CESSNA 150L

Summerville, SC — June 13, 2008

Event Information

DateJune 13, 2008
Event TypeACC
NTSB NumberCHI08LA162
Event ID20081004X12023
LocationSummerville, SC
CountryUSA
Coordinates33.04937, -80.18963
AirportSUMMERVILLE AIRPORT
Highest InjuryNONE

Aircraft

MakeCESSNA
Model150L
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None1
Total Injured0

Event Location

Probable Cause

A total loss of engine power for undetermined reasons.

Full Narrative

On June 13, 2008, approximately 1930 eastern daylight time, a Cessna 150; N5471Q, operated and piloted by a commercial pilot crashed shortly after takeoff from Summerville Airport, Summerville, South Carolina. Visual meteorological conditions prevailed at the time of the accident and the flight was was being conducted as a ferry flight under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The pilot, the only occupant, was not injured during the accident. The local flight was originating for the purpose of ferrying the aircraft about 25 miles to Mt Pleasant Regional Airport-Faison Field (KLRO).

The pilot said the engine originally started without hesitation and he taxied to runway 24 for takeoff. Upon reaching the runway, the run up indicated there was a fouled plug in the engine. Several minutes were spent clearing up the fouled plug and the pilot proceeded to takeoff. He reported he had 2475 rpm on takeoff, but, passing though about 60 feet above the ground after takeoff, the engine suddenly stopped producing power. Manipulating the throttle caused a momentary return of power, but, the engine stopped again so the pilot made a forced landing straight ahead.

A Federal Aviation Inspector inspected the engine and found the magnetos would spark and there was compression in all cylinders. The inspector also disassembled the carburetor and found no anomalies with the carburetor.

The pilot submitted a written statement but not an aircraft accident report.

The airplane and engine both had current annual inspections. The engine had 1800 hours since major overhaul.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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