MAGELLAN TERMINALS HOLDINGS, LP
hazardous_liquid Incident —
Incident Information
| Report Date | — |
| Operator | MAGELLAN TERMINALS HOLDINGS, LP |
| Commodity | — |
| Pipeline Type | hazardous_liquid |
Location
| State | |
| Coordinates | 35.94553, -96.74869 |
Cause
| Cause | INCORRECT OPERATION |
| Subcause | — |
Casualties
| Fatalities | 0 |
| Injuries | 0 |
Costs
| Property Damage | — |
| Lost Commodity | — |
| Public/Private Damage | — |
| Emergency Response | — |
| Environmental Remediation | — |
| Other Costs | — |
Location Map
Incident Narrative
ON JULY 4, 2024, AT APPROXIMATELY 09:45 A THIRD-PARTY DRIVING PAST THE SOUTH SIDE OF THE CENTRAL CUSHING CRUDE TERMINAL ONSERVED PRODUCT LEAKING FROM AN ABOVE GROUND VALVE SETTING. THE THIRD-PARTYNOTIFIED PERSONNEL AT THE FACILITY. A TECHNICIAN INVESTIGATED AND FOUND PRODUCT LEAKING FROM THE DOWNSTREAM FLANGE OF MOV 105 ON THE CENTRAL CUSHING - BP #1-16"" PIPELINE. THE PIPELINE WAS IMMEDIATELY SHUTDOWN, THE AFFECTED SEGMENT WAS ISOLATED, AND CLEAN-UP ACTIVITIES WERE INITIATED. FURTHER INVESTIGATION DETERMINED THAT A GASKET HAD FAILED. UPON REMOVAL AND INSPECTION OF THE FAILED GASKET, IT WAS DETERMINED THAT IN 2022 A CONTRACTOR SELECTED AND INSTALLED AN ANSI 150 GASKET WHERE AN ANSI 300 GASKET WAS DESIGNED TO BE. TO PREVENT A REOCCURRENCE, THE GASKET WAS REPLACED WITH AN ANSI 300 GASKET. ADDITIONALLY, SIMILARLY SITUATED GASKETS AND OTHER WORK SITES OF THE CONTRACTOR WERE INSPECTED AND ALL WERE FOUND TO BE APPROPRIATELY RATED. SUPPLEMENTAL/FINAL (10/2024): PARTS A AND H
About This Pipeline Incident
Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.