Consumer Safety Complaints
Search 2,192,899 safety complaints filed by vehicle owners with NHTSA — including 137,559 crashes, 55,854 fires, and 8,555 deaths.
Showing 27,958 complaints for BUICK
BUICK
PARK AVENUE
(2001) — ELECTRICAL SYSTEM
Oct 17, 2014
Incident date: Jun 8, 2014
DRIVING DOWN THE EXPRESSWAY, THE CAR JUST SHUT OFF. MY DAUGHTER WAS ABLE TO GET IT TO THE SIDE OF THE ROAD WITHOUT WRECKING (LUCKILY), IT WOULD NOT RESTART, WE HAD THE CAR TOWED. THE CODE READER INDICATED A PROBLEM WITH THE ANTI-THEFT SYSTEM. IF YOU CLEAR THE CODES, OR DISCONNECT THE BATTERY, THE CAR WILL START. THIS HAS HAPPENED MULTIPLE TIMES. MY DAUGHTER HAS LEARNED HOW TO CLEAR CODES WITH... Read more
Incident date: Aug 6, 2014
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. WHILE DRIVING VARIOUS SPEEDS, THE FRONT PASSENGER AIR BAG SENSOR WARNING INDICATOR ILLUMINATED ALTHOUGH THE SEAT WAS OCCUPIED. THE VEHICLE WAS TAKEN TO A DEALER. THE TECHNICIAN DIAGNOSED THAT THE SENSOR NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED, BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 53,2... Read more
Incident date: Oct 19, 2011
THE PASSENGER AIR BAG WARNING LIGHT WILL COME ON WHEN I'M DRIVING AND NO ONE IS EVEN SITTING IN THE PASSENGER SEAT. ANYTHING SITTING ON THE SEAT WEIGHS MUCH LESS THAN THE 80 LBS SPECIFIED IN THE MANUAL. SOMETIMES THE LIGHT WILL COME ON WHEN I HAVE A PASSENGER SITTING THERE, INDICATING THAT THE AIR BAGS ARE OFF - WHEN THEY SHOULD BE ON!!! THERE IS NO EVENT THAT CONSISTENTLY TRIGGERS THE LIGHT COM... Read more
Incident date: Aug 13, 2014
AT AROUND 70 MPH THE DOORS UNLOCK AND LOCK AND THE TRANSMISSION SHIFTS TO NEUTRAL CAUSING THE ENGINE TO OVER REV. *TR
Incident date: Aug 13, 2014
AT AROUND 70 MPH THE DOORS UNLOCK AND LOCK AND THE TRANSMISSION SHIFTS TO NEUTRAL CAUSING THE ENGINE TO OVER REV. *TR
Incident date: Oct 16, 2014
THE INFAMOUS GENERAL MOTORS IGNITION-SWITCH RECALL AFFECTING MY CAR EVIDENTLY DOES NOT INVOLVE REPLACING THE DEFECTIVE SWITCH, BUT INSTALLING INSERTS IN THE BASE OF THE KEY, ACCORDING TO THE SERVICE DEPARTMENT AT THE BUICK DEALER WHERE I BOUGHT THE CAR. THE INSERT CLOSES THE OBLONG HOLE AND LEAVES A SMALL ROUND HOLE; THIS PREVENTS PEOPLE FROM HANGING TOO MUCH STUFF ON THE KEY, WHICH CAN CAUSE THE ... Read more
Incident date: Oct 16, 2014
NO INCIDENT/ACCIDENT. I RECEIVED A NOTICE IN THE MAIL IN AUGUST TO RECALL MY BUICK. I AM GETTING NERVOUS AS IT'S NOW OCTOBER AND NO "SECOND LETTER" TO SCHEDULE REPAIR. WHAT'S UP?! *TR
Incident date: Sep 8, 2014
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. THE CONTACT STATED THAT WHILE MAKING A LEFT TURN, THE STEERING WHEEL SEIZED. AS A RESULT, THE VEHICLE CRASHED INTO A CURB. A POLICE REPORT WAS FILED AND THERE WERE NO INJURIES REPORTED. THE VEHICLE WAS TOWED TO A DEALER. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 102,000.
