Showing 40,517 complaints — component: ENGINE AND ENGINE COOLING
Incident date: Mar 30, 2026
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Incident date: Mar 19, 2026
See attached document for complaint.
Incident date: Apr 4, 2026
See attached document for complaint.
Incident date: May 6, 2026
The contact owns a 2015 Hyundai Sonata. The contact stated while driving at various speeds, the vehicle skipped and failed to exceed 35 MPH. The contact received notification of Hyundai Service Campaign Number: 9C2 (ECU SOFTWARE UPDATE FOR THETA II EMISSIONS IMPROVEMENT), and the vehicle was towed to the dealer, where it was diagnosed and determined that the catalytic converter was clogged and nee
... ded to be replaced at the owner's expense. The vehicle was not yet repaired. The contact's son, who was an independent mechanic, determined that the ECU might have sent erroneous signals to the O2 sensors, who then sent excessive fuel into the catalytic converter, causing a catalytic converter clog. The manufacturer was notified of the failure and was informed of the Service Campaign notification, but the manufacturer denied assistance due to the mileage and lack of warranty coverage. The failure mileage was approximately 140,000.Read more
Incident date: May 14, 2026
The contact owns a 2019 GMC Sierra LD 1500. The contact stated that while driving approximately 65 mph, the vehicle, went into low power mode, and was able to move safely to a and then the vehicle stalled. The vehicle was towed to an independent mechanic and was diagnosed as the engine has no compression, suspect a possible crankshaft failure, also a possible engine replacement. The manufact
... urer was notified of of the failure. The contact associated the failure with NHTSA Campaign Number 25V274000 (Engine and Engine Cooling). The approximate failure mileage was 130,000.Read more
Incident date: May 2, 2026
The contact owns a 2018 Honda Accord. The contact stated that while driving the vehicle she noticed a power issue with the vehicle, thinking it had to do with the battery, the vehicle was misfiring. The vehicle was towed three times to the dealer, where it was diagnosed with a engine failure. The second tow was to a independent mechanic, and the third time the vehicle was taken to a dealer where
... it was diagnosed to have a engine gasket failure. The contact was informed that there was a coolant intrusion in cylinder #2. The contact was informed that the head gasket needed to be replaced. The vehicle was repaired. The vehicle was not repaired. The manufacturer was not made aware of the failure. The failure mileage was 73,000.Read more
Incident date: Oct 1, 2025
The contact owns a2019 Nissan Kicks. The contact stated that while operating the vehicle the engine had stall while the RPMs had dropped below 2000. Also, the ABS and Traction Control warning lights had illuminated. The vehicle was taken to the local mechanic who informed of a service code related to the Mass Air Flow was identified and the air filter and battery was replaced, but the failure con
... tinued. The manufacturer and local dealer were not yet contacted. The failure mileage was 70,000.Read more
Incident date: Oct 23, 2025
The contact owns a 2020 Ram Promaster. The contact received notification of NHTSA Campaign Number: 25V720000 (Engine And Engine Cooling) however, the part to do the recall repair was not yet available. The local dealer was contacted. The contact stated that the manufacturer had exceeded a reasonable amount of time for the recall repair. The manufacturer was made aware of the issue. The contact had
... not experienced a failure.Read more
Incident date: Mar 1, 2026
The contact owns a 2021 GMC Yukon. The contact stated that the vehicle had a rough idle. There was an abnormal ticking and rattling sound detected. The vehicle lost oil pressure. The contact located smoke emerging from the vehicle. The engine light was illuminated. The vehicle was taken to the local dealer, where it was diagnosed with a failure with cylinder five, no compression, and bearing failu
... re. The dealer suggested the engine be replaced. The vehicle was not repaired. The contact indicated that the failure was related to NHTSA Campaign Number: 25V274000 (Engine and Engine Cooling) but was not included in the recall. The manufacturer was contacted who referred to the NHTSA hotline. The failure mileage was unknown.Read more
Incident date: May 7, 2026
The contact owns a 2023 Lexus LX 600. The contact stated that the rearview back up camera image displayed a distorted image. Another issue, the vehicle intermittently stalled when at a complete stop and going to accelerate. The vehicle was contacted; however, the vehicle was not diagnosed or repaired. The manufacturer was not notified of the issue. The approximate failure mileage was 41,000.
