBUILD, THE TRANSMISSION HAS FAILED 3 ADDITIONAL TIMES. *KB
Incident date: Aug 15, 2010
TL* THE CONTACT OWNS A 2003 VOLKSWAGEN JETTA WAGON. THE CONTACT STATED THAT THE SPEEDOMETER FAILED TO PROVIDE AN ACCURATE SPEED TRAVELED. THE CONTACT ALSO STATED THAT WHEN THE CRUISE CONTROL SWITCH WAS ACTIVATED, IT WOULD CAUSE THE VEHICLE TO SURGE FORWARD ABNORMALLY. THE VEHICLE WAS TAKEN TO THE DEALER WHERE THEY CONFIRMED THAT THE SENSOR IN THE TRANSMISSION NEEDED TO BE REPLACED. THE MANUFACTURE
... R WAS NOT CONTACTED AND THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 170,000 AND THE CURRENT MILEAGE WAS 211,000. UPDATED 12/14/11 THE CONSUMER STATED THE TRANSMISSION WAS EXHIBITING AN INTERMITTENT HESITATION. UPDATED 12/20/11. *JBRead more
Incident date: Sep 1, 2011
#1. VEHICLE ACCELERATES WHEN LETTING OFF GAS, EVEN WHILE GOING UPHILL THE VEHICLE WILL ACCELERATE. YOU CAN GO UP A STEEP HILL WITHOUT TOUCHING THE GAS. BROUGHT THE VEHICLE TO THE DEALERSHIP THEY REPLACED, THE THROTTLE BODY, GAS PEDAL ASSEMBLY. THEY REINSTALLED THE ORIGINAL PARTS AND TOLD US THAT THIS WAS NORMAL. WE DROVE OTHER 2011 CHEVY SILVERADO'S WHICH DID NOT DO THE SAME THING. THE DEALERSHIP
... TOLD US THAT ALL THE 2011 CHEVY SILVERADO'S ACCELERATE ON THEIR OWN. #2. THERE IS A CLUNKING NOISE FROM THE REAR WHEN DRIVING OVER BUMPS. THE DEALERSHIP SAID THIS IS NORMAL BACKLASH, AND DID NOT DO ANYTHING. *KBRead more
Incident date: May 11, 2011
I HAVE HAD NUMEROUS INSTANCES WHERE, WHEN EITHER AT A STOP LIGHT, OR PARKING OR WAITING IN THE CARPOOL LINE MY FREESTYLE HAS LUNGED FORWARD WHILE MY FOOT WAS ON THE BRAKE PEDAL. SOME INSTANCES ARE WORSE THAN OTHERS WITH MORE FORCE, BUT I AM ABLE TO STOP THE CAR BY PRESSING HARDER ON THE BRAKE PEDAL. I HAVE ALMOST HIT A COUPLE OF CARS IN THE DRIVE THRU LANES AT RESTAURANTS. I HAVE ALSO EXPERIENC
... ED MY FREESTYLE CUTTING OFF WHILE AT A LIGHT, AND EVEN ONCE WHEN I TOOK MY FOOT OFF THE GAS TO COAST INTO A PARKING LOT. THE CAR JUST DIED. I CALLED THE LOCAL FORD DEALERSHIP AND THEY STATED THAT THERE HAVE BEEN ISSUES WITH THE THROTTLE BODY STICKING AND ITS WAY OF CORRECTING ITSELF IS TO LUNGE THE CAR AND ATTEMPT TO RIGHT THE ISSUE. THEY QUOTED ANYWHERE FROM $100 TO TRY TO CLEAN THE THROTTLE BODY AND POSSIBLE HAVE TO REPLACE IT TO THE TUNE OF ABOUT $700. IF THIS PROBLEM IS SO WELL KNOWN THAT MY DEALER KNOWS ABOUT IT, WHY HAS IT NOT BEEN ADDRESSED AND RECALLED? *KBRead more