Crash
Incident date: Oct 9, 2014
TL* THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN ID NUMBER: 14V355000 (ELECTRICAL) AND THE PART WAS NOT AVAILABLE FOR THE RECALL REPAIR. THE CONTACT TOOK THE VEHICLE TO THE DEALER AFTER SCHEDULING AN APPOINTMENT WHERE THEY DID NOT HAVE AN APPROXIMATE DATE FOR THE PARTS TO BE AVAILABLE. THE MANUFACTURER WAS CONTACTED AND WAS UNABLE TO PROVIDE AN ESTIMA... Read more
Incident date: Oct 16, 2014
BACKGROUND - I JUST WENT THROUGH THE IGNITION RECALL ON MY 2007 CHEVROLET COBALT. THE IGNITION SWITCH WAS REPLACED AND I AM COMFORTABLE DRIVING THE CAR NOW. THEN I RECEIVED RECALL 14299 ON MY 2011 BUICK LUCERNE (NHTSA CAMPAIGN ID 14V355) INVOLVING A SIMILAR IGNITION ISSUE. IT ALSO MENTIONED THE WEIGHT ISSUE OF ITEMS HANGING ON THE KEY CAUSING LOSS OF ENGINE POWER, BRAKING, ETC. THE RECALL PROV... Read more
Incident date: Sep 17, 2014
RECENTLY, THE VEHICLE HAS STARTED SHUTTING OFF WHILE DRIVING. ON SEPTEMBER 13, 2014, WHILE DRIVING THE VEHICLE, THE "SERVICE BATTERY CHARGING SYSTEM" LIGHT CAME ON. I IMMEDIATELY CONTACTED THE DEALERSHIP, WHICH INSTRUCTED ME TO BRING THE VEHICLE IN. WHEN I DROPPED THE VEHICLE OFF AT THE DEALERSHIP, THE SERVICE TECHNICIAN SAW THE SERVICE LIGHT. THE DEALERSHIP INSPECTED THE VEHICLE OVER THE NEXT ... Read more
Incident date: Oct 1, 2014
2005 BUICK LACROSSE. CONSUMER WRITES IN REGARDS TO IGNITION KEY AND BRAKE PADS RECALL NOTICES. *SMD THE CONSUMER STATED THE ROTORS WERE MADE OF POOR MATERIAL. WHICH RESULTED IN PREMATURE WARPING. JUST PRIOR TO PURCHASING THE VEHICLE, THE DEALER CLAIMED THEY REPLACED ALL OF THE BRAKES. HOWEVER, A FEW WEEKS LATER, SOMETHING CAUSE THE CONSUMER TO BRAKE HARD, AND THAT ACTION CAUSED THE STEERING WHE... Read more
Incident date: Oct 1, 2014
2005 BUICK LACROSSE. CONSUMER WRITES IN REGARDS TO IGNITION KEY AND BRAKE PADS RECALL NOTICES. *SMD THE CONSUMER STATED THE ROTORS WERE MADE OF POOR MATERIAL. WHICH RESULTED IN PREMATURE WARPING. JUST PRIOR TO PURCHASING THE VEHICLE, THE DEALER CLAIMED THEY REPLACED ALL OF THE BRAKES. HOWEVER, A FEW WEEKS LATER, SOMETHING CAUSE THE CONSUMER TO BRAKE HARD, AND THAT ACTION CAUSED THE STEERING WHE... Read more
Incident date: Oct 23, 2003
THE DASH PAD HAS SEPARATED FROM THE DASHBOARD. *TR
Incident date: Oct 14, 2014
WHILE DRIVING AT DARK LOW BEAM HEADLIGHTS SHUT OFF. HIGH BEAM STILL WORKED. AFTER SEVERAL MINUTES LOW BEAMS STARTED WORKING AGAIN. THIS HAS HAPPENED TO ME 3 TIMES NOW. *TR
Incident date: Oct 14, 2014
WHILE DRIVING AT DARK LOW BEAM HEADLIGHTS SHUT OFF. HIGH BEAM STILL WORKED. AFTER SEVERAL MINUTES LOW BEAMS STARTED WORKING AGAIN. THIS HAS HAPPENED TO ME 3 TIMES NOW. *TR
