CESSNA 152

Tehachapi, CA — November 20, 2017

Event Information

DateNovember 20, 2017
Event TypeACC
NTSB NumberWPR18FA035
Event ID20171120X25221
LocationTehachapi, CA
CountryUSA
Coordinates35.14278, -118.44111
AirportTehachapi Municipal
Highest InjuryFATL

Aircraft

MakeCESSNA
Model152
CategoryAIR
FAR Part091
Aircraft DamageDEST

Conditions

Light ConditionNDRK
WeatherVMC

Injuries

Fatal1
Serious0
Minor0
None0
Total Injured1

Event Location

Probable Cause

The pilot's loss of situational awareness shortly after takeoff over a sparsely lit area in dark night conditions, which resulted in a rapid descent to ground impact.

Full Narrative

HISTORY OF FLIGHTOn November 19, 2017, about 1756 Pacific standard time, a Cessna 152 airplane, N24987, was destroyed when it impacted terrain shortly after takeoff from Tehachapi Municipal Airport (TSP), Tehachapi, California. The private pilot received fatal injuries. The airplane was operated by Barnes Aviation as a Title 14 Code of Federal Regulations Part 91 personal flight. Night visual meteorological conditions prevailed, and no flight plan was filed for the flight. The flight was originating at the time of the accident; the pilot's intended destination was not determined.

The pilot had rented the airplane from Barnes Aviation, a fixed-base operator (FBO) located at General William J. Fox Airfield (WJF), Lancaster, California. According to a representative of the FBO, the airplane fuel tanks were filled, and then the airplane was flown about 1.4 hours before its pickup by the accident pilot. The airplane was not fueled after that flight, or after the flight to TSP.

According to a flight instructor who was employed by the FBO, the pilot had reserved the airplane for a few hours in the afternoon of the accident. About 1522, the flight instructor was asked by another FBO employee to pull the airplane out of a hangar for the pilot. The airplane had been removed from the hangar by about 1530, followed by the meeting of the pilot and that instructor for the first time. In response to the instructor's query, the pilot told the instructor that he planned to fly "to Rosamond then maybe up north for a little while." Rosamond Skypark Airport (L00), Rosamond, California, was located about 8 nautical miles north of WJF. About 1535, the pilot began his preflight inspection. About 1545, the pilot started the engine of the airplane, and the instructor saw the airplane take off from runway 6 about 1555. The instructor did not mention anything unusual or concerning about the pilot's actions. The pilot's route of flight, or whether he landed at any other airports between the time of his departure from WJF and his arrival at TSP, could not be determined.

TSP was located about 26 miles northwest of WJF. Surveillance imagery from three collocated cameras at TSP captured the airplane taxi into and stop in the transient parking area about 1628. The pilot secured the airplane and walked to a nearby restaurant to eat. He returned to the airplane about 1738, by which time night had fallen. The pilot started the engine about 1749 and taxied from the parking spot about 1 minute later. A set of lights presumed to be the accident airplane could be seen departing from TSP runway 29 about 1755. The surveillance imagery appeared to depict the airplane maneuvering in a manner consistent with a right traffic pattern after takeoff, followed by a rapid descent.

Multiple witnesses saw or heard the descent and/or impact and telephoned 911 to report the accident. A ground search aided by illumination from a law enforcement helicopter searchlight located the wreckage in a ranch pasture just north of TSP. The wreckage was examined on scene. A handheld Garmin GPS II Plus device was recovered on scene and was sent to the NTSB Recorders Laboratory for possible data download. Damage to the device precluded the recovery of any data. The airplane wreckage was then recovered to a secure storage facility for subsequent detailed examination. PERSONNEL INFORMATIONFederal Aviation Administration (FAA) records indicated that the pilot held a private pilot certificate with an airplane single-engine land rating. At the time of the accident, the pilot had logged a total flight experience of about 152 hours, including about 12 hours of night experience. His most recent flight review was completed in August 2017. On October 8, 2017, he had flown solo in the accident airplane from WJF to TSP and back at night and conducted 3-night landings. AIRCRAFT INFORMATIONFAA information indicated that the airplane was manufactured in 1977 and registered to the current owner in November 2011. The two-place, high-wing airplane was equipped with a Lycoming O-235 series engine. Maintenance records indicated that the airplane had accumulated a total time in service of about 11,168 hours and that the engine had accumulated a time since major overhaul of about 2,795 hours. The most recent annual inspection was completed in April 2017, and the most recent 100-hour inspection was completed in September 2017.