Incident date: Aug 24, 2011
WE BOUGHT THIS VEHICLE (LEXUS RX300 4WD) ON 11/29/2002 WITH 27,080 MILES ON IT FROM LOCAL LEXUS DEALER. IT IS MY WIFE'S PRIMARY VEHICLE AND SHE DRIVES IT TO WORK DAILY (ABOUT 20 MILES PER DAY). AT 111,000 MILES THE CHECK ENGINE LIGHT CAME ON AND THE TRANSMISSION WAS SHIFTING ERRATICALLY IE. DOWN SHIFTING SUDDENLY WHEN IT SHOULDN'T AND SLIPPING GEARS. IT ALSO MAKES A STRANGE CONSTANT NOISE. IT HAD
... BEEN MORE AND MORE SHIFTING THIS WAY OFF AND ON FOR 2 OR 3 MONTHS. I TOOK IT TO LEXUS DEALER ON 8/24/2011 BECAUSE OF CHECK ENGINE LIGHT AND THE SERVICE CONSULTANT STATED IT NEEDS NEW TRANSMISSION (THIS WAS SAID IN THE SAME TONE OF "YOU NEED A NEW AIR FILTER") AND THEY WOULD REPLACE IT FOR $5,208.80. WHEN I ASKED SERVICE CONSULTANT IF THIS WAS A VERY COMMON PROBLEM HE STATED THAT IT WAS NOT. HE SAID MY TRANSMISSION COULD TOTALLY FAIL AT ANY TIME EVEN WHILE DRIVING. THIS IS A DEFINITE SAFETY ISSUE. THE OPERATORS MANUAL STATES "IT IS NECESSARY TO CHANGE TRANSMISSION FLUID ONLY IF YOUR VEHICLE IS DRIVEN UNDER SPECIAL OPERATING CONDITIONS" WHICH WE DON'T. I CHECKED EDMUNDS AND BLOGS ON LINE AND THERE ARE HUNDREDS OF COMPLAINTS OVER THIS ISSUE AND I THINK IT NEEDS TO BE INVESTIGATED BECAUSE I DON'T WANT MY WIFE TO GET IN AN ACCIDENT ON THE INTERSTATE AND SO IT JUST SETS IN MY GARAGE. *KBRead more
Incident date: Oct 10, 2011
TL* THE CONTACT OWNS A 2005 NISSAN MAXIMA. THE CONTACT STATED THAT AFTER SHIFTING GEARS WHILE DRIVING 25 MPH, THE VEHICLE WOULD JERK VIOLENTLY AND SUDDENLY ACCELERATED. THE VEHICLE WAS NOT TAKEN TO THE DEALER. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE AND THE CURRENT MILEAGE WAS 102,000. *KB
Incident date: Jul 9, 2011
THE FIRST TIME THE PROBLEM OCCURRED, I WAS WAITING IN A LINE TO EXIT A PARKING LOT SO I WAS IDLING WHEN THE CAR SURGED FORWARD. I SLAMMED ON THE BRAKES AND THE CAR STALLED OUT. I WAS ABLE TO RE-START BUT THEN IT WOULD SURGE AGAIN. I PUT THE CAR IN NEUTRAL AND WAS ABLE TO MAKE IT OUT. THE CAR CHUGGED A BIT BUT WHEN I GOT GOING IT WORKED FINE. A FEW DAYS LATER, WHEN IDLING, THE CAR WOULD EITHER
... CHUG AND STALL OR SURGE. THE PROBLEM WAS PARTICULARLY BAD ONE DAY AND HAD BEEN DOING IT A FEW TIMES. WE THEN WERE ENTERING THE HIGHWAY AND IT WAS LIKE THE CAR WASN'T GETTING ANY GAS, IT TOOK AWHILE TO GET THE CAR OVER 25 MPH. WE TOOK IT TO THE FORD DEALERSHIP AND THEY SAID THEY WEREN'T SURE WHAT THEY PROBLEM WAS BUT THE READOUT SAID IT WAS THE THROTTLE BODY BUT THEY WEREN'T FAMILIAR WITH ANYONE ELSE HAVING THE PROBLEM. IT SEEMS THE PROBLEM OCCURS WHEN IT IS VERY HOT AND THE AIR CONDITIONING IS RUNNING. *KBRead more
