COLONIAL PIPELINE CO
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | COLONIAL PIPELINE CO |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 29.85847, -94.97918 |
Cause
| Cause | EQUIPMENT FAILURE |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON 5/4/2023, AT OR AROUND 13:38 A TECHNICIAN PERFORMING WEEKLY MAIN LINE BLOCK VALVE (MLBV) INSPECTIONS OBSERVED PRODUCT IN AN ACCESS WELL LOCATED NEXT TO THE CEDAR BAYOU UNIT (CBU) LINE 1 MLBV. THIS SEGMENT OF LINE WAS DOWN DUE TO SCHEDULE DOWNSTREAM OPERATIONS. THE APPROPRIATE NOTIFICATIONS WERE MADE IN ACCORDANCE WITH PROCEDURE. ADDITIONAL PERSONNEL WERE MOBILIZED AND ARRIVED AT APPROXIMATELY 16:18 TO FURTHER INVESTIGATE, REPAIR AND PERFORM SPILL RECOVERY ACTIONS. THE BONNET O-RING WAS FOUND TO BE THE SOURCE OF THE LEAK. FURTHER INVESTIGATION NOTED THE O-RING FAILED AS A RESULT OF WEAR AND TEAR AND HAD BECOME COMPRESSED OVER TIME. AS A RESULT OF THE RELEASE, 3 GALLONS OF PRODUCT WAS RELEASED AND RECOVERED. ALL RELEASED PRODUCT WAS CONTAINED ON CPC PROPERTY. REPAIRS WERE COMPLETED AND THE LINE RETURNED TO NORMAL OPERATIONAL STATUS ON 5/8/2023 AT 13:54. ON 5/4/2023, AT OR AROUND 13:38 A TECHNICIAN PERFORMING WEEKLY MAIN LINE BLOCK VALVE (MLBV) INSPECTIONS OBSERVED PRODUCT IN AN ACCESS WELL LOCATED NEXT TO THE CEDAR BAYOU UNIT (CBU) LINE 1 MLBV. THIS SEGMENT OF LINE WAS DOWN DUE TO SCHEDULE DOWNSTREAM OPERATIONS. THE APPROPRIATE NOTIFICATIONS WERE MADE IN ACCORDANCE WITH PROCEDURE. ADDITIONAL PERSONNEL WERE MOBILIZED AND ARRIVED AT APPROXIMATELY 16:18 TO FURTHER INVESTIGATE, REPAIR AND PERFORM SPILL RECOVERY ACTIONS. THE BONNET O-RING WAS FOUND TO BE THE SOURCE OF THE LEAK. FURTHER INVESTIGATION NOTED THE O-RING FAILED AS A RESULT OF WEAR AND TEAR AND HAD BECOME COMPRESSED OVER TIME. AS A RESULT OF THE RELEASE, 3 GALLONS OF PRODUCT WAS RELEASED AND RECOVERED. ALL RELEASED PRODUCT WAS CONTAINED ON CPC PROPERTY. REPAIRS WERE COMPLETED AND THE LINE RETURNED TO NORMAL OPERATIONAL STATUS ON 5/8/2023 AT 13:54. ON 5/4/2023 AT 17:00 IT WAS DISCOVERED THE RELEASE WOULD MEET OR EXCEED $50,000, THUS, A NRC NOTIFICATION WAS MADE.
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.