Incident date: May 26, 2026
The contact owns a 2024 Toyota Tundra. The contact received notification of NHTSA Campaign Number: 25V322000 (Exterior Lighting) and 25V767000 (Engine and Engine Cooling) however, the part to do the recall repair was not yet available. The dealer was not contacted. The vehicle was not diagnosed or repaired. The manufacturer was not made aware of the issue. The contact stated that the manufacturer
... had exceeded a reasonable amount of time for the recall repair. The contact had not experienced a failure.Read more
Incident date: May 23, 2026
The contact owns a 2018 Ford Escape. The contact stated that while driving the vehicle misfiring, white some, hesitation. The engine light illuminated. antifreeze leaking into the cylinder. The vehicle was taken to an independent mechanic where the diagnostic code P0300 was read and an antifreeze leak into the cylinder and a design flaw in the Eco boost. The manufacturer was not notified of t
... he issue. The approximate mileage was unavailable.Read more
Incident date: Jan 15, 2026
The contact's wife owns a 2018 Ford Escape. The contact stated that while driving at various speeds, water would intrude into the engine compartment and the vehicle would independently shift into Limp Mode. The check engine warning light illuminated. The vehicle was taken to a local independent mechanic, where the ignition coils and spark plugs were replaced at the consumer's expense; however, the
... failure reoccurred. The vehicle was taken to a local dealer, where it was diagnosed with water intrusion into the engine. The vehicle was not repaired due to the costs. Upon further investigation, the contact related the failure to Ford's Customer Satisfaction Program: 21N12; however, the VIN was not included. The manufacturer was made aware of the failure. The failure mileage was approximately 75,000.Read more
Incident date: May 8, 2026
The contact owns a 2017 Mazda CX-5. While driving the vehicle, the engine overheat warning suddenly illuminated on the dashboard cluster panel. The contact pulled over immediately, restarted the engine, and coasted the vehicle to a local, independent mechanic shop. The independent mechanic diagnosed the issue as a blown head gasket. For a secondary inspection, the vehicle was transported to an aut
... horized Mazda dealership. Dealership technicians determined that the engine cylinder was actually cracked and recommended a full engine replacement. The vehicle was not repaired. The manufacturer was notified of the failure. The failure mileage was 92,000.Read more
Incident date: May 1, 2026
The contact stated that while driving the vehicle began to unexpectedly slow and then stalled. The vehicle was unable to restart. No warning lights illuminated. The vehicle was taken to the dealer where it was not diagnosed or repaired. The manufacturer was notified of the issue. The approximate failure mileage 215,000.
Incident date: Apr 1, 2022
The contact owns a 2021 Chevrolet Silverado. The contact stated that while driving at various speeds, a flashing check engine warning light appeared on the instrument panel. The vehicle was taken to a dealer where the received fault code PO300 which was a general code for a misfire in the engine. The contact brought the vehicle back to the dealer multiple times due to various fault codes; however,
... the contact was given the same information. The contact then received a "Low Oil, Check Oil", the contact checked the oil and discovered no oil on the engine's dipstick. Due to the failure, the vehicle was towed back to the dealer where they began an oil consumption test. The valves collapsed and the dealer replaced the valve in cylinders 1,3,5, and 7 as well as the spark plugs. Despite the repair, the contact stated that the failure returned almost two months later. The contact continued the oil consumption test and stated that the vehicle was losing 3 quarts of oil each oil change. The manufacturer had been notified of the failure on multiple occasions and had made multiple vehicle buyback requested; the manufacturer denied each buyback request. After his latest phone call with the manufacturer, he was referred to the NHTSA Hotline to file a complaint. The vehicle was not repaired. The failure mileage was 12,000.Read more
Incident date: Oct 1, 2025
The contact owns a 2016 Kia Optima. The contact stated that while operating the vehicle a knocking and rattling noise coming from the engine and the check engine light had remained illuminated. The vehicle was towed to the local dealer who informed that the engine had failed and needed to be replaced. The vehicle was not yet repaired. The manufacturer was notified of the failure but no assistance
... was offered. The failure mileage was 150,000.Read more
Incident date: Apr 26, 2026
The contact owns a 2019 HYUNDAI Kona. The contact stated while driving the vehicle at an undisclosed speed, he noticed he had an engine knock, and noticed that the engine was consuming a good amount of oil with no warning lights or oil leaks. The contact pulled over to the side when the knock started and noticed the vehicle was starving of oil although a recent oil change shows it was recent. The
