ENBRIDGE ENERGY, LIMITED PARTNERSHIP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENBRIDGE ENERGY, LIMITED PARTNERSHIP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.55349, -87.88525

Cause

CauseNATURAL FORCE DAMAGE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JULY 13, 2017 AT 10:51 AM, ENBRIDGE LOCAL STATION TECHNICIAN NOTICED OIL SHEEN ON STANDING WATER IN THE GRAVELED AREA NEAR LINE 14 TRAP AND PCV AREA AT THE MOKENA STATION. STATION TECHNICIAN CALLED THE EDMONTON CONTROL CENTER AND LINE 14 WAS IMMEDIATELY SHUT DOWN AND THE STATION WAS ISOLATED. CONTRACT RESOURCES AND ENBRIDGE PIPELINE MAINTENANCE CREWS RESPONDED AND DISCOVERED THE SOURCE TO BE A SMALL DIAMETER THREADED CONNECTION - VALVE PACKING AND GREASE FITTING ON THE BURIED PORTION OF VALVE 461.17-14/6-XV. THE MAJORITY OF THE 67 GALLONS RELEASED REMAINED ON SITE; HOWEVER, APPROXIMATELY 1.47 GALLONS MADE IT THROUGH THE OUTFLOW OF CONTAINMENT POND AND OFF SITE. THE SMALL DIAMETER THREADED FITTING AND PIPING THAT WAS LEAKING WAS REMOVED AND A THREADED PLUG WAS INSTALLED. THE REPAIRS WILL BE COMPLETED THROUGH AN OUTAGE REQUEST. THE CAUSE OF THE RELEASE HAS BEEN DETERMINED TO BE DUE TO FROST HEAVE. APPROXIMATELY 195 TONS OF CONTAMINATED SOIL AND VEGETATION WAS DISPOSED OF AT AN APPROVED SITE. THE CRUDE OIL THAT LEFT THE SITE WAS CLEANED UP THROUGH REMOVAL OF VEGETATION AND ABSORBING THE RESIDUAL WITH ABSORBENT PADS.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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