ONEOK NGL PIPELINE, LLC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorONEOK NGL PIPELINE, LLC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates38.36916, -97.83204

Cause

CauseINCORRECT OPERATION
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

THE 11313 PIPELINE REACHED 109% OF MOP (787 PSI VERSUS 720 MOP) DURING A PIPELINE START-UP RESULTING IN A PRESSURE RELIEF VALVE AT THE 313 JUNCTION RELIEVING TO ATMOSPHERE. THE PRESSURE EVENT WAS THE RESULT OF ONEOK PIPELINE CONTROL OPENING THE 313 PIPELINE'S INLET VALVE (V26) IN ERROR WITH AN UPSTREAM PRESSURE EXCEEDING THAT SPECIFIED IN THE OPERATING PROCEDURE. IN ADDITION, VALVE V26 DID NOT RE-CLOSE QUICKLY ENOUGH, UPON DETECTING HIGH PRESSURE, TO STOP THE PRESSURE INCREASE PRIOR TO THE RELIEF VALVE ACTIVATING. IN IMMEDIATE RESPONSE TO THE EVENT, THE SCADA SCREEN HAS BEEN UPDATED TO PROVIDE ADDITIONAL CLARITY. ADDITIONALLY, A PROJECT IS UNDERWAY TO RELOCATE V26'S PRESSURE SWITCH TO THE UPSTREAM SIDE OF THE VALVE THUS PREVENTING THE VALVE FROM OPENING UNDER THIS SCENARIO.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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