Piper PA 31P

East Brady, PA — August 20, 2019

Event Information

DateAugust 20, 2019
Event TypeACC
NTSB NumberERA19LA252
Event ID20190821X63912
LocationEast Brady, PA
CountryUSA
Coordinates40.93111, -79.66222
Highest InjuryNONE

Aircraft

MakePiper
ModelPA 31P
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Event Location

Probable Cause

A total loss of left engine power for undetermined reasons.

Full Narrative

On August 20, 2019, about 1130 eastern daylight time, a Piper PA-31P, N90AP, was substantially damaged when it was involved in an accident near East Brady, Pennsylvania. The private pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot had recently purchased the airplane and had an annual inspection completed. The airplane had not undergone an annual inspection since April 21, 2010, and in that time, had accumulated 3 hours of total flight time. The pilot reported that, after a normal preflight and engine runup, he departed on a cross-country flight with all six fuel tanks filled to capacity, a total of 242 gallons. He initially set the fuel selectors to the inboard fuel tanks, then after 30 minutes of flight time, he switched to the outboard tanks. About 45 minutes en route, and 15 minutes after switching tanks, the left engine lost total power. Unable to restore power to the left engine per the emergency checklist, he secured the left engine and applied climb power to the right engine, but the airplane continued to descend. The pilot performed a forced landing to a field, during which the airplane impacted an electric fence and trees and came to rest 180° from the direction of travel.
According to the Federal Aviation Administration (FAA) inspector who responded to the accident site, the landing gear had separated, and the right aileron, right wing tip, elevator, and left aileron displayed damage. A detailed examination confirmed engine continuity and compression. The left and right magnetos were disassembled and revealed no anomalies.
Further testing was conducted on the fuel servo and controller. The fuel servo was within limits but was not the correct part number. The controller was within the lower limits but did not meet the high-end fuel flow limits. Postaccident examination of the engine revealed no other evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation.

Examination of the airplane’s maintenance records found no indication that FAA Airworthiness Directive 2009-02-03, which requires inspecting servo plugs for looseness and damage and inspecting the servo plug gasket, had been complied with.
The airplane was equipped with three fuel tanks in each wing: outboard, inboard, and a nacelle tank. The two inboard fuel tanks had a capacity of 56 gallons each; the outboard fuel tanks had a capacity of 40 gallons each, and the two nacelle fuel tanks had a capacity of 25 gallons each. The left wing outboard and inboard tanks were empty; the nacelle tank was full. The right-wing outboard tank was empty; the inboard and nacelle fuel tanks were full.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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