... vehicle was taken to a dealer where it was diagnosed to have poor service, and engine sludge although dealer stated there was none. The vehicle was not repaired. The manufacturer was notified of the failure. The failure mileage was 120,132.Read more
Incident date: May 13, 2026
The contact owns a 2021 Kia Seltos. The contact stated while driving at an undisclosed speed, the contact noticed an unusual knocking sound and the engine seized. In addition, several warning lights were illuminated. The contact stated that while attempting to start the vehicle, the vehicle started. The contact inspected the vehicle and noticed that the oil was three quarts low. The contact stated
... that the vehicle was scheduled for a service appointment for an oil change the following week. The vehicle was not diagnosed or repaired by an independent mechanic or dealer. The contact referenced an unknown recall; however, the VIN was not associated with a recall related to the failure. The manufacturer was not made aware of the failure. The failure mileage was approximately 60,000.Read more
Incident date: Apr 20, 2026
The contact owns a 2013 Hyundai Santa Fe Sport. The contact stated that occasionally, while driving at various speeds, an abnormal knocking sound was heard coming from under the hood while the accelerator pedal was depressed, and the steering wheel would shudder. The Check engine oil warning light illuminated. Upon further investigation, the contact related the failure to NHSTA Campaign: 17V226000
... (Engine and Engine Cooling). The vehicle was taken to a local dealer, where it remains for further investigation; however, the vehicle was not diagnosed or repaired due to a lack of maintenance records, and the recall repairs were rejected. The manufacturer was made aware of the failure and determined that the recall repairs were performed under previous ownership; however, the recall repairs were not completed. The failure mileage was approximately 147,000.Read more
Incident date: May 17, 2026
The contact owns a 2022 Nissan Rogue. The contact received notification of NHTSA Campaign Number: 25V437000(Engine and Engine Cooling). The vehicle was taken to the dealer where the contact was informed that the dealer reprogrammed the engine control module (ECM) software and test drove the vehicle and found no failures. Despite the dealer's claims that they test drove the vehicle, the contact sta
... ted that her mileage had not changed upon picking up the vehicle. The contact then stated that while driving at 55 MPH, an audible ding sound emitted from the vehicle as both an "Engine Malfunction" and "Power Reduced Service Now" warning messages appeared on the instrument panel. The vehicle began to slow down upon depression of the accelerator pedal. While at a stop light, the vehicle failed to accelerate above 5 MPH as the contact coasted the vehicle into a parking lot. Due to the failure, the vehicle was towed to another dealer where after the dealer spoke with the manufacturer; they agreed to repair the vehicle under the initial recall. The contact had yet to notify the manufacturer directly about the failure. The vehicle had yet to be repaired and remained in the possession of the dealer. The failure mileage was approximately 35,000Read more
Incident date: Mar 28, 2026
The contact owns a 2020 Ford Ecosport. The contact stated while starting the vehicle up she noticed that it hesitate was turning on and noticed the oil pressure warning light illuminated, and stated while accelerating the vehicle starts to shake and would not go above 30 MPH, and while trying to stop at a red light the vehicle struggles to brake although the brakes are applied, after coming to a f
... ull stop the vehicle shutdowns and would have restart. The vehicle was taken to a dealer, where it was diagnosed to have a broken intake camshaft and bank 1, causing the engine block to be repaired. The contact referenced NHTSA Campaign Number: (23V905000 (ENGINE AND ENGINE COOLING) however, the dealer would not repair the recall due to the extensive issues caused by the pending recall. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was 57,000.Read more
Incident date: May 20, 2026
The contact owns a 2023 RAM Promaster 2500. The contact received a recall notification, NHTSA Campaign Number: 25V720000 (Engine and Engine Cooling) however the parts were unavailable. The contact, who was a business owner, stated that he did not want his vehicle to break down while on the road. The contact stated that the recall was initiated over six months ago. The dealer was contacted, the con
... tact was informed that the parts were unavailable. The manufacturer was not contacted. The contact's vehicle had not experienced any failure regarding the unrepaired recall.Read more
Incident date: Mar 1, 2026
