ONEOK NGL PIPELINE, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorONEOK NGL PIPELINE, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.05151, -95.24527

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JUNE 30TH, 2020 AT APPROXIMATELY 8:28 PM, ONEOK PIPELINE CONTROL CENTER RECEIVED A GAS DETECT ALARM FOR THE ONEOK STERLING II GROVETON PUMP STATION. THE GAS DETECT ALARM ACTIVATED THE STATION SHUTDOWN AND ISOLATED THE PUMP STATION. ONEOK PIPELINE CONTROL DISPATCHED LOCAL FIELD OPERATIONS TO THE LOCATION. AT APPROXIMATELY 9:15PM, THE ONEOK FIELD OPERATOR ARRIVED ON SITE AND NOTICED VAPORS IN THE VICINITY OF THE NUMBER 1 PUMP. FIELD OPERATOR ISOLATED THE PUMP AND BEGAN EVACUATING HYDROCARBONS FROM THE PUMP AND ASSOCIATED PIPING AT 9:25PM. AFTER EVACUATION OF HYDROCARBONS, A PINHOLE LEAK IN THE OUTBOARD BEARING COOLER RETURN TUBING WAS DISCOVERED AS THE SOURCE OF THE RELEASE. THE AFFECTED TUBING WAS FOUND TO BE IN CONTACT WITH THE OUTBOARD OIL DRAIN PIPING, RESULTING IN A PINHOLE DEVELOPING IN THE TUBING, BECAUSE OF FRICTION. THE TUBING WAS REPLACED AND ADJUSTED SO NOT TO CONTACT THE OIL DRAIN PIPING AND THE PUMP RETURNED TO SERVICE. INVESTIGATION INTO THE CAUSE OF THE RELEASE, DETERMINED THE PUMP OIL DRAIN PIPING HAD INADVERTENTLY BEEN INSTALLED IN CONTACT WITH THE COOLER INLET TUBING DURING PREVIOUS MAINTENANCE ACTIVITIES.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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