MAHER DANIEL J VELOCITY

Worcester, MA — April 30, 2016

Event Information

DateApril 30, 2016
Event TypeACC
NTSB NumberERA16LA177
Event ID20160504X63038
LocationWorcester, MA
CountryUSA
Coordinates42.26722, -71.87556
AirportWORCESTER RGNL
Highest InjuryNONE

Aircraft

MakeMAHER DANIEL J
ModelVELOCITY
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None2
Total Injured0

Probable Cause

The overstress failure of the nose landing gear fork assembly.

Full Narrative

On April 30, 2016, about 1556 eastern daylight time, an experimental amateur-built Velocity SEFG, N7044Q, was substantially damaged during landing at Worcester Regional Airport (ORH), Worcester, Massachusetts. The airline transport pilot and passenger were not injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local personal flight conducted under the provisions of 14 Code of Federal Regulations Part 91

According to the pilot, immediately after nose wheel contact upon landing, the nose wheel fork separated from the nose wheel landing gear strut, and the airplane began skidding on the bottom of the nose landing gear strut. After the separation of the nosewheel fork, the pilot applied held backpressure on the control stick, which resulted in a propeller strike.

The pilot stated that he had purchased the airplane in November 2015. There were no preflight anomalies noted before the local area flight, and no mechanical or performance deficiencies before the final full-stop landing. There was no record of any maintenance done on the nose landing gear fork.

Examination of photographs revealed the airplane rested on the nose landing gear strut with the nose wheel and its mounting fork separated. The nose wheel remained in the fork and the nose gear fork was fractured at the gear mount attach point. The propeller tips were damaged, and parallel slash marks consistent with a propeller strike were visible on the runway surface prior to where the airplane came to rest. The composite airframe structure at the nose landing gear strut attach point had also fractured, and had punctured the cockpit footwell, which resulted in substantial damage to the airframe.

Further examination of the nose landing gear fork revealed it fractured from overstress. The manufacturer stated that this part and design had been modified twice because of similar fractures, as it had been discovered that excessive nose landing gear shimmying would result in overstress fractures. The first redesign included a dampener consisting of bellville washers to reduce stress on the nose fork. The next iteration included a hydraulic dampener. In addition to changing the design of the nose fork, the new parts were made of a different material.

The accident airplane did not have either modification installed , and was the original nose fork installed on the airplane.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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