The contact owns a 2018 Ford Escape. The contact stated that after driving her vehicle, she notices that her coolant levels drain very quickly, causing her to fill up after every trip, and stated her vehicle was overheating at times. The vehicle was taken to a independent mechanic where it was diagnosed to have coolant leaking into cylinder two, needing a new engine replacement. The vehicle was no
... t repaired. The manufacturer was not notified of the failure. The failure mileage was 119,000.Read more
Incident date: May 14, 2026
The contact owns a 2015 Ford Escape SE. The contact stated that while idle at a stop light with the left-turn signal on, the vehicle started to jerk, and loud noises were coming from the front end of the vehicle. The Check Engine light illuminated, and the vehicle failed to move. The Fire Department arrived and assisted the contact with pushing the vehicle to the side of the road. The vehicle was
... towed to a certified mechanic at Precision Auto Shop, who diagnosed that the coolant was leaking. After further inspection, the dealer also diagnosed that the transmission had failed and needed to be replaced. The vehicle was not repaired. The manufacturer was informed of the failure, and a claim was filed. The failure mileage was approximately 111,400.Read more
Incident date: May 3, 2026
The contact owns a 2021 Audi Q7. The contact stated that while driving approximately 50 - 55 MPH, the Check Engine light had illuminated. The vehicle was taken to the dealer, who diagnosed code PO299, which referred to coolant migration into the vacuum system. The contact was unable to provide the exact parts that were needed for repairs. The vehicle was not repaired. The manufacturer was informed
... of the failure. The manufacturer opened a case regarding the issue. The failure mileage was approximately 60,000.Read more
Incident date: May 14, 2026
The contact owns a 2016 RAM 1500. The contact stated while the contact's husband was driving at 75 MPH, the engine seized. In addition, several warning lights illuminated. The contact stated that the vehicle was seized in the middle of a busy highway. The contact stated while attempting to start the vehicle, the vehicle failed to start. The vehicle was towed to the dealer where it was diagnosed wi
... th a delaminated tone wheel. The contact was informed that the tone wheel needed to be replaced. The vehicle was not repaired. The contact received a recall notification, NHTSA Campaign Number: 23V411000 (Engine and Engine Cooling). The contact was informed that the repair was not covered under the recall. The manufacturer was made aware of the failure but provided no assistance. The failure mileage was approximately 125,000.Read more
Incident date: Sep 1, 2025
The contact owns a 2016 Kia Soul. The contact stated that while driving at an undisclosed speed, the engine oil warning light illuminated. The contact pulled over and inspected the vehicle. The contact discovered that there was no oil in the engine; however, the vehicle previously had an oil change. The contact added oil to the engine. The failure persisted. Additionally, the vehicle made rattling
... sounds and emitted a burning oil odor. The brake pedal had to be firmly depressed to stop the vehicle, the windows inadvertently rolled down, and the interior lights intermittently failed due to an electrical system failure. The vehicle was taken to the dealer, who determined that the timing cover needed to be resealed and the brake master cylinder, oil pan gasket, brake fluid, spark plugs, ABS, and window master switch needed to be replaced. The vehicle was not repaired. The contact related the failure to NHTSA Campaign Number: 19V120000 (Engine, Engine And Engine Cooling); however, the VIN was not included in the recall. The manufacturer was made aware of the failure. The failure mileage was approximately 80,000.Read more
Incident date: May 16, 2026
The contact owns a 2021 Kia Soul. The contact stated that upon starting the vehicle, the oil pressure sensor light was illuminated. The vehicle was making an abnormal knocking sound. The contact had to add additional oil. The vehicle was taken to an independent mechanic who informed the vehicle was related to the recall. The vehicle was towed to the local dealer, where it was diagnosed that the ca
... mshaft and timing needed to be replaced. The vehicle was not repaired. The contact stated that the vehicle was taken previously to the local dealer for NHTSA Campaign Number: 25V099000 (Engine and Engine Cooling). The manufacturer was contacted, who confirmed there was no warranty coverage. The failure mileage was approximately 126,000.Read more
Incident date: Sep 11, 2025
The contact owns a 2020 Hyundai Palisade. The contact received notification of NHTSA Campaign Number: 26V034000 (Air Bags) and 25V607000 (Seat Belts); however, the parts for the repairs were unavailable. The contact stated that the manufacturer had exceeded a reasonable timeframe for the remedies to be available. The contact stated that when driving at various speeds and while idle, the vehicle wo