Incident date: Mar 20, 2014
DRIVING WESTBOUND ON ILLINOIS RT-7 TOWARDS LOCKPORT, ILLINOIS WHEN VEHICLE WENT OUT OF CONTROL AND INTO ONCOMING LANE NEARLY CAUSING A HEAD-ON COLLISION. UPON INSPECTION, IT WAS DETERMINED THAT THE FRONT STRUTS RUSTED THROUGH AT THE MOUNTING FLANGES WHEREBY THE FRONT SUSPENSION COLLAPSED FALLING DOWN ON THE LEFT FRONT TIRE DESTROYING THE NEW MICHELIN TIRE THROWING THE CAR OUT OF CONTROL AND INTO ... Read more
Incident date: Aug 4, 2014
TL* THE CONTACT OWNS A 2009 BUICK LUCERNE. WHILE DRIVING 70 MPH, THE VEHICLE STALLED WITHOUT WARNING. THE CONTACT WAS ABLE TO RESTART THE VEHICLE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE CONTACT RECEIVED A RECALL NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM); HOWEVER, THE PARTS NEEDED FOR THE REPAIR WERE NOT AVAILABLE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. TH... Read more
Incident date: Oct 2, 2014
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. THE CONTACT STATED THAT THE VEHICLE FAILED TO START. AFTER INSPECTING THE VEHICLE, THE CONTACT NOTICED SMOKE COMING FROM THE FUSE BOX. THE FUSES WERE MELTED AND BURNED. THE VEHICLE WAS TOWED TO THE DEALER. THE TECHNICIAN DIAGNOSED THAT THE FUSE BOX HOUSING AND FUSES NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED AND THE MANUFACTURER WAS NOTIFIED. TH... Read more
Fire
Incident date: Oct 1, 2014
2005 BUICK LACROSSE. CONSUMER WRITES IN REGARDS TO SAFETY RECALL REPAIRS. *TGW THE IGNITION SWITCH WAS REPLACED. *JB
BUICK
RENDEZVOUS
(2003) — FUEL SYSTEM, OTHER
Oct 14, 2014
Incident date: Oct 9, 2014
FILLED TANK AND PARKED IN GARAGE. NEXT MORNING GARAGE HAD EXTREMELY STRONG GASOLINE FUMES. BACKED CAR INTO DRIVEWAY. FOUND FUEL ON GARAGE FLOOR. IT WAS RUNNING OUT OF THE TANK AT THE JUNCTION OF THE FUEL LINE TO THE GAS TANK. IT APPEARED TO BE THE SEAL BETWEEN THE FUEL LINE (WHERE THE GAS RUNS DOWN INTO THE TANK WHEN YOU FILL IT) AND THE TANK, THE INTAKE VALVE. THE LEAK WAS SEVERE AND DANGEROUS, T... Read more
Incident date: Oct 14, 2014
TL* THE CONTACT OWNS A 2011 BUICK ENCLAVE. THE CONTACT RECEIVED A RECALL NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 14V266000 (SEAT BELTS); HOWEVER, THE PARTS NEEDED FOR THE REPAIR WERE UNAVAILABLE. THE DEALER WAS UNCERTAIN WHEN THE PARTS WOULD BECOME AVAILABLE TO SERVICE THE VEHICLE. THE MANUFACTURER WAS NOTIFIED. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Aug 13, 2014