According to the airplane manufacturer's published performance data, the typical minimum flight endurance, not including a 45-minute reserve, is about 3 hours. Actual endurance can be increased significantly, primarily as a function of power setting, cruise altitude, and engine leaning procedures. Calculations that accounted for the estimated flight time of the airplane since its last known refueling indicated that the airplane likely had at least 1 hour and 45 minutes' worth of fuel on board at the time of the accident. METEOROLOGICAL INFORMATIONThe 1755 TSP automated weather observation included winds from 320° at 3 knots, visibility 10 miles, clear skies, temperature 7° C, dew point 0° C, and an altimeter setting of 30.13 inches of mercury.

Local sunset occurred at 1646, and civil twilight ended at 1713. The moon was a waxing crescent with 2% of its disc illuminated. Local moonset occurred at 1802. AIRPORT INFORMATIONFAA information indicated that the airplane was manufactured in 1977 and registered to the current owner in November 2011. The two-place, high-wing airplane was equipped with a Lycoming O-235 series engine. Maintenance records indicated that the airplane had accumulated a total time in service of about 11,168 hours and that the engine had accumulated a time since major overhaul of about 2,795 hours. The most recent annual inspection was completed in April 2017, and the most recent 100-hour inspection was completed in September 2017.

According to the airplane manufacturer's published performance data, the typical minimum flight endurance, not including a 45-minute reserve, is about 3 hours. Actual endurance can be increased significantly, primarily as a function of power setting, cruise altitude, and engine leaning procedures. Calculations that accounted for the estimated flight time of the airplane since its last known refueling indicated that the airplane likely had at least 1 hour and 45 minutes' worth of fuel on board at the time of the accident. WRECKAGE AND IMPACT INFORMATIONThe initial impact point was located about 350 ft west-northwest of, and offset about 2,050 ft north-northwest of, the runway 11 threshold. The accident site terrain was hard-packed, dry earth, flat and level, with mostly dried grass and some low, dried shrubs. All airplane components were accounted for at the accident site. No evidence consistent with in-flight fire or in-flight structural failure was observed.

Ground scars were consistent with the airplane impacting the terrain in a nose- and right-wing-low attitude. The right wingtip strike was the beginning of the ground scar. The earliest identifiable piece of wreckage was an outboard fragment of the right aileron. A ground scar consistent with the right main landing gear (RMLG) was located about 20 ft beyond the right wingtip strike. Scarring consistent with nose landing gear or propeller contact began about 10 ft beyond the RMLG strike. The ground scars and airplane damage were consistent with the wreckage tumbling and sliding before coming to rest.

The main wreckage consisted of the engine, wings, empennage, and most of the fuselage. The main wreckage came to rest about 250 ft, on a bearing of 138° true, from the initial impact point. Several items, including the propeller, some engine accessories, and some fuselage fragments, formed a debris field between the initial impact point and the main wreckage. The debris field orientation was within about 14° of the runway alignment. Several high-density items such as the battery and the alternator core came to rest several hundred feet beyond the main wreckage.

Both wings exhibited full-span, aft-direction crush damage along their leading edges.
Both lift struts remained attached to their respective wings but were separated from the fuselage. Both wings retained their respective fuel tank caps. Both flaps remained fully attached to their respective wings; the flaps were relatively undamaged and were found in positions consistent with being fully retracted at the time of impact. Both ailerons remained attached to their respective wings.

The vertical stabilizer with rudder and horizontal stabilizers with the elevators remained attached to the aft fuselage. The pitch trim tab remained attached to the right horizontal stabilizer.

All wing and empennage control surfaces retained their respective balance weights. Control continuity was established from both ailerons to the fuselage break in the cockpit. Control continuity was established from both elevators, the pitch trim tab, and the rudder to the fuselage break in the cockpit.

