BEECH 35

Geary, OK — September 9, 2012

Event Information

DateSeptember 9, 2012
Event TypeACC
NTSB NumberCEN12CA625
Event ID20120912X50304
LocationGeary, OK
CountryUSA
Coordinates35.61945, -98.52250
AirportMcKinley Ranch Airport
Highest InjuryNONE

Aircraft

MakeBEECH
Model35
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Event Location

Probable Cause

The student pilot failed to maintain control of the airplane during a forced landing attempt which resulted in an aerodynamic stall. Contributing to the accident was the instructor pilot's delay in taking control of the airplane and the loss of engine power for undetermined reasons.

Full Narrative

After an uneventful local instructional flight, the student pilot and instructor pilot were practicing emergency landing procedures. After a missed approach to the private ranch airport, the student attempted a go-around. During the go-around, there was a loss of engine power during the climb and the student pilot tried to set up for an actual emergency landing. While maneuvering the airplane to land, both the instructor pilot and student attempted to trouble shoot and regain engine power by switching fuel tanks attempting a restart. About 20 feet above the runway, the airplane stalled, impacted the runway, and came to a stop in a grassy area to the left of the runway. Both wings sustained substantial damage. After the accident, the student pilot, who owned the airplane, stated that he may have moved the fuel selector lever to the left tank position while he and the instructor were trying to trouble shoot the loss of engine power. The instructor pilot occupied the right seat and would not have been able to see the fuel selector lever position. Postaccident examination of the airplane and engine revealed that both the right main fuel tank and auxiliary fuel tank had usable fuel. The left main fuel tank was empty and was not compromised. The fuel selector lever was found in the left tank position. No evidence of mechanical malfunction or any other preimpact abnormalities were found. Although the loss of engine power could be linked to possible fuel starvation, the cause for the loss of engine power could not be substantiated.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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