Incident date: Aug 18, 2011
WHILE DRIVING IN FIRST GEAR ON LIGHT THROTTLE, THE TRANSMISSION SHIFTED FROM 1ST GEAR INTO 2ND GEAR VIOLENTLY. NEARLY EVERY TIME UNDER LIGHT THROTTLE (UNDER NORMAL ENGINE OPERATING TEMPERATURE) SINCE THE FIRST OCCURRENCE, THE TRANSMISSION EITHER UPSHIFTS (1ST TO 2ND GEAR) OR DOWNSHIFTS (3RD TO 2ND GEAR) VIOLENTLY. *KB
Incident date: Oct 11, 2011
I BOUGHT MY USED TOURING MODEL SEBRING IN MAY OF 2011, AND SINCE THEN IT HAS REPEATEDLY JUMPED OR LEAPED FORWARD WHEN COMING TO A STOP OR IDLING, EVEN WITH MY FOOT ON THE BRAKE. I HAVE ALMOST CAUSED A FEW ACCIDENTS BY RAMMING THE CAR IN FRONT OF ME AT A STOP LIGHT AND SUCH. AS WELL, IT STALLED OUT ON ME WHEN I MADE A COMPLETE STOP ON 10/11/11. I HAVE SEEN MANY, MANY OF THE SAME COMPLAINTS AND WISH
... I KNEW WHAT THE ISSUE WAS. WILL BE TAKING IT INTO THE REPAIR SHOP TOMORROW. *KBRead more
Incident date: Aug 18, 2010
I'M NOT SURE IF THIS IS A POWER TRAIN OR OTHER PROBLEM, CAR LURCHES DANGEROUSLY AT LOW SPEEDS, AND WHEN CHANGING GEAR INTO AND OUT OF REVERSE. I HIT A POST PARKING IN AUGUST OF 2010 DUE TO THIS, AND IT'S BEEN GETTING GRADUALLY WORSE. TOOK IT TO THE DEALER WHO REPLACED A BROKEN UPPER MOTOR MOUNT THAT WAS CONNECTED TO THE TRANSMISSION. DIDN'T HELP, ALTHOUGH IT SEEMED LIKE A GOOD GUESS AT THE TIME
... . IT HELPS TO KEEP FOOT FIRMLY ON BRAKE WHEN CHANGING GEAR OR HOLDING STILL, WHILE THE CAR TRIES TO LURCH FORWARD (OR BACK) WITH UNPLANNED ACCELERATION. SEEMS TO BE GETTING INCREASINGLY WORSE AND NOW I DON'T FEEL IT'S SAFE TO LET ANYONE ELSE DRIVE IT, LIKE AT VALET PARKING. TAKING IT BACK TO DEALER TOMORROW, BUT WE LET WARRANTY EXPIRE RECENTLY DARN IT. WE GET SO MANY FAKE SPAM WARRANTY-EXPIRING PHONE CALLS THAT I GOT CONFUSED AND DROPPED THE BALL. THROTTLE CONTROL MODULE MAY BE GIVING FALSE SIGNAL TO CARBURETOR, NOT SURE WHAT IT IS. *KBRead more
Crash
Incident date: Oct 11, 2011
I HAVE BEEN AT THE DEALERS REPAIR SHOP LIKE 10+ TIMES FOR THE SAME TRANSMISSION PROBLEM. TODAY I WAS OUT ON A QUICK TRIP TO THE STORE AND WHEN I CHANGED GEARS FROM REVERSE (TO GET OUT OF MY DRIVE WAY) THEN TO DRIVE THE GEAR SHIFTER BECAME HARD TO MOVE? AND THEN THE "HOLD" LIGHT CAME ON. AFTER THAT MY CAR WENT ON AND OFF ACCELERATION DRAGGING, THEN ON MY WAY OUT OF THE PARKING LOT OF THE STORE, I P
