ENERGY TRANSFER COMPANY

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENERGY TRANSFER COMPANY
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates32.09031, -101.88090

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON MAY 5TH, 2016, AT APPROXIMATELY 16:00 HRS ENERGY TRANSFER LIQUID CONTROL CONTACTED COMPANY FIELD PERSONNEL REQUESTING ASSISTANCE AT THE BADEN FACILITY, DUE TO INCREASING PRESSURES. AT 16:10 HRS, ENERGY TRANSFER EMPLOYEE, ON LOCATION AT BADEN FACILITY, HEARD A RELIEF VALVE ACTIVATE ON A 10"" STATIONARY METER PROVER. THE EMPLOYEE NOTIFIED LIQUID CONTROL THAT BADEN WAS BEING OVER PRESSURED AND TO REROUTE INCOMING PRODUCT. AT 16:16 HRS, THE FLANGE GASKET FAILED ON THE 10"" STATIONARY METER PROVER, RESULTING IN A RELEASE OF PRODUCT. LIQUID CONTROL WAS NOTIFIED TO SHUT DOWN BADEN FACILITY. THE 10"" STATIONARY METER PROVER LOOP WAS SHUT DOWN AND ISOLATED, THE GASKET WAS REPLACED AND THE FACILITY WAS RETURNED TO SERVICE AT 22:40 HRS. THE PRODUCT RELEASED WAS ESTIMATED AT 63 BBLS. THIS FACILITY IS UNDER JURISDICTION OF THE TEXAS RAILROAD COMMISSION AND WERE TELEPHONICALLY NOTIFIED OF THE RELEASE UNDER REPORT NUMBER 1348. PRELIMINARY INVESTIGATIONS HAVE REVEALED THAT A THIRD PARTY DELIVERY HAD INADVERTENTLY INCREASED FLOW, INTO THE BADEN FACILITY, AND STATION EQUIPMENT WAS UNABLE TO REACT QUICK ENOUGH TO PREVENT THE OVER PRESSURING. THE INLET PIPING WAS MODIFIED ON MAY 21, 2016 SO THAT THERE IS ADEQUATE PROTECTION AND REOCCURRENCE IS NOT POSSIBLE. UPDATE 11/29/2016 NO UPDATES TO BE MADE. NOTE AS FINAL REPORT.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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