CASHEN Super Acro Sport

Detroit Lakes, MN — July 16, 2019

Event Information

DateJuly 16, 2019
Event TypeACC
NTSB NumberCEN19LA226
Event ID20190720X65807
LocationDetroit Lakes, MN
CountryUSA
Coordinates46.83306, -95.89389
AirportDetroit Lakes-Wething Field
Highest InjuryMINR

Aircraft

MakeCASHEN
ModelSuper Acro Sport
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor1
None0
Total Injured1

Probable Cause

An open circuit in the engine's electrical switch box, which resulted in a partial loss of engine power and subsequent forced landing.

Full Narrative

On July 16, 2019, about 1845 central daylight time, an experimental Super Acro Sport airplane, N61SC, made a forced landing in a cornfield near Detroit Lakes Airport (DTL), Detroit Lakes, Minnesota. The pilot sustained minor injuries and the airplane sustained substantial damage. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time of the accident and no flight plan had been filed. The local fight had departed about 1815 and was returning to DTL at the time of the accident.
The pilot stated to the responding Federal Aviation Administration (FAA) inspector that he was conducting a local flight to ensure the airplane was operating normally for his upcoming trip. While returning to the airport the engine suddenly experienced and loss of power and he was unable to maintain altitude. He could not reach the airport so he executed a forced landing to the corn field. After the airplane flipped inverted, he exited under his own power. The pilot added that he had installed a 260-horsepower Mercury marine-type outboard engine. This engine was too heavy for the airplane so he later installed a 200-horsepower Mercury marine-type outboard engine, which was water-cooled with a fabricated radiator and heat exchange system.
The airplane came to rest inverted in a corn field about 1/4-mile northwest of DTL. About 50 ft of corn had been flattened leading up the accident site. Fuel residue was observed around the airplane's fuel tank and absorbent material had been placed on the ground by first responders to absorb the fuel spillage.
In a post-accident statement, the pilot reported that he was about 1.5 miles north of runway 17 when he felt the airplane settle so he advanced the throttle, but the engine did not respond. He was unable to reach the runway so he completed a "falling leaf" maneuver to descend quickly. As the airplane approached the ground, he "broke the stall" and then settled into the corn stalks. The airplane continued forward about 150 ft, then nosed over and came to rest inverted. He added that the engine was new and had accumulated about 4.5 hours of ground run time with no anomalies.
On July 29, 2019, the pilot reported to the NTSB that he had examined the engine and determined that one of the engine's electrical switch boxes had an open circuit and the open circuit did not allow and electrical charge to reach the Nos. 1, 3, and 5 spark plugs. The other switch box that allowed electrical charge to the other 3 cylinders had a closed circuit and operated normally.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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