SUNOCO PIPELINE L.P.

hazardous_liquid Incident —

Incident Information

Report Date
OperatorSUNOCO PIPELINE L.P.
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.97056, -102.02884

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JULY 21, 2021 AT APPROXIMATELY 12:00PM, A CRUDE OIL SPILL OCCURRED AT THE CRAWFORD STATION SOUTH OF MIDLAND. AT 1:00PM, COMPANY PERSONNEL DROVE UP TO THE FACILITY AND CONFIRMED A CRUDE OIL SPILL FROM A RELIEF VALVE ON THE 10INCH PIONEER CRAWFORD 38H-7JH, CALLED OPERATIONS AND SHUT THE FACILITY DOWN. COMPANY RESOURCES ARRIVED AT THE FACILITY AND CLOSED VALVE BA601 UPSTREAM OF THE LEAK AND VALVE BA603 DOWNSTREAM OF THE LEAK TO ISOLATE THE SPILL POINT. IT WAS DETERMINED THAT THE RELEASE MEET THE REPORTING CRITERIA AND A CALL WAS PLACED TO THE TX RRC ON 7/21/21 AT 1:43PM (RRC INCIDENT # 2453). A THIRD PARTY WAS CALLED TO CLEAN UP ALL FREE PRODUCT AND REMEDIATE THE SOIL. THE CAUSE OF THE LEAK WAS DUE TO A CRACK IN THE THREADS OF A 2INCH FITTING ON THE RELIEF VALVE BLEAD RING. THE CRACK WAS DUE TO EXCESSIVE VIBRATION. A NEW FITTING WAS INSTALLED AND BRACING WAS PUT IN PLACE TO MINIMIZE VIBRATIONS AND TO PREVENT FURTHER LEAKS. AT APPROXIMATELY 3:00PM THE FACILITY WAS RESTARTED. AN INCREASE OF PATROLS WILL BE CONDUCTED AT THE FACILITY TO MONITOR NEW FITTING THAT WAS INSTALLED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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