"ONEOK ROCKIES MIDSTREAM, LLC"

gas_transmission Incident — — November 13, 2025

Incident Information

Incident DateNovember 13, 2025
Operator"ONEOK ROCKIES MIDSTREAM, LLC"
CommodityNATURAL GAS
Pipeline Typegas_transmission

Location

State
Coordinates48.29207, -103.56041

Cause

CauseMATERIAL FAILURE OF PIPE OR WELD
SubcauseORIGINAL MANUFACTURING-RELATED (NOT GIRTH WELD OR OTHER WELDS FORMED IN THE FIELD)

Casualties

Fatalities0
Injuries0

Costs

Property Damage$4,000
Emergency Response$0
Other Costs$1,800

Location Map

Incident Narrative

"ON NOVEMBER 13, 2025, ONEOK GAS CONTROL REPORTED A PRESSURE DROP ON THE 16-INCH STEEL TYPE C EAST FORK DISCHARGE PIPELINE. AN OPERATOR RESPONDED TO EAST FORK COMPRESSOR STATION FOR AN EMERGENCY SHUTDOWN (ESD). A SECOND OPERATOR WAS DISPATCHED TO ISOLATE THE PIPELINE AT A NEARBY BLOCK VALVE. THE PIPELINE WAS ISOLATED, AND OPERATIONS CONFIRMED THE RELEASE LOCATION. THE AREA AROUND THE POINT OF RELEASE WAS BARRICADED TO PREVENT ENTRY. WE DEEMED A REPORTABLE EVENT HAD OCCURRED. THE DAMAGED PIPE MATERIAL WAS SENT FOR METALLURGICAL ANALYSIS. THERE WERE REPAIRS MADE TO THE AFFECTED SECTION. THE PIPELINE OPERATING PRESSURE WAS DE-RATED PENDING ANALYSIS RESULTS. A SUPPLEMENTAL WILL BE SUBMITTED WAS ONCE RESULTS FROM THE INVESTIGATION HAVE BEEN RECEIVED AND REVIEWED. SUPPLEMENTAL- THE RESULTS OF THE METALLURGICAL ANALYSES REVEALED THAT THE IN-SERVICE FAILURE WAS ASSOCIATED WITH LATENT MECHANICAL DAMAGE ON THE PIPE BODY. THE FAILURE ORIGINATED WITHIN A GOUGE THAT WAS 1.7 FEET LONG AT AN ORIENTATION OF 7:30. SHEAR CRACKS DEVELOPED IN THE GOUGE WHICH ULTIMATELY CAUSED THE FAILURE. THE SOURCE OF THE GOUGE IS UNKNOWN."

About This Pipeline Incident

Pipeline incident data is reported to the Pipeline and Hazardous Materials Safety Administration (PHMSA). All significant incidents involving fatalities, injuries, or property damage over $50,000 must be reported.

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