ON AUG 13 I NOTICED THAT I WAS HAVING ISSUES STARTING MY 2004 BUICK REGAL. ON AUG 25 I HAD MY 2004 BUICK REGAL TOWED TO GATEWAY BUICK GMC AT 11438 LBJ FWY, DALLAS, TX DUE TO THE CAR IMMEDIATELY SHUTTING OFF AFTER STARTING IT AND SHUTTING OFF WHILE DRIVING. THE MECHANICS DETERMINED THAT IT WAS DUE TO WIRING IN THE ENGINE HARNESS THAT SHORTED OUT THE BATTERY AND ALSO DAMAGED THE CAMSHAFT AND THE CRA... Read more
Incident date: Aug 1, 2014
TL* THE CONTACT OWNS A 2008 BUICK LUCERNE. THE CONTACT RECEIVED A RECALL NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM); HOWEVER, THE PARTS NEEDED TO REPAIR THE VEHICLE WERE NOT AVAILABLE. THE DEALER STATED THAT THE CONTACT HAD TO WAIT FOR THE SECOND RECALL NOTIFICATION. THE SECOND NOTIFICATION WAS RECEIVED, BUT THE PARTS WERE STILL NOT AVAILABLE. THE MANUFACTURER WAS MADE A... Read more
Incident date: Oct 10, 2014
MY WIFE WAS TAKING HER FATHER TO THE HOSPITAL WHEN SHE THE LOW BEAM HEADLIGHTS WERE TO COME ON THEY DID NOT. SHE HAD TO DRIVE THE REST OF THE WAY WITH ONLY HER PARKING LIGHTS ON. THIS IS NOT THE FIRST TIME THIS HAS HAPPENED IN 2013 WE HAD TO REPLACE A RELAY UNDER THE HOOD IN THE FUSE BOX FOR THE SAME ISSUE. THIS TIME WE TOOK IT INTO OUR LOCAL PARTS SHOP TO REPLACE THE RELAY AND FOUND OUT THAT THE ... Read more
Incident date: Oct 10, 2014
MY WIFE WAS TAKING HER FATHER TO THE HOSPITAL WHEN SHE THE LOW BEAM HEADLIGHTS WERE TO COME ON THEY DID NOT. SHE HAD TO DRIVE THE REST OF THE WAY WITH ONLY HER PARKING LIGHTS ON. THIS IS NOT THE FIRST TIME THIS HAS HAPPENED IN 2013 WE HAD TO REPLACE A RELAY UNDER THE HOOD IN THE FUSE BOX FOR THE SAME ISSUE. THIS TIME WE TOOK IT INTO OUR LOCAL PARTS SHOP TO REPLACE THE RELAY AND FOUND OUT THAT THE ... Read more
Incident date: Oct 6, 2014
HAD TO REMOVE DOME LIGHT BULBS BEAUSE IT DOESNT TURN OFF, THE LIGHTS ON THE REAR ST TIMES AND I'V JUST BOUGHT A SECOND BATTERY 3 DAYS AGO BECAUSE THE LIGHTING PROBLEM CAUES THEM TO BURN OUT. SOMETIMES THE LIGHTS WILL FADE OUT. MST TIME IT DOESNT AND I CAN'T TURN THEM OFF MANUALLY EITHER. JUST FOUND OUT ABOUT THE RECALLS ON THIS VEHICLE. *TR
Incident date: Oct 6, 2014
HAD TO REMOVE DOME LIGHT BULBS BEAUSE IT DOESNT TURN OFF, THE LIGHTS ON THE REAR ST TIMES AND I'V JUST BOUGHT A SECOND BATTERY 3 DAYS AGO BECAUSE THE LIGHTING PROBLEM CAUES THEM TO BURN OUT. SOMETIMES THE LIGHTS WILL FADE OUT. MST TIME IT DOESNT AND I CAN'T TURN THEM OFF MANUALLY EITHER. JUST FOUND OUT ABOUT THE RECALLS ON THIS VEHICLE. *TR
Incident date: Oct 12, 2014
WHEN I BOUGHT THE CAR LAST YEAR THE DEALER TOOK $1900 OF MY MONEY IN A RUSE - I WILL DIE BEFORE EVER STEPPING FOOT IN [XXX] EVER AGAIN. I WILL NOT TAKE THIS VEHICLE IN FOR ANY SAFETY RECALL. INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR
Incident date: Oct 10, 2014
AS THE 2008 BUICK ENCLAVE VEHICLE WAS SLOWED TO MAKE A RIGHT TURN INTO A DRIVEWAY, IT SUDDENLY AND UNEXPECTEDLY BECAME VERY, VERY DIFFICULT TO STEER, SUCH THAT THE VEHICLE ALMOST WENT OFF OF THE ROAD AND INTO A TELEPHONE POLE. FORTUNATELY, THE VEHICLE WAS GOING SLOWLY ENOUGH THAT IT COULD BE ABRUPTLY STOPPED IN THE MIDDLE OF THE ROAD AND IT WAS NOT REAR-ENDED. THIS IS A VERY DANGEROUS CONDITION. W... Read more
Incident date: Sep 27, 2014
TL* THE CONTACT OWNS A 2007 BUICK LACROSSE. WHILE DRIVING 40 MPH, THE ENGINE STALLED. THE CONTACT SHIFTED INTO NEUTRAL AND WAS ABLE TO RESTART THE VEHICLE. THE FAILURE OCCURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE CONTACT RECEIVED A RECALL NOTICE FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM) AND STATED THAT THE PART NEEDED TO REMEDY THE VEHICLE WAS UNAVA... Read more
Incident date: Sep 27, 2014
TL* THE CONTACT OWNS A 2007 BUICK LACROSSE. WHILE DRIVING 40 MPH, THE ENGINE STALLED. THE CONTACT SHIFTED INTO NEUTRAL AND WAS ABLE TO RESTART THE VEHICLE. THE FAILURE OCCURRED ON NUMEROUS OCCASIONS. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE CONTACT RECEIVED A RECALL NOTICE FOR NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM) AND STATED THAT THE PART NEEDED TO REMEDY THE VEHICLE WAS UNAVA... Read more
Incident date: Sep 26, 2014
TL* THE CONTACT OWNS A 2008 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM) HOWEVER, THE PART TO DO THE RECALL WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Oct 10, 2014
TL* THE CONTACT OWNS A 2005 BUICK LACROSSE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM) AND STATED THAT THE PART NEEDED WAS UNAVAILABLE TO SERVICE THE VEHICLE UNDER THE RECALL. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Oct 9, 2014
TL* THE CONTACT OWNS A 2006 BUICK LUCERNE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN: 14V355000 (ELECTRICAL SYSTEM). HOWEVER, THE PARTS NEEDED WERE UNAVAILABLE. THE DEALER WAS UNCERTAIN WHEN THE PARTS WOULD BECOME AVAILABLE TO SERVICE THE VEHICLE UNDER THE RECALL. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM. THE CONTACT HAD NOT EXPERIENCED A FAILURE. THE VIN WAS NOT AVAILABLE.
Incident date: Jul 7, 2014
TL* THE CONTACT OWNS A 2014 BUICK ENCLAVE. THE CONTACT RECEIVED A NOTIFICATION FOR NHTSA CAMPAIGN 14V266000 (SEAT BELTS). HOWEVER, THE DEALER COULD NOT PERFORM THE REPAIRS FOR THREE MONTHS BECAUSE THE PARTS WERE NOT AVAILABLE. THE MANUFACTURER WAS MADE AWARE OF THE ISSUE. THE VEHICLE HAD NOT EXPERIENCE THE FAILURE.
