MOONEY M20E

Livermore, CA — February 24, 2021

Event Information

DateFebruary 24, 2021
Event TypeACC
NTSB NumberWPR21LA119
Event ID20210226102679
LocationLivermore, CA
CountryUSA
Coordinates37.69909, -121.81075
AirportLIVERMORE MUNI
Highest InjuryNONE

Aircraft

MakeMOONEY
ModelM20E
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Event Location

Probable Cause

A total loss of engine power due to fuel starvation as a result of corrosion and rust in the fuel injection servo.

Full Narrative

On February 23, 2021, at 1645 Pacific standard time, a Mooney M20E, N3254F, was substantially damaged when it was involved in an accident near Livermore, California. The pilot and one passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, the takeoff from runway 7 was normal; about 100 ft above ground level (agl), the engine lost total power. The pilot elected to make an off-airport landing about 1 mile northeast of the airport on the overpass of Interstate 580. During the landing roll, the propeller struck the trunk of a car. The airplane pivoted around and impacted the left side of the car before coming to a stop near the side of the road.

The driver of the car, the sole occupant, was not injured.

According to a Federal Aviation Administration (FAA) inspector, the airplane sat outside, and had not been flown for about 8 to 10 years before the accident flight. When the fuel tanks were slumped, a small quantity of water was present in the right fuel tank, and the left tank was free of contamination.

A visual examination of the engine revealed no evidence of any mechanical damage to the crankcase. The engine was manually rotated, and mechanical and valve train continuity established. The engine-to-magneto timing was within manufacturer limits. The spark plugs were removed and were in good condition. When the engine was manually rotated, the P-leads sparked at all cylinders. The fuel flow divider was disassembled and was clear of debris; the diaphragm was intact. The fuel injectors were removed and were clear of debris.

A visual examination of the fuel servo revealed that it was intact and not damaged. The throttle and mixture levers were free to move from stop-to-stop. Before attaching it to the test stand, the fuel servo inlet screen was removed and inspected; debris was observed in the inlet screen.

A functional test of the fuel servo was unsuccessful; no fuel flowed through the unit. The fuel servo was disassembled for further examination. Extensive corrosion and debris were noted in the regulator center body and diaphragm assembly, which prevented a successful fuel flow check on the test stand. The corrosion and debris were attributed to water in the system.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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