BEECH B36TC

LaPorte, TX — August 20, 2018

Event Information

DateAugust 20, 2018
Event TypeACC
NTSB NumberCEN18LA340
Event ID20180820X05353
LocationLaPorte, TX
CountryUSA
Coordinates29.67250, -95.06973
AirportLa Porte Municipal
Highest InjuryNONE

Aircraft

MakeBEECH
ModelB36TC
CategoryAIR
FAR Part091
Aircraft DamageDEST

Conditions

Light ConditionDAWN
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Event Location

Probable Cause

The loss of engine power due to a torn intercooler hose that resulted in an overly rich fuel mixture, which, when combined with the pilot's activation of the auxiliary fuel pump, flooded the engine.

Full Narrative

On August 20, 2018, at 0620 central daylight time, a Beech B36TC single-engine airplane, N6860W, was destroyed when the engine lost power and the pilot made a forced landing in a wooded area 1/4-mile southeast of La Porte Municipal Airport (T41), La Porte, Texas. The airplane was registered to and operated by RD Airways, Channelview, Texas, under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed for local flight. The flight was originating from T41 at the time of the accident.The pilot reported that after taking off and starting a climb, the airplane began to make a "weird very loud sound and the engine started to lose power." The pilot verified the throttle, mixture, and propeller controls were full forward. The engine noise "started to get louder and power was almost gone." When the pilot activated the auxiliary fuel pump, the engine "just got real loud [and] sounded very deep. I knew I was descending." The airplane continued to descend, and the pilot made a forced landing near a housing development on unsuitable terrain. Both wings were separated from the airplane. The pilot was not injured.

A Federal Aviation Administration (FAA) inspector examined the airplane, and reported "the exhaust section looks like it had been having some issues for a while. Also disturbing is the v-band clamp condition." He also stated an Airworthiness Directive (A.D. 2018-06-11) had been issued in June 2018. That AD added a life limit to the exhaust tailpipe v-band clamp that attaches the exhaust tailpipe to the turbocharger and requires an annual visual inspection of the exhaust tailpipe v-band coupling (clamp).

The engine was sent to Continental Motors, Mobile, Alabama, where, on March 13, 2019, it was functionally tested under the oversight of an FAA inspector. The engine performed with no anomalies. According to Continental Motors, the v-band may have been loose enough to allow manual rotation of the turbo outlet collar. A hose used to connect the aftermarket intercooler was oil-soaked and did not appear to be freshly torn. If the hose failed in flight, manifold pressure would have immediately dropped and the "weird" sound could have been turbo discharge pressure escaping through the tear. When the engine lost turbo pressure, the fuel pump would have continued to operate with a much richer mixture, not sensing the loss of induction pressure to the engine. When the pilot turned on the auxiliary fuel pump, the engine would have been further flooded with excess fuel pressure.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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