ENERGY TRANSFER COMPANY

hazardous_liquid Incident —

Incident Information

Report Date
OperatorENERGY TRANSFER COMPANY
Commodity—
Pipeline Typehazardous_liquid

Location

State
Coordinates30.14072, -94.39894

Cause

CauseCORROSION FAILURE
Subcause—

Casualties

Fatalities0
Injuries0

Costs

Property Damage
Lost Commodity
Public/Private Damage
Emergency Response
Environmental Remediation
Other Costs

Location Map

Incident Narrative

ON 10/31/24 AT APPROXIMATELY 15:00, A MEASUREMENT TECH NOTICED A CRUDE SMELL AT THE SOUR LAKE STATION, PERFORMED AN AREA WALK THROUGH AND DISCOVERED CRUDE OIL ON THE SURFACE ABOVE THE PIPING IN THE AREA OF TANK 721. THE LINE WAS SHUT IN AND ISOLATED. THE AREA WAS EXCAVATED AND IT WAS IDENTIFIED THAT THE FAILURE OCCURRED ON A SECTION OF ""DEAD LEG"" PIPING. THE LEAK WAS COMING FROM A PINHOLE AT THE 6 O'CLOCK POSITION. THE SEGMENT WAS DRAINED AND TWO SKILLET BLINDS WERE INSTALLED. 2 BARRELS OF CRUDE OIL WAS RELEASED. CONTRACTORS CLEANED UP FREE PRODUCT AND REMEDIATED IMPACTED SOIL. THE CAUSE OF THE ACCIDENT WAS DETERMINED TO BE FROM INTERNAL CORROSION. TO PREVENT REOCCURRENCE, THE LINE SEGMENT WAS DE-INVENTORIED AND REMAINS ISOLATED INDEFINITELY. PIPING MODIFICATIONS TO THE MANIFOLD ARE PLANNED TO PERMANENTLY REMOVE THE DEAD LEG.

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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