COLONIAL PIPELINE CO

hazardous_liquid Incident —

Incident Information

Report Date
OperatorCOLONIAL PIPELINE CO
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates36.67822, -79.39588

Cause

CauseEQUIPMENT FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON JANUARY 03, 2023, A COLONIAL EMPLOYEE WAS PERFORMING A ROUTINE STATION CHECK AT THE WITT BOOSTER STATION IN DANVILLE, VIRGINIA. DURING THIS CHECK THE EMPLOYEE OBSERVED NOTICEABLE SHEEN ON THE FACILITY RETENTION POND. UPON FURTHER INVESTIGATION, DISTRESSED VEGETATION WAS DISCOVERED BETWEEN THE LINE 03 DOWNSTREAM ISOLATION VALVE AND THE POND. IMMEDIATE NOTIFICATIONS WERE MADE TO THE ALPHARETTA CONTROL CENTER AND APPROPRIATE PERSONNEL. AT THE TIME OF THE INCIDENT DISCOVERY, LINE 03 WAS NOT OPERATING IN ORDER TO ACCOMMODATE MAINTENANCE AT GREENSBORO JUNCTION. CONFIRMED DISCOVERY OCCURRED AT 12:30 AND THE NRC NOTIFICATION WAS MADE AT 13:21. EMERGENCY RESPONSE NOTIFICATIONS WERE MADE, AND RESOURCES WERE MOBILIZED. AN INCIDENT COMMAND POST WAS ESTABLISHED TO SUPPORT THE RESPONSE. THE INITIAL INVESTIGATION HAS IDENTIFIED AN O-RING FAILURE, RESULTING IN THE LEAK. FOLLOWING THE REPAIR OF THE VALVE, LINE 03 WAS RETURNED TO NORMAL OPERATIONS ON JANUARY 8, 2023, AT 17:51. A COMPREHENSIVE INCIDENT ANALYSIS IS CURRENTLY BEING CONDUCTED. UPDATE: AN ACCIDENT INVESTIGATION DETERMINED THAT THE APPARENT CAUSE OF THE RELEASE WAS DUE TO THE COMPRESSION OF THE BONNET O-RING OVER ITS SERVICE LIFE, AND THE CONTRIBUTING FACTOR WAS IDENTIFIED AS NO PREVENTATIVE MAINTENANCE PLAN EXISTED FOR REPLACING SOFT GOODS IN GATE VALVE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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