PIPER PA-18-150
Wasilla, AK — February 21, 2025
Event Information
| Date | February 21, 2025 |
| Event Type | ACC |
| NTSB Number | ANC25LA019 |
| Event ID | 20250221199729 |
| Location | Wasilla, AK |
| Country | USA |
| Coordinates | 61.48950, -149.60366 |
| Airport | Tidewater Airport |
| Highest Injury | NONE |
Aircraft
| Make | PIPER |
| Model | PA-18-150 |
| Category | AIR |
| FAR Part | 091 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 0 |
| Minor | 0 |
| None | 1 |
| Total Injured | 0 |
Event Location
Probable Cause
A total loss of engine power for undetermined reasons.
Full Narrative
On February 20, 2025, about 1642 Alaska standard time, a Piper PA-18-150 airplane, N2447J, was substantially damaged when it was involved in an accident near Wasilla, Alaska. The pilot was uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
According to the pilot, he departed Tidewater Airport (77AK) about 1500 and flew the airplane to a different airport and completed about 15 practice landings. He then flew back to 77AK, where he landed then decided to depart again to practice touch-and-go landings. He stated that, during final approach to runway 01 with the carburetor heat on, the airplane’s engine suddenly lost total power when the airplane was about 400 to 450 ft above ground level. After assessing that the airplane had insufficient altitude to glide to the runway, the pilot selected nearby hay flats as a forced landing site. During the forced landing, the right main landing gear collapsed, and the airplane’s right wing impacted terrain, resulting in substantial damage to the fuselage and right wing. The pilot reported that, after the accident, he observed fuel leaking from the damaged right wing, so he positioned the fuel selector to the left tank to stop some of the fuel from leaking out.
A postaccident examination of the engine revealed no evidence of any preimpact mechanical malfunction or failure that would have precluded normal operation. The examination included disassembly of the carburetor heat control cable with no discrepancy noted. About 8 gallons of fuel was recovered from the left wing, about 14.5 gallons was recovered from the right wing, and about 2.5 gallons was recovered from the fuselage sump drains.
The recorded temperature and dew point near the accident site were about 39°F and 19°F, respectively. A review of the Carburetor Icing Probability Chart located in the FAA’s Special Airworthiness Information Bulletin (SAIB) CE-09-35, Carburetor Icing Prevention, dated June 30, 2009, indicated that these conditions were conducive to the formation of carburetor icing at glide and cruise power settings. The SAIB stated that, to prevent carburetor icing, the pilot should assure the proper functionality of the carburetor heat during the before takeoff check and use carburetor heat on approach and descent when operating at low power settings or in conditions where carburetor icing is probable.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.