GARLICK HELICOPTERS INC OH-58A+
Rowley, MA — July 15, 2010
Event Information
| Date | July 15, 2010 |
| Event Type | ACC |
| NTSB Number | ERA10LA362 |
| Event ID | 20100716X02415 |
| Location | Rowley, MA |
| Country | USA |
| Coordinates | 42.77056, -70.87473 |
| Highest Injury | NONE |
Aircraft
| Make | GARLICK HELICOPTERS INC |
| Model | OH-58A+ |
| Category | HELI |
| FAR Part | 137 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 0 |
| Minor | 0 |
| None | 2 |
| Total Injured | 0 |
Event Location
Probable Cause
The failure of the power turbine governor internal driveshaft bearings, resulting in the failure of the governor.
Full Narrative
On July 15, 2010, at 1358 eastern daylight time, a Garlick Helicopter, OH-58A+, N802JB, registered to and operated by Horizon Helicopters LLC, experienced a hard landing in a salt marsh following a loss of the main rotor rpm control near Rowley, Massachusetts. The aerial application flight was operated under the provisions of 14 Code of Federal Regulation Part 137 with no flight plan filed. Visual meteorological conditions prevailed. The certificated commercial pilot and passenger reported no injuries, and the helicopter was substantially damaged. The flight departed Kent's Island road, Newbury, Massachusetts, at 1342.
The pilot stated that he was performing an aerial application when the low rotor rpm audio warning sounded. The collective was lowered and the rpm returned to normal. The pilot elected to fly the helicopter for another 30 minutes to ensure normal operation, and the helicopter operated normally. Shortly thereafter, while in cruise flight at approximately 200 feet above ground level at 70 knots, the low rotor rpm audio warning sounded again. The collective was lowered to restore rotor rpm, but engine and rotor speed accelerated through the upper limits. The collective was then increased to load the engine and main rotor to prevent an over-speed. This attempt had no noticeable effect and, subsequently, the pilot rolled the throttle to idle, performed an autorotation, landed hard, and buckled the tail boom. The pilot did not report any flight control anomalies prior to the accident.
A Federal Aviation Administration inspector examined the helicopter. Flight control continuity was confirmed from the cockpit through the tail rotor system, and from the cockpit cyclic and collective controls through the main rotor head. Further examination of the helicopter revealed that the power turbine governor was damaged, and removed for further examination.
The power turbine governor was examined by representatives of the power turbine governor, bearing and engine manufacturers, under the supervision of the FAA inspector, on September 1 2010. Examination of the drive housing and drive shaft assemblies revealed that the inner and outer races were "frosted" in the ball tracks. Further examination of the driveshaft revealed that the bearing ball separators were damaged. A review of the engine records indicated that the last overhaul of the power turbine governor was completed at 1,942.9 hours time since new. The power turbine governor had accumulated an additional 1,590 hours time since overhaul. The power governor turbine time before overhaul (TBO) time is 2,000 hours.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.