ENBRIDGE ENERGY, LIMITED PARTNERSHIP

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENBRIDGE ENERGY, LIMITED PARTNERSHIP
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates41.55449, -87.88651

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JANUARY 2, 2019 AT APPROXIMATELY 1135 CST, THE GRIFFITH AREA ELECTRICAL TECHNICIAN WAS PERFORMING ROUNDS AT MOKENA STATION AND DISCOVERED A CRUDE OIL RELEASE OF APPROXIMATELY 24.5 GALLONS FROM THE STATION INJECTION BOOSTER PUMP. THE PUMP WAS ISOLATED AND GRIFFITH PIPELINE MAINTENANCE PERSONNEL WERE ON SITE TO PERFORM CLEANUP OF THE AFFECTED AREA. THE PRODUCT WAS CONTAINED TO THE IMMEDIATE AREA OF THE BOOSTER AND MANIFOLD PIPING. DUE TO THE ANTICIPATED COST OF THE CLEANUP, THE NRC WAS NOTIFIED AT 1238 CST (NRC #1234389). THE CAUSE OF THE RELEASE WAS DUE TO GASKET FAILURE. FAILED GASKET WAS REPLACED. APPROXIMATELY 9.61 TONS OF CONTAMINATED SOIL HAVE BEEN PROPERLY DISPOSED OF AT AN APPROVED LANDFILL.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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