Incident date: Jul 31, 2014
I RECEIVED A RECALL NOTICE 14V355 FOR THE IGNITION SWITCH. PARTS WERE NOT AVAILABLE AT THE TIME I RECEIVED THE NOTICE. IT'S BEEN TWO MONTHS SINCE I RECEIVED THE NOTICE. COVERT AUTO GROUP IN AUSTIN TX SAYS THERE ARE STILL NO PARTS AVAILABLE. I BELIEVE IT'S TAKING TOO LONG TO RESOLVE THIS UNSAFE CONDITION. *TR
Incident date: Jul 31, 2014
I RECEIVED A RECALL NOTICE 14V355 FOR THE IGNITION SWITCH. PARTS WERE NOT AVAILABLE AT THE TIME I RECEIVED THE NOTICE. IT'S BEEN TWO MONTHS SINCE I RECEIVED THE NOTICE. COVERT AUTO GROUP IN AUSTIN TX SAYS THERE ARE STILL NO PARTS AVAILABLE. I BELIEVE IT'S TAKING TOO LONG TO RESOLVE THIS UNSAFE CONDITION. *TR
Incident date: Oct 8, 2014
TL* THE CONTACT OWNS A 2009 BUICK LACROSSE. THE CONTACT RECEIVED A NOTIFICATION FOR RECALL NHTSA CAMPAIGN NUMBER: 14V355000 (ELECTRICAL SYSTEM). HOWEVER, THE PARTS NEEDED WERE UNAVAILABLE. THE DEALER WAS UNCERTAIN WHEN THE PARTS WOULD BECOME AVAILABLE TO SERVICE THE VEHICLE UNDER THE RECALL. THE MANUFACTURER WAS NOTIFIED OF THE PROBLEM AND THEY STATED THAT THE PARTS SHOULD HAVE BEEN AVAILABLE.... Read more
Incident date: Oct 9, 2014
TL* THE CONTACT OWNS A 2006 BUICK LACROSSE. THE CONTACT RECEIVED A RECALL NOTIFICATION OF NHTSA CAMPAIGN ID NUMBER: 14V355000 (ELECTRICAL SYSTEM). HOWEVER, THE PART NEEDED WAS UNAVAILABLE TO PERFORM THE REPAIR. THE MANUFACTURER WAS NOT NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE.
Incident date: Aug 26, 2014
IN A LINE OF TRAFFIC GETTING READY TO MAKE A LEFT TURN AND WITHOUT WARNING, THE ENGINE RACED CAUSING THE CAR TO ACCELERATE AND SLAM INTO THE REAR OF ANOTHER CAR CAUSING OVER $5K WORTH OF DAMAGE TO THE ENCORE. THE AIR BAGS DID NOT GO OFF. THE IMPACT WAS SO INTENSE THAT THE REAR GLOVE BOX OPENED TOSSING THE CONTENTS OUT INTO THE TRUNK. *TR
Crash
1 injured
Incident date: Aug 26, 2014
IN A LINE OF TRAFFIC GETTING READY TO MAKE A LEFT TURN AND WITHOUT WARNING, THE ENGINE RACED CAUSING THE CAR TO ACCELERATE AND SLAM INTO THE REAR OF ANOTHER CAR CAUSING OVER $5K WORTH OF DAMAGE TO THE ENCORE. THE AIR BAGS DID NOT GO OFF. THE IMPACT WAS SO INTENSE THAT THE REAR GLOVE BOX OPENED TOSSING THE CONTENTS OUT INTO THE TRUNK. *TR
Crash
1 injured
Incident date: Aug 26, 2014
IN A LINE OF TRAFFIC GETTING READY TO MAKE A LEFT TURN AND WITHOUT WARNING, THE ENGINE RACED CAUSING THE CAR TO ACCELERATE AND SLAM INTO THE REAR OF ANOTHER CAR CAUSING OVER $5K WORTH OF DAMAGE TO THE ENCORE. THE AIR BAGS DID NOT GO OFF. THE IMPACT WAS SO INTENSE THAT THE REAR GLOVE BOX OPENED TOSSING THE CONTENTS OUT INTO THE TRUNK. *TR
Crash
1 injured
Incident date: Sep 2, 2014
TL* THE CONTACT OWNS A 2005 BUICK LACROSSE. THE CONTACT STATED THAT WHILE DRIVING A VARIOUS SPEEDS, THE POWER STEERING SENSOR LIGHT ILLUMINATED AS THE POWER STEERING MALFUNCTIONED CAUSING THE STEERING WHEEL TO BECOME VERY DIFFICULT TO TURN. THE VEHICLE WAS TAKEN TO THE DEALER. THE TECHNICIAN DIAGNOSED THAT THE POWER STEERING WAS FAULTY. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE FAILURE... Read more
Incident date: Oct 4, 2014
TL* THE CONTACT OWNS A 2006 BUICK LUCERNE. THE CONTACT STATED WHILE DRIVING APPROXIMATELY 65 MPH, A SQUEAKING SOUND EMITTED FROM THE FRONT END OF THE VEHICLE. THE CONTACT DISCOVERED THAT THE POWER STEERING HOSE EXHIBITED A HOLE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 55,000.
