DENNIS l ZUMBALT SKY BOLT
Deming, NM — March 23, 2019
Event Information
| Date | March 23, 2019 |
| Event Type | ACC |
| NTSB Number | WPR19LA101 |
| Event ID | 20190326X93228 |
| Location | Deming, NM |
| Country | USA |
| Coordinates | 32.26024, -107.74970 |
| Airport | Private airstrip |
| Highest Injury | SERS |
Aircraft
| Make | DENNIS l ZUMBALT |
| Model | SKY BOLT |
| Category | AIR |
| FAR Part | 091 |
| Aircraft Damage | SUBS |
Conditions
| Light Condition | DAYL |
| Weather | VMC |
Injuries
| Fatal | 0 |
| Serious | 1 |
| Minor | 0 |
| None | 0 |
| Total Injured | 1 |
Event Location
Probable Cause
The pilot’s failure to properly position the fuel selector before takeoff, which resulted in a total loss of engine power due to fuel starvation.
Full Narrative
On March 23, 2019, about 1130 mountain daylight time, an experimental, amateur-built Sky Bolt airplane, N254PM, was substantially damaged when it was involved in an accident near Deming, New Mexico. The pilot was seriously injured. The airplane was being operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot reported that he was departing on a local flight when the engine lost total power near the end of the runway at an altitude of about 400 ft above ground level. The pilot turned left and lowered the nose to maintain airspeed. Unable to make it back to the runway, the pilot made a sharp right turn and the airplane touched down in an open dirt area and traveled about 50 ft before it collided with a sand dune, then came to a complete stop upright. As a result of the landing sequence, the airplane sustained structural damage to the upper wing spar, the right lower wing panel, and the forward section of the fuselage. The pilot reported that he took off with 25 gallons of automotive fuel onboard, which he added to the main header tank before takeoff. The pilot further reported no mechanical issues with the airplane or engine before departure.
The fuel selector was found in the AUX/wing tank position following the accident. Examination of the airframe and engine revealed no evidence of any preimpact mechanical malfunctions or anomalies that would have precluded normal operation.
During a follow-up telephone interview, the pilot stated that he never fueled the AUX/wing tank, and that he only filled and operated off the main header tank.
About This NTSB Record
This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.