NOBLE ENERGY INC

hazardous_liquid Incident —

Incident Information

Report Date
OperatorNOBLE ENERGY INC
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates31.37889, -103.55440

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

COMPANY EMPLOYEE ARRIVED ON SITE AS PART OF ROUTINE DUTIES AND OBSERVED LEAK ON ABOVE GROUND PIPING. EMPLOYEE THEN PROCEEDED TO ISOLATE THE AFFECTED PIPING AND NOTIFIED PRODUCTION SUPERVISOR OF SITUATION. SPILL CALCULATION WAS PERFORMED AND ESTIMATED AT 1.35 BBLS OF CRUDE OIL. NOTIFICATION WAS MADE TO TEXAS RAILROAD COMMISSION BY PRODUCTION SUPERVISOR AND DETERMINATION MADE THAT NO EMERGENCY RESPONSE OR OSRO RESOURCES NEEDED AS RELEASE WAS CONTAINED TO COMPANY OWNED/CONTROLLED PROPERTY AND NO FURTHER DANGER TO PUBLIC OR ENVIRONMENT EXISTED. PIPING WAS EVACUATED AND DISASSEMBLED AS PART OF INVESTIGATION. PINHOLE DUE TO CORROSION WAS OBSERVED IN PIPE AND SENT OFF FOR METALLURGICAL EVALUATION, BUT FIELD EXAMINATION BY COMPANY SME'S INDICATES CORROSION DUE TO MIC. REMEDIATION OF SOIL IS ONGOING AT THE SITE, TEMPORARY SPOOL INSTALLED IN AFFECTED PIPING, AND SYSTEM WAS RESTARTED. PLAN FOR PERMANENT REPAIR IS REPLACEMENT WITH INTERNALLY COATED SPOOL PIECE.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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