... uld shake. The contact had checked oil levels and noticed that there was no oil in the vehicle. The contact had to begin changing the oil every 1,000 miles. The contact looked up the CarFax and learned that the vehicle had a history of oil consumption issues. The vehicle was taken to the dealer, who confirmed that the remedies were not available and then diagnosed an oil consumption failure. The dealer completed an oil consumption and cleaning and advised them to drive 1,000 miles to receive assistance for the engine, as it was at risk of seizing. The vehicle was not repaired. The manufacturer was informed of the failure. The manufacturer informed the contact that the failure was not covered by recall or warranty. The failure mileage was approximately 83,000.Read more
Incident date: May 18, 2026
The contact owns a 2018 Ford Edge. The contact stated while driving at an undisclosed speed, the check engine warning light was illuminated. The vehicle was taken to an independent mechanic where it was diagnosed that the head gasket needed to be replaced; the independent mechanic made the contact aware of an unknown technical service bulletin associated with the failure. The vehicle was not repai
... red. The vehicle was taken to a different independent mechanic where it was diagnosed once again that the head gasket needed to be replaced. The vehicle was not repaired. The vehicle was taken to a dealer where it was diagnosed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was approximately 78,000.Read more
Incident date: Oct 1, 2025
The contact owns a 2014 Kia Optima. The contact stated that while driving at 15-20 MPH, the vehicle stalled after 7 months of ownership. The vehicle stalled in the intersection. A few guys were able to push the vehicle out of the roadway. No warning lights were illuminated. The contact received a recall notice for NHTSA Campaign Number: 17V224000 (Engine and Engine Cooling). The vehicle was towed
... to the local dealer, where it was diagnosed as having a locked-down motor. The vehicle was not repaired. The warranty was declined due to the prior service records. The contact mentioned a class action lawsuit. The manufacturer was contacted, who opened a case, but no additional assistance was provided. The failure mileage was approximately 141,000.Read more
Incident date: May 9, 2026
The contact owns a 2026 Honda CBR600RR. The contact stated that while thee vehicle was parked, oil was observed on the ground and oil was observed as empty in the tank. The vehicle experienced a harsh cranking noise and the power diminishes when changing gears. The vehicle was taken to the dealer where engine oil was added and observed for any additional leaks. The dealer stated for the contac
... t to come to the dealer every 200 miles to add oil. The manufacturer was not notified of the issue. The approximate failure mileage was 1,800.Read more
Incident date: May 9, 2026
The contact owns a 2017 Hyundai Santa Fe Sport. The contact stated that while driving approximately 35 MPH a loud noise and smoke was suddenly present coming from under the hood of the vehicle and the engine stalled. The vehicle was towed back to the home. The contact indicated that during the failure no warning messages or lights had displayed. The cause of the failure was not yet determined. The
... local dealer and manufacturer were not yet contacted. The VIN was not available. The failure mileage was 83,000.Read more
Incident date: Apr 19, 2026
The contact owns a 2021 Kia Soul. The contact stated that while driving at an undisclosed speed, the check engine warning light illuminated. The vehicle was taken to an independent mechanic, who determined that one cylinder had low pressure while the other three cylinders had pressures higher than 100%. The contact was informed that the engine needed to be replaced. The vehicle was then taken to t
... he dealer, who performed the recall repair under NHTSA Campaign Number: 25V099000 (Engine And Engine Cooling); however, the engine was not replaced. The piston ring was tested and passed. The vehicle was not repaired. The manufacturer was not made aware of the failure. The failure mileage was approximately 109,000.Read more
Incident date: Apr 15, 2026
The contact owns a 2018 Ford Edge. The contact stated that while driving, the vehicle began to vibrate excessively. There was an abnormal swishing sound detected. The check engine light was illuminated. The vehicle was taken to the local dealer, where a video was sent to the contact displaying coolant intrusion into the cylinders. The vehicle was not diagnosed or repaired. The manufacturer was not
... notified. The failure mileage was approximately 79,000.Read more
Incident date: May 15, 2026
The contact owns a 2019 GMC Acadia. The contact stated that while driving at an undisclosed speed, a “Steering Assist is Reduced ” warning message unexpectedly displayed. The contact also stated that the thermostat became inoperable. Additionally, the thermostat information was no longer displayed on the instrument panel. The vehicle was taken to the dealer, where it was diagnosed that the the