The cockpit/cabin was found torn open. The windshield was reduced to numerous smallfragments. Both cabin doors were completely fracture-separated from the airplane. The flap handle was found in the "Up/Retract" position. The elevator trim indicator and trim wheel were impact damaged. The trim actuator measurement indicated a 5º-tab-trailing-edge-up position. The control lock was found stowed in the back pocket of the right seat.

The primer, throttle, and mixture controls in the cockpit were found in their full forward positions; the throttle and mixture cables were continuous to the carburetor. The carburetor heat control was not identified in the wreckage. The fuel selector was found in the "ON" position. The master switch and all circuit breakers were absent from their receptacles.

The ignition switch was found in the "OFF" position with the key installed and bent to the left.

The engine remained partially attached to the engine mount and forward fuselage. The engine was relatively intact, but sustained impact damage in the aft and up directions. There was significant ductile bending of the exhaust system components. Several engine accessories or external components were fracture-separated from the engine. There was no evidence of abnormal external oil streaking observed on any of the airplane skins. No evidence of any pre-impact catastrophic failures was observed.

The vacuum pump remained securely attached to its mounting pad on the engine accessory face. The pump was removed and disassembled. The shear coupling, rotor, and vanes were all intact. The rotor rotated freely by hand, and all vanes moved freely in their slots. The artificial horizon was fracture-separated from its mount and was missing its face. The gyro rotor case was opened for examination and no internal scoring or other damage was observed.

The engine was separated from the attached wreckage for further examination. The top spark plugs were removed and examined; their appearance was consistent with normal operation. The crankshaft was rotated manually and freely in both directions. Thumb compressions was obtained in proper sequence on all four cylinders. Clean, uncontaminated oil was observed at all four rocker box areas. Mechanical continuity and proper operational sequence were established throughout the rotating group, valve train, and accessory section.

The combustion chamber of each cylinder was examined via borescope; all cylinders and valves exhibited normal operational signatures, and no damage was observed. No oil residue was observed in the exhaust system gas path. The oil displayed evidence of metal contamination.

Examination of the gascolator screen and the forward and aft strainers at each wing tank found no visible contaminants. The engine compartment fuel line was found to be in place and secure at its respective B nuts; however, the fitting at the carburetor inlet was fracture-separated, consistent with overload. The carburetor was undamaged and remained securely attached to the engine. Reliable positions of the mixture and throttle settings at the time of impact could not be determined.

No external fuel staining was observed on the carburetor. The carburetor was opened for examination. All internal locking tabs and safety devices of the carburetor were in place and properly secured. The fuel bowl was free of visible contaminants. The float assembly remained secure at the mounting and free of damage. The metal float pontoons exhibited no evidence of rubbing against the wall of the bowl. The right float exhibited slight hydraulic crushing on each side. The left float appeared normal.

The carburetor fuel inlet screen was found properly installed. The fuel inlet screen contained a loosely packed material consistent with lint that constituted approximately 50% of the screen internal volume. The material was submitted to the NTSB Materials Laboratory for identification. The material consisted of two different fibrous materials: one blue, and one reddish-brown in color. A spectrometer was used to collect and process infrared wavelength absorbance spectra of the material; the spectral results indicated that the material was most likely cellulose, which is found in natural plant fibers such as cotton. The material was foreign to the airplane fuel system, and it was not determined when or by what means the lint was introduced into the fuel system.

The left magneto was found securely clamped to its engine mounting pad. Magneto-to-engine timing could not be ascertained due to the destruction of the flywheel. The magneto produced spark at all four plug leads during hand rotation of the drive. The impulse coupler drive was intact and properly safetied.

The right magneto was fracture-separated from its engine mounting pad and impact-damaged. The fracture surface signatures at the magneto mounting flange were consistent with overload. The pieces of magneto flange that remained at the mounting pad were securely clamped. Magneto-to-engine timing could not be ascertained. The right magneto would not produce spark when hand-rotated at the drive due to impact damage. The impulse coupler drive was intact and properly safetied.

