ONEOK NGL PIPELINE, LLC
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | ONEOK NGL PIPELINE, LLC |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 32.40217, -102.69515 |
Cause
| Cause | INCORRECT OPERATION |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
AT APPROXIMATELY 12:10 ON 2/26/2018, THE ONEOK PIPELINE CONTROL CENTER RECEIVED A CALL FROM A DCP EMPLOYEE AT THE DCP ANDREWS METER STATION CONNECTION, ADVISING OF VAPOR RELEASE ON ONEOK'S METER PIPING. THIS CONNECTION IS NOT ACTIVE AT THIS TIME. ONEOK FIELD EMPLOYEES RESPONDING TO THE CALL DETERMINED THE LEAK ORIGINATED BETWEEN TWO FLANGES WHERE A FLEXITALLIC GASKET AND A FIBER INSULATOR GASKET HAD BEEN IMPROPERLY INSTALLED TOGETHER. THE INSULATOR GASKET HAD FAILED AND WAS THE CAUSE OF THE LEAK. THE PIPING WAS ISOLATED AND DE-PRESSURED. THE FLEXITALLIC GASKET WAS REMOVED AND A NEW INSULATOR GASKET INSTALLED BETWEEN THE FLANGES AND RETURNED TO NORMAL OPERATIONS. ONEOK'S INVESTIGATION DETERMINED THE GASKETS HAD BEEN IMPROPERLY INSTALLED IN 2012 BY THE PREVIOUS OPERATOR OF THE ASSET.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.