Piper PA32

Wrangell, AK — September 3, 2018

Event Information

DateSeptember 3, 2018
Event TypeACC
NTSB NumberANC18LA069
Event ID20180906X05209
LocationWrangell, AK
CountryUSA
Coordinates55.96889, -132.42305
Highest InjuryNONE

Aircraft

MakePiper
ModelPA32
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Event Location

Probable Cause

The total loss of engine power due to oil starvation after an interruption of oil circulation for reasons that could not be determined based on the available evidence.

Full Narrative

On September 3, 2018, about 1353 Alaska daylight time, a Piper PA-32 airplane, N3957X, sustained substantial damage when it was involved in an accident near Wrangell, Alaska. The private pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, while in level cruise flight, the engine rpm increased from a cruise power setting of 2,300 to 3,100, and he reduced the manifold pressure to correct for the high rpm. Shortly thereafter, he noticed the engine oil pressure drop and oil visible on the airplane’s windscreen, followed by a total loss of engine power. He performed an emergency landing near the high tide line in an area of seagrass. During the emergency landing, the airplane sustained substantial damage to the fuselage and left wing.

The airplane was equipped with a Lycoming IO-540-K1G5 engine. Examination of the engine revealed a large fracture hole near the Nos. 4- and 5-cylinder pads. The Nos. 4 and 5 connecting rods were fragmented, and pieces of the connecting rods and a large amount of metal debris were located within the engine and oil suction screen. The Nos. 4 and 5 connecting rods and rod bearing journals exhibited extensive mechanical damage and signatures consistent with extreme high heat.

The engine oil pump was intact with no evidence of thermal damage. The engine case halves displayed mechanical damage with multiple protrusions from the inside out. When the oil sump was removed, damaged connecting rod ends and a large amount of metal debris were discovered.

The pilot reported that the oil filter element had not been cut and examined at the last oil change, contrary to Lycoming Mandatory Service Bulletin No. 480F.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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