BEECH B24R

Bellefontaine, OH — March 15, 2009

Event Information

DateMarch 15, 2009
Event TypeACC
NTSB NumberCEN09LA209
Event ID20090316X92527
LocationBellefontaine, OH
CountryUSA
Coordinates40.37222, -83.82000
AirportBellefontaine Regional Airport
Highest InjuryNONE

Aircraft

MakeBEECH
ModelB24R
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Event Location

Probable Cause

The inadequate torque of the Number 3 cylinder rod bolts by maintenance personnel, which resulted in a failure of the connecting rod and a total loss of engine power.

Full Narrative

On March 15, 2009, at 1500 eastern daylight time (edt), a Beech B24R (Sierra), N9348S, owned and piloted by a private pilot, was substantially damaged during a forced landing following an en route loss of engine power near Bellefontaine, Ohio. Visual meteorological conditions prevailed at the time of the accident. The personal flight was operating under the provisions of 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The pilot and his passenger were not injured. The flight departed Grimes Field Airport (I74), near Urbana, Ohio, at 1445 edt and was en route to Bluffton Airport (5G7), near Bluffton, Ohio.

According to the pilot, the airplane was in cruise flight when he noticed abnormal engine noises and a partial loss of engine oil pressure. He immediately diverted to the nearest airport, Bellefontaine Regional Airport (KEDJ), and entered downwind for runway 7 (4,999 feet by 100 feet, asphalt). During the turn to base leg, the engine oil pressure dropped to zero pounds per square inch and the engine seized. He established best glide speed and continued the turn onto final approach. The pilot reported that the airplane was not in a position to reach the runway threshold, or to clear the airport perimeter fence. He lowered the landing gear and selected full flaps prior to landing in the grass area outside of the airport perimeter fence. During landing rollout the airplane impacted the airport perimeter fence, damaging both wings and the nose landing gear.

An engine teardown examination revealed that the number 3 cylinder connecting rod assembly had separated from its corresponding crankshaft journal. The crankshaft journal surface was blue in color, consistent with exposure to excessive heat and lack of lubricant. The oil suction screen was obstructed with bearing material. The number 3 cylinder connecting rod cap was found jammed beneath the counterbalance weight. One of the two connecting rod stretch bolts remained intact. The corresponding nut was found finger tight. The measured torque for the upper and lower stretch bolts on the number 2 cylinder connecting rod was 15 foot-pounds (ft-lbs) and 6 ft-lbs, respectively. The manufacturer specified torque value was 40 ft-lbs. The Lycoming IO-360-A1B6 engine, serial number L-13455-51A, had accumulated 492.7 hours since its last overhaul in September 1999 following a propeller strike.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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