... USHED TO ACCELERATE AND THEN MY CAR BARELY MOVED LIKE SLOWER THAN THE CARS REGULAR CRUISE (LIKE WHEN YOU LET THE CAR MOVE ON ITS OWN IN MOTION OFF THE ACCELERATOR) IT WENT SLOWER THAN THAT. I AM ABOUT UP TO MY SHOULDERS IN FRUSTRATION WITH IT, NOW THE HOLD LIGHT WONT COME OFF AND I ALMOST GOT IN A CAR ACCIDENT NOW IT FEELS UNSAFE TO DRIVE. *KBRead more
Incident date: Oct 11, 2011
CVT TRANSMISSION FAILED FOR THE SECOND TIME WHILE DRIVING. VEHICLE LURCHED AND THE WRENCH LIGHT CAME ON, FRONT END SHUDDERED. RESTARTED THE VEHICLE AND IT WOULD DRIVE, BUT WOULD ONLY ACHIEVE 20 MPH WITH VERY HIGH RPMS. DEALER SAYS TRANSMISSION WILL HAVE TO BE REPLACED. AS I UNDERSTAND READING THE NUMEROUS COMPLAINTS, THEY DON'T MAKE THIS UNIT ANYMORE. I AM FACED WITH A VEHICLE THAT I CAN'T DRIVE.
... PLEASE DO SOMETHING. *KBRead more
Incident date: Oct 7, 2011
I HAVE BEEN GETTING SERVICE ENGINE SOON LIGHT ON THE DASHBOARD. THEN SHORTLY AFTER MY BATTERY NEEDED TO BE REPLACED AND I THOUGHT THAT WAS THE PROBLEM. WELL THE NEXT WEEKEND THE LIGHT CAME ON AND NOW WHEN I SWITCH GEARS I GET A LOUD THUMP AND THE CAR JUMPS REALLY HARD. I WENT TO ADVANCED AUTO PARTS WITH THE SERVICE ENGINE LIGHT STILL ON THEY WERE ABLE TO RETRIEVE CODES AND VERIFY THE TRANSMISSION
... RANGE SENSOR A CIRCUIT WHILE IN PARK/REVERSE/NUETRAL AND DRIVE. AND THEY ALSO RETRIEVED THE TRANSMISSION CONTROL SENSOR. I AM SCARED TO DRIVE MY CAR NOW AND I WILL NOT DRIVE IT TILL IT GETS FIXED. I HAVE HAD TRANSMISSION PROBLEMS FOR THE LONGEST TIME AND I AM SCARED THIS CAR WILL CAUSE AN ACCIDENT. IT IS A VERY UNSAFE CAR AND I AM CONCERNED ABOUT THE PROBLEM WITH THE AIRBAG NOT DEPLOYING DUE TO MANY COMPLAINTS. YOU NEED TO DO A RECALL ON THIS CAR BEFORE SOMEONE GETS BADLY INJURED OR KILLED. *KBRead more
Incident date: Jun 8, 2010
VEHICLE SURGES AT LOW SPEEDS. THE PROBLEM IS WORSE WITH THE AIR CONDITIONING ON. *KB
Incident date: Sep 26, 2011
I WAS DRIVING ON A MAJOR HIGHWAY WITH MY CHILDREN AND ALL OF A SUDDEN MY CAR'S TRANSMISSION LIGHT CAME ON, MY CAR STARTED BUCKING, AND SOON LOST POWER AND I WAS FORCED TO PUT MY CAR IN PARK IN HEAVY TRAFFIC AND RESTART IT. *KB
Incident date: Jul 5, 2011
