CESSNA 172N
Longmont, CO — May 4, 2025
Event Information
| Date | May 4, 2025 |
| Event Type | ACC |
| NTSB Number | CEN25LA168 |
| Event ID | 20250505200108 |
| Location | Longmont, CO |
| Country | USA |
| Coordinates | 40.17483, -105.18750 |
| Airport | VANCE BRAND |
| Highest Injury | NONE |
Aircraft
| Make | CESSNA |
| Model | 172N |
| Category | AIR |
| FAR Part | 091 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 0 |
| Minor | 0 |
| None | 1 |
| Total Injured | 0 |
Probable Cause
The disconnected throttle control that resulted in a loss of engine power due to improper maintenance.
Full Narrative
On May 4, 2025, about 1200 mountain daylight time, a Cessna 172N airplane, N75775, was substantially damaged when it was involved in an accident near Longmont, Colorado. The student pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.
The student pilot stated that he was on final approach when he noticed that the engine was not responding to his throttle control changes. The engine speed was about 2,000 rpm when he attempted a go-around. However, the engine power did not increase as he applied full throttle, and the airplane would not climb due to the low power setting. He noted that the engine subsequently lost power completely and he executed a forced landing to a field. During the landing, the airplane struck a fence and nosed over. The airframe sustained substantial damage to the right wing, vertical stabilizer, and rudder.
A post-accident examination conducted by a Federal Aviation Administration inspector determined that the throttle cable was disconnected from the carburetor. Both the throttle cable and the carburetor control arm moved freely and there was no evidence of damage to either component. The connecting hardware – bolt and nut – were not observed at the time of the examination.
Airplane maintenance records revealed that a 100-hour inspection was completed three weeks before the accident, and the engine carburetor was replaced at that time. The airplane had accumulated about 9.9 hours flight time since that maintenance. The mechanic noted that an apprentice had replaced the carburetor. He had gotten busy with other tasks and did not fully inspect the apprentice’s work.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.