... rmostat had failed and needed to be replaced. The vehicle was not repaired. The manufacturer was made aware of the failure and referred the contact to the NHTSA Hotline for further assistance. The failure mileage was approximately 48,500.Read more
Incident date: Jan 29, 2026
The contact owns a 2023 Chevrolet Silverado LD Crew. The vehicle was taken for a recall repair due to a the crank shaft bearings failure. The contact stated that awhile after the repair was completed , the engine was ticking. The vehicle was taken to the dealer again, where it was diagnosed with metal shavings in the engine. The dealer stated a new motor may be needed which would be the fourth
... motor installed. The vehicle was not repaired. The manufacturer was notified of the issue. The approximate failure mileage was 40,000.Read more
Incident date: Nov 15, 2025
The contact owns a 2017 Ford Escape. The contact stated that when attempting to turn on the AC unit, it would fail, causing them to have to fill the vehicle with new coolant every 2 to 3 weeks. There were no leaks underneath the vehicle or warning lights. The vehicle was not taken to the dealer for diagnosis or repair. The dealer informed the contact that there was no recall attached to the VIN. T
... he manufacturer was not informed. The failure mileage was 140,144.Read more
Incident date: Apr 8, 2026
The contact noticed the oil drained quickly and RPMs increased rapidly upon starting the vehicle. The approximate failure mileage was 86,100. The vehicle was taken to the dealer where the ECU was replaced twice, the piston rings were not replaced; the issue persisted. The manufacturer was notified of the issue. The approximate failure mileage was 86,100
Incident date: Apr 30, 2026
The contact owns a 2008 Hyundai Veracruz. The vehicle The contact stated that while driving, The approximate failure mileage was 202,427. The oil light illuminated, looked and there was no oil. The vehicle knocked. the vehicle stalled.
Incident date: Sep 15, 2024
The contact owns a 2023 Mazda. The contact stated that the vehicle was braking randomly while driving. There was an unknown malfunction code that flashed quickly. The steering was stiff and failed to turn. The steering wheel adjusted and guided the vehicle into the wrong lane. The RPM was sporadically reeving. The RPM increased, and the vehicle stalled without acceleration. There was smoke emergin
... g from the hood. There was oil leaking. The vehicle failed to turn off and on. The fuel gauge and infotainment center were not working properly. The contact stated that while leaving the local dealer, the vehicle stalled. The battery was replaced. The vehicle was towed to another unknown local dealer who determined the battery needed to be replaced. The vehicle was replaced, but the failure recurred. The dealer determined that there was an oil leak and needed to replace the transmission, serpentine belt, and battery. The dealer informed me additional testing was needed. The vehicle was not repaired. The manufacturer was contacted regarding a buyback, but no assistance was provided. The failure mileage was approximately 37,000.Read more
Incident date: May 11, 2026
The contact owns a 2020 Honda Accord. The contact stated that after starting the vehicle the engine was hesitant to start and while driving the flashing check engine light had illuminated and the vehicle did not accelerate past 40 MPH. The vehicle was slowly driven to the local dealer who diagnosed that the both the engine head gasket and water pump needed to be replaced. The vehicle was not yet r
... epaired. The manufacturer was not yet contacted. The contact was informed that the VIN was not included in the NHTSA Campaign Number: 23V858000(FUEL SYSTEM, GASOLINE). The contact indicated that the vehicle had experienced that same failure listed in the recall. The failure mileage was 100,000.Read more
Incident date: Mar 13, 2026
The contact owns a 2019 Ford Mustang. The contact stated while driving at an undisclosed speed, the accelerator pedal was depressed, however the vehicle failed to accelerate as intended. The vehicle's speed did not accelerate above 20 MPH. In addition, the check engine warning light illuminated. The vehicle was driven to the shoulder of the road. The vehicle was towed to the contact's residence. T
... he vehicle was taken to an independent mechanic where it was diagnosed with coolant intrusion and a failed engine. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The vehicle was taken to the dealer where it was diagnosed with coolant intrusion and a failed engine. The contact was informed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was not made aware of the failure. The failure mileage was approximately 103,000.Read more
Incident date: May 6, 2026
The contact owns a 2024 Mini Cooper S. The contact stated that a brake pad failure message was illuminated on the vehicle. The vehicle was taken to the dealer, who diagnosed the brake fluid service issue. The brake fluid flush was completed, and a complimentary oil change was provided. Two days after doing so, approximately two days later, the Oil Light illuminated, advising to add a quart of oil.
