GRUMMAN AMERICAN AVN. CORP. AA-1B

River Falls, WI — June 1, 2022

Event Information

DateJune 1, 2022
Event TypeACC
NTSB NumberCEN22LA220
Event ID20220601105171
LocationRiver Falls, WI
CountryUSA
Coordinates44.83978, -92.75065
AirportST CROIX RIVIERA
Highest InjurySERS

Aircraft

MakeGRUMMAN AMERICAN AVN. CORP.
ModelAA-1B
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious1
Minor1
None0
Total Injured2

Event Location

Probable Cause

The student pilot’s and flight instructor’s inadequate preflight fuel planning, which resulted in a total loss of engine power due to fuel exhaustion.

Full Narrative

On June 1, 2022, about 1215 central daylight time, a Grumman AA-1B airplane, N6298L, was substantially damaged when it was involved in an accident near St. Croix Riviera Airport (6WI2), River Falls, Wisconsin. The student pilot sustained minor injuries, and the flight instructor sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.
The flight instructor reported that, during the accident flight, he and the student pilot performed two takeoffs and landings and that, on the third takeoff, the engine “quit abruptly” at an altitude of about 150 ft. The flight instructor stated that the engine appeared to have “seized instantly.” The student pilot reported that, during the initial climb after takeoff and when the airplane was about 150 to 200 ft above ground level, the engine “locked up” and lost total power. At that time, the flight instructor assumed control of the airplane and made a forced landing to a vacant field south of the airport, which was straight ahead of the departure runway. The airplane came to rest upright in the field, which resulted in substantial damage to the left outboard wing panel.
Examination of the airplane at the accident scene found no fuel in the wing fuel tanks. A subsequent examination revealed that the fuel tanks were not breached and that the other fuel system components had no discrepancies. According to the accident report submitted by the flight instructor they departed with 8 gallons of fuel and were flying for about 1 hour and 15 minutes.
The engine rotated freely, and compression was verified on all cylinders. Both magnetos produced spark when rotated.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

All Aviation Events More in WI