PIPER PA 30

Othello, WA — July 17, 2014

Event Information

DateJuly 17, 2014
Event TypeACC
NTSB NumberWPR14LA298
Event ID20140718X52044
LocationOthello, WA
CountryUSA
Coordinates47.31667, -119.13333
AirportOthello Municipal
Highest InjuryNONE

Aircraft

MakePIPER
ModelPA 30
CategoryAIR
FAR Part091
Aircraft DamageSUBS

Conditions

Light ConditionDAYL
WeatherVMC

Injuries

Fatal0
Serious0
Minor0
None4
Total Injured0

Event Location

Probable Cause

The partial loss of engine power for reasons that could not be determined based on the available information.

Full Narrative

On July 17, about 1515 Pacific daylight time, a Piper PA-30 twin-engine airplane, N7981Y, was substantially damaged following a partial loss of power on the left engine, and a collision with terrain during takeoff/initial climb at the Othello Municipal Airport, Othello, Washington. The private pilot and the three passengers were not injured. The airplane was registered to Warden Air, LLC and operated by the pilot as a Title 14 Code of Federal Regulations Part 91 personal flight. An instrument flight rules (IFR) flight plan was filed for the cross-country flight. The airplane was departing at the time and was destined for Klamath Falls, Oregon.

The pilot reported that during the power up for takeoff, the left engine revolutions per minute (RPM) was 2,200 while the right engine was 2,600 RPM. He leaned the mixture on the left engine to bring the RPM up to 2,600 and proceeded with the takeoff. After the takeoff roll he initiated a climb and noted that the exhaust gas temperature (EGT) on the left engine was much higher than the EGT of the right engine. The left engine RPM suddenly dropped to 2,000 RPM and the airplane yawed to the left and started to descend. The pilot was unable to overcome the yaw and descent, and the airplane impacted the ground.

The pilot reported that he should not have leaned the left engine for takeoff.

A review of the left engine's logbook revealed a logbook entry dated March 21, 2014 indicating that the fuel flow divider had been removed, repaired, and reinstalled. The fuel servo and turbo charger had also been removed, repaired, and reinstalled. The entry also noted that a flow test was performed, the engine was run tested and checked for leaks, and returned to service. The pilot did not provide the time the airplane had flown since the maintenance work was completed.

The NTSB did not respond to the accident site and the wreckage was retained by the insurance company. Prior to examination, the wreckage and engines were sold for salvage and no longer available for examination.

About This NTSB Record

This aviation event was investigated by the National Transportation Safety Board (NTSB). NTSB investigates all U.S. civil aviation accidents to determine probable cause and issue safety recommendations to prevent future accidents.

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