The single-piece, all-aluminum, two-bladed, fixed-pitch propeller was fracture-separated from the engine at the crankshaft flange. The fracture surfaces exhibited signatures consistent with overload due to rotation. The propeller blades displayed leading edge gouging, torsional twisting, chordwise striations across the cambered surfaces, and trailing edge "S" bending. The signatures were consistent with significant rotational energy being applied to the crankshaft at the time of impact. ADDITIONAL INFORMATIONTSP Surveillance Camera Imagery

Three surveillance cameras that captured the accident airplane were mounted atop a hangar located on the south-southwest side of the runway, adjacent to the transient parking ramp. The camera views included most of the transient ramp, the eastern side of the fuel pit, portions of the runway and its parallel taxiway, and portions of the highway and non-airport property north-northwest of the airport. All three camera channels were recorded as continuous motion imagery. Captured imagery included the arrival of the airplane at the transient parking area, some of the pilot's post- and pre-flight activities, and portions of the taxi-out and accident flight.

After the airplane taxied from the transient parking ramp, the night conditions, airplane distance from the cameras, and camera resolution caused the airplane image to be reduced to a set of whitish lights. The airplane appeared to taxi for the departure runway via the parallel taxiway, and calculations based on time and airplane position indicated that the taxi speed ranged between 11 and 14 knots. The pilot spent about 3 to 4 minutes near the approach end of runway 29 before beginning his takeoff roll. The airplane traversed about 1,300 ft in about 14 seconds during its late takeoff roll, liftoff, and initial climb, yielding an average calculated speed about 54 knots. Another camera captured the airplane in its initial climb; calculations indicated that the climb speed was about 81 knots.

Two of the cameras captured the airplane maneuvering in a manner consistent with it flying the right crosswind and right downwind traffic pattern legs. A few seconds after it appeared to have entered the downwind leg, the airplane descended rapidly toward the ground, and then disappeared from view. The descent took about 7 seconds, and the descent path was depressed about 30° below horizontal in the camera image frames. None of the captured imagery depicted any flashes consistent with a ground impact explosion or any postimpact fire. The image quality precluded any determination of airplane attitude, altitude, distance from the cameras, or specific heading.

Spatial Disorientation & Situational Awareness

According to the FAA publication Pilot's Handbook of Aeronautical Knowledge (PHAK, FAA-H-8083-25):

Spatial disorientation specifically refers to the lack of orientation with regard to the position, attitude, or movement of the airplane in space…. During flight in visual meteorological conditions (VMC), the eyes are the major orientation source and usually prevail over false sensations from other sensory systems. When these visual cues are taken away… false sensations can cause a pilot to quickly become disoriented.

The handbook then stated that "Prevention is usually the best remedy for spatial disorientation. Unless a pilot has many hours of training in instrument flight, flight in reduced visibility or at night when the horizon is not visible should be avoided."

The handbook defined situational awareness as the "accurate perception of the operational and environmental factors that affect the airplane, pilot, and passengers during a specific period of time." The handbook stated that a situationally aware pilot "has an overview of the total operation and is not fixated on one perceived significant factor." The handbook stated that "some of the elements inside the airplane to be considered are the status of airplane systems," and cautioned that "an awareness of the environmental conditions of the flight, such as spatial orientation of the airplane, and its relationship to terrain… and airspace must be maintained." MEDICAL AND PATHOLOGICAL INFORMATIONThe Kern County, Bakersfield, California, Sheriff-Coroner's Office autopsy report indicated that the cause of death was "blunt injuries," and that there were "no signs of natural disease such as to qualify as clues to a cause of the accident."

FAA medical records indicated that the pilot had failed the color vision test on the four medical certificate applications that were on file. His FAA medical examiner(s) did not identify any significant adverse conditions, and his most recent third-class FAA medical certificate was issued in April 2016.

Toxicology testing of the pilot's tissue samples at the FAA Forensic Sciences Laboratory was negative for carbon monoxide and ethanol. Ranitidine was detected in urine and blood samples. This medication is used to treat intestinal ulcers, gastroesophageal reflux disease, heartburn associated with acid indigestion, and other conditions where the stomach produces too much acid. The FAA has no limitations on its use by pilots.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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