CESSNA 421

Foley, AL — April 26, 2016

Event Information

DateApril 26, 2016
Event TypeACC
NTSB NumberERA16LA171
Event ID20160427X81659
LocationFoley, AL
CountryUSA
Coordinates30.41639, -87.70028
AirportFoley Municipal Airport
Highest InjuryMINR

Aircraft

MakeCESSNA
Model421
CategoryAIR
FAR Part091
Aircraft DamageDEST

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor1
None0
Total Injured1

Event Location

Probable Cause

The pilot's failure to obtain proper takeoff speed before breaking ground, which resulted in the airplane’s failure to gain altitude and a collision with trees and terrain.

Full Narrative

On April 26, 2016, at 1424 central daylight time, a Cessna 421B, N3372Q, was destroyed when it impacted trees and terrain in Foley, Alabama. The private pilot sustained minor injuries. Visual meteorological conditions prevailed, and no flight plan had been filed for the flight from Foley Municipal Airport (5R4), Foley, Alabama, to West Georgia Regional Airport (CTJ), Carrollton, Georgia. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.

During a postaccident interview with a Federal Aviation Administration Inspector, the pilot recounted that he taxied out and lined up for takeoff on the runway. With brakes on, he cycled the propellers and they "checked good." The magneto check at 1,500 rpm was also "good," as were the oil pressure and oil temperature. The pilot then ensured that the fuel selectors were position to both main fuel tanks, the throttles were full, mixtures were all the way forward, the fuel boost pumps were on low, and the propellers were all the way forward. He selected the flaps to the takeoff position and released the brakes.

During the takeoff roll, everything was "normal" (temperatures and pressures were "in the green"), and when the airplane had accelerated to 75-80 knots, the pilot pulled back on the yoke slowly, and the airplane began to climb. The pilot raised the landing gear and noticed that the airplane wasn't climbing. He looked at the airspeed indicator, which indicated 80 knots. The pilot heard the stall warning and pulled back on the yoke. He then shut the boost pumps off and lowered the flaps before a hard impact.

After impact, the pilot found himself upside down. He released his seat belt, saw fire and went to the back of the airplane. He opened the aft hatch and rolled forward, landing flat on his back. Two men then helped him up and led him to a nearby building. When asked about the performance of the airplane's engines the pilot stated, "the engines were operating fine and I screwed up."
Review of the normal takeoff checklist for the airplane revealed that the minimum control speed was 86 knots, and the break ground and climb out speed was 106 knots.

A witness stated that during the takeoff from runway 18, the airplane left the ground at the departure runway end, just clearing the airport's perimeter fence. The airplane was unable to gain sufficient altitude to clear the trees less than ¼ of a mile south of the runway. The airplane began hitting tree tops, and impacted a large oak tree with the left wing, then spun into two other large oak trees 30 feet to the southwest. The airplane then flipped over, hit the ground, exploded and was consumed by fire. The pilot jumped from the rear entry door and landed on his back. The pilot refused medical attention and sustained burns and a cut to his left hand.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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