ENERGY TRANSFER COMPANY

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENERGY TRANSFER COMPANY
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.71437, -102.73573

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON APRIL 6TH AT APPROXIMATELY 15:00, A PIPELINE TECHNICIAN WAS PERFORMING ROUTINE SITE INSPECTION AND NOTED A RELEASE COMING FROM THE VALVE BODY DRAIN PORT ON 12-INCH MAINLINE VALVE #1. THE CONTROL CENTER WAS IMMEDIATELY NOTIFIED AND SUBSEQUENTLY SHUT DOWN THE UPSTREAM PUMP AT BROOKE STATION AND CLOSED MLV #1 WHICH STOPPED THE RELEASE. APPROXIMATELY 29 GALLONS OF CRUDE WAS RELEASED TO THE GROUND INSIDE THE VALVE SITE AREA. ALL FREE PRODUCT WAS RECOVERED AND CONTAMINATED SOIL REMOVED. UPON INVESTIGATION IT WAS DETERMINED THAT THE VALVE BODY BLEED PORT SEAL HAD FAILED DUE TO DEBRIS IN THE SEAL. THE DRAIN PORT WAS REPLACED WITH A PIPE NIPPLE AND A VALVE. THE VALVE IS PLUGGED WHEN NOT IN USE. SIMILAR APPURTENANCES ARE BEING INSPECTED AND REPLACED AS NEEDED.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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