... The vehicle was returned and inspected. It was assumed the cap was not on tight enough. The air conditioner failed shortly after. The vehicle was returned, and it was diagnosed that the AC motor had failed. The motor was replaced, and 2 days later, the Oil Light advising for 1 quart of oil illuminated again. The vehicle was taken to a certified mechanic, who diagnosed an oil leak but had not identified where. They added 2 quarts of oil and advised returning to the dealer. The dealer confirmed an oil leak and provided the contact with a loaner. The vehicle was not repaired. The manufacturer was not informed of the issues. The failure mileage was 12,625.Read more
Incident date: May 11, 2026
The contact owns a 2023 Chevrolet TrailBlazer. The contact stated while driving 70 MPH on the interstate , the vehicle independently went into engine power reduce mode. The contact mention she pulled off the interstate, turned the vehicle off for five to ten minutes then turned the vehicle back on and the vehicle began to work as intended. A dealer was contacted. The vehicle was taken to a dealer
... where it was diagnsonesd the turbo booster needed to be replaced. The vehicle was not repaired. The manufacturer was notified on the failure, and they informed her there were no recalls at this time. The approximate failure mileage was 103,000.Read more
Incident date: Apr 22, 2026
The contact owns a 2024 Chevrolet Trax. The contact stated that while driving at 70 MPH with cruise control engaged. The low-pressure oil light illuminated. The driver was able to pull over. The vehicle was taken to the local dealer, who determined that it was 4 quarts low and replenished it. An oil compensation test was performed. The dealer found no issue. While driving, there was an abnormal ba
... nging sound. The "Pull over and turn off the engine" message was displayed. The driver noticed that there was smoke emerging from the engine. There was oil leaking from the vehicle. The vehicle was towed to the local dealer, where it was diagnosed as having a blown engine. A hole was located in the block due to low oil. The vehicle was not repaired due to the parts being backordered. The manufacturer was not contacted. The approximate failure mileage was 41,000.Read more
Incident date: May 12, 2024
The contact owns a 2018 Volkswagen Atlas. The contact stated that while driving on several occasions at various speeds, "low coolant" and "overheating" messages and the check engine warning light illuminated. On the first two occasions, the low coolant message appeared. The vehicle was pulled to the side of the road and inspected, and she observed a leak under the engine compartment. The vehicle w
... as taken to the same dealer twice, where it was diagnosed that the water pump needed to be replaced. The vehicle was repaired twice, but the failure reoccurred approximately two years later. The contact stated that on the third occasion, an "overheating, turn engine off immediately" message appeared and an alert warning chime went off. The vehicle was pulled over to the side of the road and turned off to cool down. The contact stated that when the vehicle was turned on, it began to overheat again. The vehicle was then towed to the same dealer, where it was diagnosed that the water pump and a possible additional unknown failure were the cause. The vehicle was repaired, but the failure persisted. The dealer advised the contact that they may need to replace the head gasket as well. The vehicle was not repaired. The manufacturer was not notified of the failure. The failure mileage was approximately 40,000.Read more
Incident date: May 12, 2026
The contact owns a 2023 Chevrolet Tahoe. The contact stated that while driving at 75 MPH, the vehicle shut off without warning. Due to the failure, the contact used excessive force to steer the vehicle off to the shoulder of the highway where the vehicle was then towed to a dealer. After the vehicle remained in the dealer's possession for over a week, the vehicle was diagnosed with an engine failu
... re. The contact was then informed that the vehicle was placed under recall NHTSA Campaign Number: 25V274000 (Engine) and that the engine would be replaced. Despite the engine repair, the contact stated that an abnormal, rattling sound would emit from the vehicle upon start of the engine. In addition, the contact stated that the vehicle would violently jerk upon depression of the accelerator pedal while at a complete stop. The failure started intermittently; however, the contact stated that overtime the failure became more persistent. The vehicle was taken to the dealer where they claimed that the transmission was four quarts low on transmission fluid; they then informed the contact that they could not guarantee that remedy would repair the failure. The contact stated that failure improved; however, she would still experience a slight hesitation upon depression of the accelerator pedal. The manufacturer was notified of the failure but offered no assistance. The vehicle was not repaired. The failure mileage was approximately 39,000.Read more
Incident date: May 9, 2026
The contact's friend owns a 2017 Ford Escape. The contact stated that the owner had to add additional coolant after it was low. The vehicle stalled while driving, and all the coolant was depleted. The owner used approximately 2 jugs of antifreeze. The driver was stranded. The low coolant light was illuminated. The vehicle was pulled to the owner's residence. The local dealer was contacted, but the
... vehicle was not diagnosed or repaired. The manufacturer was not notified. The failure mileage was approximately 145,000.Read more