HUGHES 269A

Mc Cool Junction, NE — September 19, 2012

Event Information

DateSeptember 19, 2012
Event TypeACC
NTSB NumberCEN12LA648
Event ID20120920X63049
LocationMc Cool Junction, NE
CountryUSA
Coordinates40.74100, -97.59093
Highest InjuryNONE

Aircraft

MakeHUGHES
Model269A
CategoryHELI
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Event Location

Probable Cause

The flight instructor’s inadequate supervision of the student pilot’s entry into the autorotation, which resulted in a hard landing. Contributing to the accident was the loss of engine power as a result of the student pilot rapidly lowering the helicopter’s collective and the partly obstructed air filter.

Full Narrative

On September 19, 2012, about 1230 central daylight time, a Hughes 269A, helicopter, N37754, performed a hard landing, following an autorotation near Mc Cool Junction, Nebraska. The certificated flight instructor (CFI) and student pilot were not injured. The helicopter sustained substantial damage to the fuselage and tail boom. The helicopter was registered to and operated by the Star City Flying Club, Lincoln, Nebraska, under the provisions of 14 Code of Federal Regulations Part 91 as an instructional flight. Visual meteorological conditions prevailed for the flight, which operated without a flight plan. The flight originated from a private airfield.

According to statements taken by the responding Federal Aviation Administration inspectors, the purpose of the flight was to prepare the student pilot for an upcoming check ride. After takeoff, about 400 feet above ground level and at an airspeed on 50 knots, the CFI brought the engine back to idle to simulate a loss of engine power. The student dropped the collective and the engine quit producing power. An autorotation was initiated; however, the helicopter rapidly descended and landed hard. The tail boom was severed and the helicopter rolled over on its side. An inspection of the airframe and engine by inspectors from the FAA inspectors revealed that the air filter was approximately 80% obstructed by debris. A ground run was performed on the engine and the engine was found to have an excessively rich mixture.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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