BEECH H35

LaCrosse, WA — July 1, 2022

Event Information

DateJuly 1, 2022
Event TypeACC
NTSB NumberWPR22LA247
Event ID20220712105457
LocationLaCrosse, WA
CountryUSA
Coordinates46.78597, -117.90988
Highest InjurySERS

Aircraft

MakeBEECH
ModelH35
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious1
Minor0
None0
Total Injured1

Event Location

Probable Cause

The pilot’s failure to monitor and manage the fuel supply, which resulted in a loss of engine power due to fuel starvation.

Full Narrative

On July 1, 2022, about 1340 Pacific daylight time, a Beechcraft H35 Bonanza, N5546D, was substantially damaged when it was involved in an accident near Lacrosse, Washington. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot reported that he departed from Arlington Municipal Airport (KAWO), Arlington, WA, after an extended preflight and ground run, with an intended destination of Port of Whitman Business Air Center Airport (S94), Colfax, WA. The pilot reported the airplane contained 50 gallons of fuel on departure. After about 1.5 hours, while the pilot performed his pre-landing checklist for his approach, the engine lost all power. The pilot described that the engine power loss sounded as if the engine went to idle. He then switched the fuel selector from the right to left fuel tank, applied full throttle, and increased the mixture to full rich, but the engine did not respond. Shortly after, the pilot initiated a forced landing onto a wheat field. The engine separated from the firewall and the airplane sustained substantial damage to the engine mount and truss during the landing.
Postaccident examination of the airframe and engine did not reveal any preimpact mechanical anomalies. Flight control continuity was established from the cockpit to all flight surfaces. The fuel system was traced from each wing tank to the fuel selector, which rotated normally and was unobstructed. The right main, left main, right auxiliary, and left auxiliary tanks were not breached and had about 2 gallons, 4 gallons, 8 gallons, and 2.5 gallons, respectively. According to the manufacturer, the unusable fuel of each 20-gallon main tank is 3 gallons and there is a total of 1 gallon of unusable fuel in both auxiliary tanks combined.
Mechanical continuity was established throughout the rotating group, valvetrain, and accessory section as the crankshaft was manually rotated at the propeller by hand. Thumb compression was achieved at all six cylinders and the valves displayed normal lift when the crankshaft was rotated. Examination of the cylinders’ combustion chamber using a lighted borescope revealed normal piston face and valve signatures, and no indications of catastrophic engine failure.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

All Aviation Events More in WA