THE VEHICLE WOULD AT DIFFERENT TIMES, HAVE TROUBLE SHIFTING FROM PARK TO REVERSE, IN DRIVE, ETC. IT SOUNDED LIKE THE TRANSMISSION WAS BROKEN. THIS PROBLEM WOULD ARISE, AND THEN GO AWAY. THE FIRST TIME THE DEALERSHIP RESET THE COMPUTER, AND IT RAN FINE FOR WEEKS, THEN THE PROBLEM CAME ABOUT AGAIN, AND WENT AWAY, THE LAST TIME AROUND SEPT 18TH, IT WAS WORSE, SO I HAD IT TOWED AND REPAIRED. THE DEAL
... ERSHIP REPLACED THE OUTPUT SHAFT SENSOR AND TURBIN SHAFT SENSOR AT A COST OF $700. I WAS IMPELLED TO REPORT A CONCERN, AFTER SEEING OTHER CONCERNS ON LINE FOR THE SAME ISSUES, AND A CUSTOMER OF MINE WHO HAS AN EDGE IS EXPERIENCING THE SAME ISSUES. FORD MOTOR COMPANY, AND THE DEALERSHIPS DO NOT SEEM TO WANT TO SERIOUSLY ADDRESS THIS ISSUE, AND I FELT LIKE THEY WERE TRYING TO AVOID ADMITTING TO A MAJOR PROBLEM. *KBRead more
Incident date: Oct 4, 2011
MY TRANSMISSION IS BADLY JERKING AND SCARED TO DRIVE. GEAR SHIFTTING IS NOT PROPERLY OPERATING. *KB
Incident date: Oct 6, 2011
WHILE DRIVING ON THE HIGHWAY, TRANSMISSION SLIPPAGE OCCURRED SWITCHING SUDDENLY FROM DRIVINIG TO NEUTRAL, GEAR COULD NOT BE CHANGED UNLESS VEHICLE WAS PARKED AND BRAKE PEDAL WAS PRESSED DOWN. SCARY SITUATION CONSIDERING THAT I COULD BE DRIVING ON THE LEFT LANE. PLEASE CONSIDER THIS AS A SAFETY COMPLAINT AND REQUEST FOR SAFETY RECALL. *KB
Incident date: Sep 24, 2011
OVER THE PAST FEW WEEKS WHILE DRIVING THE VEHICLE WILL FLASH A WARNING SAYING SERVICE PARK ASSIST SYSTEM. WHEN THIS HAPPENS THE GEAR DISPLAY ON THE DASH PRND WILL ALL 4 GET CIRCLED AND FLASH AND THEN AS YOU ARE ACCELERATING YOU CAN FEEL THE VEHICLE LOSE SPEED. YOU CAN NO LONGER ACCELERATE THE VEHICLE AND HAVE TO COAST OFF THE ROAD. ONCE YOU STOP AND SHIFT TO PARK THEN BACK TO DRIVE IT WILL RESE
... T AND THEN ALLOW YOU TO ACCELERATE. I WAS GOING 65 ON THE FREEWAY WHEN THIS HAPPENED LAST AND THIS IS A MAJOR SAFETY ISSUE. FOR ABOUT THE PAST 30,000-40,000 K MILES WE HAVE HAD ISSUES WITH IT SHIFTING PROPERLY AND EVERY TIME WE TOOK IT TO THE DEALER THEY CAN NEVER RE CREATE THE ISSUE. NOW WE ARE RECEIVING THIS WARNING AND IT ACTUALLY STOPS ACCELERATING ON ITS OWN. IT IS HAPPENING MORE AND MORE. WE TOOK IT TO THE DEALER SINCE THIS WARNING NOW CAME ON AND THEY SAID THEY HAVE NEVER HEARD OF IT, THEY COULDN'T RE CREATE IT, THAT IT HAS NOTHING TO DO WITH THE SHIFTING AND TO TURN OFF OUR PARK ASSIST SYSTEM SO IT DOESN'T HAPPEN. WE ARE ATTEMPTING A DIFFERENT DEALER TODAY BUT FIRST THING THEY SAID IS THEY NEVER HEAR OF THIS EITHER. SO COMFORTING! *KBRead more