Schweizer 300C

Ogden, UT — June 2, 2008

Event Information

DateJune 2, 2008
Event TypeACC
NTSB NumberLAX08CA138
Event ID20080627X00938
LocationOgden, UT
CountryUSA
Coordinates41.35472, -112.00639
AirportOgden
Highest InjurySERS

Aircraft

MakeSchweizer
Model300C
CategoryHELI
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious1
Minor0
None1
Total Injured1

Event Location

Probable Cause

The pilot under instruction's encounter with a settling with power condition, and the flight instructor's failure to maintain adequate rotor rpm during the subsequent go-around. Also causal was the instructor pilot's delayed remedial action during the approach sequence and his inadequate supervision of the flight.

Full Narrative

In a written statement, the instructor pilot reported that he and the private pilot under instruction performed a normal takeoff and departure. After a short flight they arrived at Rocky Point (9 miles north of Ogden-Hinckly Airport), where they were to practice pinnacle approaches and landings. They reconnoitered the area at 300 feet above ground level (agl) in preparation for landing. They performed a power check at 500 feet agl, and concluded that engine power was sufficient to maintain an out of ground effect (OGE) hover. The student began the approach at 350 feet agl. The approach became slightly steep and went past the point of the intended landing. The pilot under instruction reported that the rate of descent was 500 feet per minute (fpm) at 25 knots. At 30 feet agl, the helicopter's descent rate increased, the pilot under instruction aborted the approach, and began a go-around. The instructor realized that rotor revolutions-per-minute (rpm) had degraded below the normal range, so he took the controls from the student. Because the go-around had been initiated, the helicopter was moving forward slowly over a descending hill slope and the instructor was not able to land the helicopter. He attempted to gain power by lowering and raising collective; however, the helicopter's skid contacted the ground and the helicopter rolled over.

FAA-H-8083-21, Rotorcraft Flying Handbook, states that vortex ring state (settling with power) is likely when the rate of descent exceeds 300 fpm, and the horizontal velocity is slower than effective translational lift.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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