Ziermann RV8

Garrison, MN — January 12, 2008

Event Information

DateJanuary 12, 2008
Event TypeACC
NTSB NumberCHI08LA067
Event ID20080122X00082
LocationGarrison, MN
CountryUSA
Coordinates46.32139, -93.84028
Highest InjurySERS

Aircraft

MakeZiermann
ModelRV8
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious1
Minor0
None0
Total Injured1

Event Location

Probable Cause

The loss of engine power for undetermined reasons during cruise and the misjudged flare resulting in a hard landing. Contributing to the accident was the frozen lake to which the pilot performed a forced landing.

Full Narrative

On January 12, 2008, about 1238 central standard time, N617MZ, an experimental amateur-built Ziermann RV8 airplane, operated by a private pilot, sustained substantial damage on impact with Round Lake during a forced landing following an in-flight loss of engine power near Garrison, Minnesota. The 14 CFR Part 91 personal flight was operating in visual meteorological conditions. No flight plan was on file. The pilot received serious injuries. The flight originated about 1215 from the Brainerd Lakes Regional Airport, near Brainerd, Minnesota, and was destined for the Winsted Municipal Airport, near Winsted, Minnesota.

The Aitkin County Sheriff's interview of a witness who was fishing on Round Lake, in part, stated:

[The witness] was outside of his fish house, when he heard this plane,
the engine was sputtering, that was traveling east. [The witness] stated,
the plane then banked hard right, and went down on the ice. [The
witness] stated, the plane was almost flat when it hit the ice. When it
hit, debris started to fly around, and the plane spun around, and slid to
a stop.

The pilot's accident report stated, "Headed home after eating lunch, no indication of any trouble up to that point." The pilot reported that he departed on the flight with 30 gallons of 100 low lead aviation gasoline on board the airplane.

A Lycoming IO-360 engine with serial number L-20187-51A powered the airplane. The airplane's last conditional inspection was conducted on October 7, 2007. The pilot reported that the airplane had accumulated 279.5 hours of total time at the time of the accident.

Engine logbook entries show that the engine was previously installed on a Lake LA-4-200, N3027P. An entry dated May 7, 1996, indicated that the Lake LA-4-200 airplane was destroyed in an accident and that the engine had accumulated a total time of 1,529.0 hours. The endorsement on the engine logbook's next page showed maintenance actions that included an inspection of cylinder compression. That page was signed off with the accident pilot's name, certificate number, and signature.

Federal Aviation Administration inspectors examined the airplane wreckage. Flight and engine control continuity was established. No pre-impact anomalies were detected.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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