Incident date: Aug 16, 2014
MY FAMILY AND I WERE ON OUR WAY BACK TO WISCONSIN FROM A TRIP TO FLORIDA ON SATURDAY, AUGUST 16, 2014. MY HUSBAND HAD EXITED THE INTERSTATE AND WAS PULLING INTO A PARKING SPACE AT A FAST FOOD RESTAURANT. THE SPACE WAS ON A SLIGHT INCLINE. AS HE PULLED INTO THE SPACE, THE ENCLAVE STARTED TO ROLL BACKWARD. I CHECKED THE POSITION OF THE GEARSHIFT THINKING THAT HE HAD ACCIDENTALLY SHIFTED INTO NEU... Read more
Incident date: Jun 2, 2014
TL* THE CONTACT OWNS A 2005 BUICK LACROSSE. THE CONTACT STATED THAT WHILE DRIVING, THE LOW BEAM HEADLIGHTS SHORTED AND TURNED OFF ON SEVERAL OCCASIONS. THE VEHICLE WAS TAKEN TO A REPAIR SHOP. THE TECHNICIAN DIAGNOSED THAT THE RELAY SWITCH AND WIRING NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAG... Read more
Incident date: Jun 2, 2014
TL* THE CONTACT OWNS A 2005 BUICK LACROSSE. THE CONTACT STATED THAT WHILE DRIVING, THE LOW BEAM HEADLIGHTS SHORTED AND TURNED OFF ON SEVERAL OCCASIONS. THE VEHICLE WAS TAKEN TO A REPAIR SHOP. THE TECHNICIAN DIAGNOSED THAT THE RELAY SWITCH AND WIRING NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED BUT THE FAILURE RECURRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAG... Read more
Incident date: Jun 18, 2012
RIGHT FRONT PASSENGER SEAT AIRBAG TURNS ITSELF OFF INTERMITTENTLY WITH PASSENGER SEATED AND BUCKLED. DEALER REMOVED AND REINSTALLED SEAT AND REPLACED FAULTY PPS MODULE AND CUSHION ASSEMBLY 06/18/2012, 48,072 MILES. PROBLEM RECURRED, DEALER REZEROED SYSTEM AND RECHECKED OK, 02/20/13, 62,481 MILES. PROBLEM RECURRED, DEALER REPLACED PPS SENSOR 03/13/2013, 63,441 MILES. PROBLEM IS NOW RECURRING 10/0... Read more
Incident date: Aug 15, 2014
TL* THE CONTACT OWNS A 2011 BUICK REGAL. THE CONTACT RECEIVED A NOTIFICATION FOR NHTSA CAMPAIGN NUMBER: 14V447000 (SEATS). HOWEVER, THE PART NEEDED WAS UNAVAILABLE TO PERFORM THE REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PAM UPDATED 11/20/14*LJ UPDATED 02/03/15